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railroad_incidents_analysis.csv
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railroad_incidents_analysis.csv
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,IYR,IMO,RAILROAD,STATE,STATION,COUNTY,NARR,STRUCK,DERAIL,OTHER,HAZMAT,DAMAGE,damages_total
0,19,11,ATK,6,CASTROVILLE,MONTEREY,"CAMERA-EQUIPPED TRAIN 14 STRUCK AN OCCUPIED SANITATION TRUCK AT MP 110.68, A PRIVATE RD CROSSING. T HE OCCUPANT OF THE VEHICLE WAS A CONFIRMED FATALITY.",True,False,False,False,False,0.0
1,19,10,MNCW,9,NORWALK,FAIRFIELD,"PRODUCTION GANG, TRAVELING NORTH WITH 22 PIECES OF EQUIPMENT, HAD 7 SEPERATE PIECES OF EQUIPMENT MAK E IMPACT WITH ONE ANOTHER.",False,False,True,False,False,0.0
2,19,4,FEC,12,POMPANO BEACH,BROWARD,BLF 604 WAS TRAVELING SOUTHBOUND ON EAST MAIN AT APPROXIMATELY 79 MPH AND NOTICED A TRESPASSER COMIN G ACROSS THE TRACKS WITH HIS BIKE FROM THE WEST SIDE OF THE TRACKS TO THE EAST SIDE OF THE TRACKS. LOCOMOTIVE ENGINEER SOUNDED HORN AND BELL TO WARN TRESPASSER AND PLACED TRAIN INTO EMERGENCY. TRESP ASSER WAS STRUCK RESULTING IN A FATALITY. BLF COSTS WERE $15325.,True,False,False,False,False,15325.0
3,19,4,FEC,12,POMPANO BEACH,BROWARD,BLF 606 WAS TRAVELING SOUTHBOUND ON EAST MAIN AND NOTICED A VEHICLE FOULING HAMMONDVILLE ROAD. LOCO MOTIVE ENGINEER SOUNDED HORN AND BELL AND PLACED TRAIN IN EMERGENCY. TRAIN STRUCK VEHICLE AND PASSE NGERS IN VEHICLE WERE TRANSPORTED TO LOCAL HOSPITAL WITH MINOR INJURIES. BLF COSTS WERE $10793.,True,False,False,False,False,10793.0
4,19,4,CSX,12,SEVILLE,VOLUSIA,AMTRAK P09811 STRUCK SEMI AT PRIVATE CROSSING.,True,False,False,False,False,0.0
5,19,9,BLF,12,WEST PALM BEACH,PALM BEACH,BLF 605 TRAVELING NB ON THE WEST MAIN TRACK STRUCK A VEHICLE AT WESTWOOD RD MP 300.76. VEHICLE WENT AROUND LOWERED GATES THAT WERE WORKING AS INTENDED. TRAIN STRUCK THE VEHICLE AND ENGINEER PLACED T RAIN INTO EMERGENCY CAUSING IMPACT AND FATALITY TO DRIVER. FEC DAMAGE: $615.33,True,False,False,False,True,615.33
6,19,2,IANR,19,WATERLOO,BLACK HAWK,"FEBRUARY 13, 2019
AT APPROXIMATELY 0001, A CREW OPERATING A NORTHBOUND LITE ENGINE CONSIST (7 LOC OMOTIVES) APPROACHED THE SOUTH NEW LEAD SWITCH AT BRYANT YARD WITH THE INTENT OF STOPPING TO LINE TH E SWITCH IN ORDER TO PROCEED TOWARD TRACK 6. AS THE ENGINEER APPLIED THE INDEPENDENT BRAKES TO THE C ONSIST, NO BRAKING EFFECT OCCURRED DUE TO SNOW BUILD UP ON THE BRAKE SYSTEM APPARATUS. AS A RESULT O F NOT BEING ABLE TO STOP, THE ENGINE CONSIST COLLIDED WITH A SECOND SET OF LITE ENGINES (4 LOCOMOTIV ES) SITTING ON THE MAIN TRACK. THE COLLISION CAUSED THE RAIL TO SPREAD AND SUBSEQUENTLY DERAILED LEA DING LOCOMOTIVE AND ONE LOCOMOTIVE IN SECOND CONSIST.
THE BRAKING EFFECT WAS NOT ACHIEVED DUE TO BRAKE APPARATUS NOT BEING CONDITIONED PRIOR TO THE BRAKE APPLICATION.",False,True,False,False,False,0.0
7,19,1,BNSF,19,KEOKUK,LEE,KJRY CREW WAS SHOVING INTO YARD FROM BNSF MAIN TRACK WHEN ICE AND SHOW BUILDUP IN THE CROSSING CAUSE D THE CARS TO DERAIL. CARS DERAILED ON BNSF MAINLINE.,False,True,False,False,False,0.0
8,19,4,UP,19,CHARITON,LUCAS,"TRAIN MDMEW-08 AT MP 23.1 WENT INTO EMERGENCY. AFTER TRAIN WAS STOPPED, IT WAS DISCOVERED THAT CAR TILX635869 HAD ONE SET OF TRUCKS ON THE GROUND DUE TO SOFT SUBGRADE IN THE SPIRAL OF A CURVE.",False,False,True,False,False,0.0
9,19,4,BNSF,19,ALBIA,MONROE,X-BVAEDY5-13 DERAILED 3 RAILCARS WHILE SHOVING INDUSTRY TRACK 2320 DUE TO IMPROPER INSTRUCTIONS TO T RAIN CREW. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
10,19,1,EIRR,16,REXBURG,MADISON,"AT APPROXIMATELY 13:00 ON 1/30/2019, THE EAST BELT CREW WAS TRAVELLING NEAR MP 27.5 ON THE EAST BELT SUBDIVISION WHEN THEY ENCOUNTERED DEEP SNOW DRIFTS ACROSS THE MAIN LINE. THE CREW CUT AWAY FROM TH EIR TRAIN TO PROCEED AHEAD TO CLEAR A PATH THROUGH THE DRIFTS WHEN THEY DERAILED ON A PRIVATE CROSSI NG NEAR MP 27.23. AFTER COMING TO A STOP THE LOCOMOTIVE PROCEEDED TO ROLL OVER ON THE ENGINEER'S SI DE.",False,True,False,False,False,0.0
11,19,3,UP,17,MELROSE PARK,COOK,"YPR20R-21 DERAILED 2 RAILCARS IN BOWL TRACK 6. CGCX20382 SUSTAINED DAMAGE TO THE B-END CROSSOVER, I T WAS BENT DUE TO HARD IMPACT FROM ARMN933921. ARMN933921 HAD A -END MINOR DERAIL AND COMPLETE DEST RUCTION OF SLIDING SILL. WEPX3668 - A/B MINOR DERAIL. THE B-END COUPLER IS BROKEN TO INCLUDE END SILL DAMAGE.",False,True,False,False,True,0.0
12,19,4,BNSF,17,MENDOTA,LA SALLE,AMTRAK REPORTED THAT THEY HAD A TRACK MOTOR FIRE ON THE LEAD LOCOMOTIVE. LOCAL FIRE PERSONAL WERE D ISPATCHED TO EXTINGUISH.,False,False,True,False,False,0.0
13,19,5,UP,17,MELROSE PARK,COOK,MPRWN-23 DERAILED CN625795 AND CNIS623242 WHILE PULLING WEST AND RERAILED ONCE IT HIT THE FROG.,False,True,False,False,False,0.0
14,19,5,UP,17,MELROSE PARK,COOK,"THE YPR26R-24 JOB WAS SHOVING SOUTH WITH 2 LOCOMOTIVES AND 101 CARS FROM TRACK 27 TOWARDS THE HUMP W HEN 6 CARS DERAILED, CAUSING DAMAGE TO 2 MORE CARS IN TRACK 28.",False,True,False,False,True,0.0
15,19,1,GRW,18,GARY,LAKE,"AT 2259HRS THE 2230HMRCL31 ASSIGNMENT, OPERATING THE GRW 318 WITH A SINGLE RCO OPERATOR WAS IN THE P ROCESS OF PULLING THE LOADS FROM #14BF. THE RCO HAD TIED ONTO THE IL171 AND IL 155 ON THE LOAD TRACK AT #14BF. THE RCO WAS INSTRUCTED TO DELIVER THE LOADED LADLES TO THE QBOP.
AS THE RCO PULLED OUT OF THE LOAD TRACK AND ACROSS THE ROAD WAY THE GRW 318 AND IL 171 DERAILED. THE IL 155 WAS THE REAR L ADLE AND REMAINED ON THE TRACK AT THE TIME. THE FRONT SET OF TRUCKS ON THE GRW 318 AND IL 171 DERAIL ED. THE RCO WAS POSITIONED ON THE POINT OF HIS GRW 318 WHEN HE FELT THE LOCOMOTIVE BOUNCE AND THEN C OME TO A HALT. THE RCO IMMEDIATELY PUT HIS ENGINE IN STOP AS SOON AS HE COULD. RCO NOTIFIED THE SCAL ES YARDMASTER THAT HE HAD DERAILED AT 2259HRS.",False,True,False,False,False,0.0
16,19,8,NICD,18,GARY,LAKE,PANTOGRAPH GOT ABOVE THE MID SPAN WIRE ALLOWING IT TO GET INTO THE CANTENARY.,False,False,True,False,False,0.0
17,19,8,KCT,20,KANSAS CITY,WYANDOTTE,"CREW ON UP TRAIN MNPINP-19 USING KCT MAIN LINE AS HEAD ROOM TO SET OUT BAD ORDER IN UP ARMOURDALE YA RD, TRAIN PULLED EAST OUT OF ARMOURDALE INBOUND TO KCT MAIN 3. CONDUCTOR MADE CUT AND INSTRUCTED EN GINEER TO PULL EAST TO CLEAR SWITCHES ON LEAD, ENGINEER BROUGHT TRAIN TO STOP USING INDEPENDENT BRAK E CAUSING BUFF FORCES IN THE TRAIN CAUSING MTNR175009 TO DERAIL ON KCT MAIN LINE. KCT MAINTAINS TRA CK AND SIGNAL WITH DAMAGE OF $3900. UP OWNS CONSIST WITH DAMAGE OF $7852. #12 SUBDIVISION NAME IS LS 1001.",False,True,False,False,True,11752.0
18,19,9,BNSF,20,FORT SCOTT,BOURBON,"H-GALTUL9-19 DERAILED 7 RAILCARS IN YARD TRACK 106. AFTER SHOVING THROUGH AN IMPROPERLY LINED SWITCH , SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO CONTROL SHOVE MOVE IN TURN RUN NING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
19,19,5,UP,20,BUFFALO,WILSON,"THE CSACD9-05, LEAD LOCOMOTIVE UP7832, WAS TRAVELING NORTHBOUND NEAR MILE POST 413.5 OF THE COFFEYVI LLE SUBDIVISION WHEN IT DERAILED 19 CARS DUE TO A WASHOUT IN FRONT OF THEM. THE TRAIN WAS PLACED IN TO EMERGENCY BRAKE APPLICATION. CAR# : IAPX 1121 ARGON LIQUID COMPLETE CAR RELEASE AND 199,400 LBS. CAR#: IAPX 1105 ARGON LIQUID COMPLETE RELEASE AND 202,500 LBS.",False,True,False,False,False,0.0
20,19,9,MS,26,NORTH MUSKEGON,MUSKEGON,A LARGE TREE FELL ON A STATIONARY MHLX 15199 RAIL CAR DUE TO HIGH WINDS. THE TREE DAMAGED THE TOP HA TCH AND BENT THE ROOF OF THE HOPPER CAR. THE CAR WAS INSPECTED BY A CARMEN AND HE FOUND IT TO BE IN NEED OF REPAIRS REQUIRING TO BE HOME SHOPPED DUE TO THE AMOUNT OF DAMAGE.,False,False,True,False,True,0.0
21,19,2,ATK,26,KALAMAZOO,KALAMAZOO,"TRAIN 355 OPERATING WITH LOCOMOTIVE E/27 AND 5 CARS STRUCK AN OCCUPIED VEHICLE AT MP 147.70, ELEVENT H STREET CROSSING. THE VEHICLE DROVE AROUND THE GATES AND STOPPED ON THE CROSSING. THERE WERE 3 CO NFIRMED FATALITES IN THE VEHICLE. THE INCIDENT REMAINS UNDER INVESTIGATION.",True,False,False,False,False,0.0
22,19,10,GDLK,26,KALAMAZOO,KALAMAZOO,THE 100 CREW WENT TO PUT A CAR INTO 13 TRACK WHEN THE CARS THEY SET OUT IN 12 ROLLED OUT AND SIDE SW IPED THE CAR THEY WE'RE SETTING OUT INTO 13.,False,False,True,False,False,0.0
23,19,4,ATK,26,DOWAGIAC,CASS,"TRAIN 364 WAS DELAYED DEPARTING DOWAGIAC STATION DUE TO A BATTERY FIRE ON C/54558. ONCE FIRE WAS EX TINGUISHED, THE CREW WAS ABLE TO ISOLATE THE POWER IN C/54558 AND RESTORE HEP ON THE TRAIN.",False,False,True,False,False,0.0
24,19,7,WC,26,MANISTIQUE,SCHOOLCRAFT,AT 1330 EDT ON JULY 31ST TRAIN A45181-31 DERAILED 7 CARS AND THEIR DP UNIT.,False,True,False,False,False,0.0
25,19,2,UP,29,DEXTER,STODDARD,THE ZMQG4-06 WAS IN THROTTLE 2 TRAVELING APPROXIMATELY 20 MPH WHEN TRAIN WENT INTO EMERGENCY. CONDU CTOR WALKED BACK AND FOUND 14 CARS HAD DERAILED. CAUSE OF DERAILMENT WAS DETERMINED TO BE STRAIGHT LINE WIND.,False,True,False,False,False,0.0
26,19,8,CMR,29,ST ALBANS,FRANKLIN,"AT AROUND MP 41 ON A CURVE, FELD STACK AS CREW ROUNDED THE CURVE AND IMMEDIATLY PLACEDS ENGINE IN EM ERGENCY ONCE REALIZED THERE WAS NOT NORMAL SLACK. 6 CARS DERAILED ON THE MAIN IN AN S CURVE. ENGINE ER THEN CUT THE ENGINES AWAY.",False,True,False,False,False,0.0
27,19,4,ATK,28,WESSON,COPIAH,"TRAIN 59 OPERATING WITH LOCOMOTIVE E/139 AND 7 CARS STRUCK AN OCCUPIED UTILITY VAN AT MP 774.37, COL LIER ST CROSSING. THE VEHICLE OPERATED INTO PATH OF THE TRAIN, THROUGH THE CROSSING WITH AMPLE PROT ECTION CAUSING THE VAN TO SPIN AND STRIKE ANOTHER OCCUPIED VEHICLE.",True,False,False,False,False,0.0
28,19,12,BNSF,38,STANLEY,MOUNTRAIL,L-MON8332-08 DERAILED 3 RAILCARS WHILE SHOVING YARD TRACK 6535 DUE TO FAILURE TO CONTROL SHOVE MOVE IN TURN RUNNING THROUGH OVER A DERAIL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
29,19,11,UP,31,GRAND ISLAND,HALL,"LCB53-12 CREW PULLED INTO GRAND ISLAND YARD OFF MAIN 2 AT MP 145. AS THE CREW TRAVERSED DOWN THE EA ST LEAD, THE REAR TRUCKS ON THE REAR LOCOMOTIVE AND FIRST FIVE CARS DERAILED AFTER THE SWITCH BETWEE N 4 AND 718 TRACK. THE CREW WAS LINED PROPERLY ON A FACING POINT SWITCH DOWN 4 TRACK/THE REMAINDER OF THE EAST LEAD. AFTER THE FIRST TWO LOCOMOTIVES PROPERLY CAME OVER THE SWITCH, THE SWITCH OPENED UP DERAILING THE REAR TRUCKS ON THE THIRD LOCOMOTIVE AND THE FIRST FIVE CARS. AFTER INVESTIGATION, IT WAS DETERMINED THAT THE LAST CREW TO OPERATE THE SWITCH WAS A NCRC CREW WORKING IN GRAND ISLAND Y ARD. THE HOOK OF THE SWITCH WAS NOT PLACED INSIDE THE HASP OF THE SWITCH TO PREVENT SWITCH MOVEMENT .",False,True,False,False,False,0.0
30,19,11,UP,31,NORTH PLATTE,LINCOLN,"YNP40R-17 CONDUCTOR MADE A HOOK IN FORWARDER 10, DROPPED THE RETARDER AND UNTIED BRAKES. HE BEGAN H IS SECOND SHOVE BY STARTING AT COUPLE SPEED AND LISTENED FOR THE SLACK TO BUNCH, THEN HE WAITED 15-2 0 SECS FOR THE ENTIRE CONSIST TO BUNCH BEFORE SLOWLY NOTCHING SPEED TO 7 MPH AS PER PROPER TRAIN HAN DLING. SHORTLY AFTER RAMPING UP TO 7 MPH HE HEARD SOMEONE TELL HIM TO STOP. CONDUCTOR STOPPED IMME DIATELY AFTER AND NOTICED THAT A LUMBER CAR WAS DERAILED IN THE DIRT ON THE EAST END OF FORWARDER 10 .",False,True,False,False,False,0.0
31,19,1,BNSF,38,MANDAN,MORTON,"C-BTMCOB0-04 DERAILED 1 LOCOMOTIVE IN YARD TRACK 2199 WHILE OPERATING LIGHT ENGINES. AFTER SHOVING T HROUGH AND IMPROPERLY LINED SWITCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO CONTROL SHOVE MOVE IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIAL WAS RELEASED.",False,True,False,False,False,0.0
32,19,11,UP,31,CENTRAL CITY,MERRICK,"UEY8DD-27, HAD 11 CARS DERAIL DUE TO BROKEN RAIL. MAX SPEED WAS 7 MPH IN NOTCH 4, AND TRAIN WENT IN TO EMERGENCY AT 5 MPH. BROKEN RAIL DEFECT WAS UNNOTICEABLE OF CAMERAS AND DERAILMENT OCCURRED 55 CA RS FROM THE HEAD END.",False,True,False,False,False,0.0
33,19,11,UP,31,SHELTON,BUFFALO,"MVPNP-07, TRAVELING WESTBOUND AT 29 MPH, STRUCK A TRACTOR TRAILER CARRYING A WIND MILL MOTOR AT THE MP 170.23 CROSSING KEARNEY SUBDIVISION. THE COLLISION RESULTED IN THE DERAILMENT OF THE LEAD LOCOMO TIVE UP5481.",True,True,False,False,False,0.0
34,19,3,BNSF,29,SPRINGFIELD,GREENE,Y-SPM7321-07 DERAILED 1 LOCOMOTIVE WHILE SHOVING YARD TRACK 1298 DUE TO FAILURE TO CONTROL SHOVE MOV E IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
35,19,2,UP,29,KANSAS CITY,JACKSON,"THE YKC20R-25 WAS HUMPING A CUT OF 100 CARS OFF OF 104 TRACK WHEN THE CREW HAD TO STOP ON A HOLD POI SON CAR. ONCE THAT CAR WAS RELEASED AND THE LEAD WAS CLEAR, THEY ATTEMPTED TO CONTINUE HUMPING. WI TH THE HUMP SYSTEM ENGAGED, THE CUT OF CARS WOULD NOT MOVE. UPON INSPECTION, THERE WERE 2 CARS DERA ILED DOWN IN THE CUT, NEAR THE ENGINE.",False,False,True,False,False,0.0
36,19,2,KCS,29,KANSAS CITY,JACKSON,CREW FAILED TO LINE BOTH ENDS OF CROSSOVER FROM WORK LEAD TO 901 & DID NOT PROTECT SHOVE THRU SWITCH RESULTING IN A RUN-THRU SWITCH & WHEN PULLED FORWARD THEY DERAILED. MP 2.5 PITTSBURG SUBDIVISION,False,True,False,False,False,0.0
37,19,2,KCS,29,KANSAS CITY,JACKSON,"CPRS CREW FAILED TO SECURE TRACK 9 & THEY KICKED CARS INTO TRACK 9 & CARS ROLLED OUT THE EAST END & DAMAGED 2 CARS. CPRS CONSIST INCLUDED 2 KCS CARS WITH EQUIP DAMAGE OF $36,000. MP 4 PITTSBURG SUB",False,False,True,False,True,36000.0
38,19,8,NS,29,WENTZVILLE,ST CHARLES,"DW26 WHILE SHOVING EAST WITH NS 5299, TEN EMPTIES, 545 TONS, 937 FEET DERAILED CN 712148, WHEELS R1, R2, L1,L2, WHILE OPERATING OVER THE DIVIDE SWITCH INTO THE GENERAL MOTORS OUTBOUND RAMP.",False,True,False,False,False,0.0
39,19,8,NS,29,WENTZVILLE,ST CHARLES,NS TRAIN D99D708 DERAILED 3 LOADED AUTO RACKS WHILE PULLING THROUGH THE EAST LEAD CROSSOVER DUE TO A DEFECTIVE FROG.,False,True,False,False,False,0.0
40,19,12,KCS,29,KANSAS CITY,JACKSON,"BNSF CREW RAN THRU 126 SWITCH & THEN SHOVED BACK THRU & DERAILED 2 CARS. BNSF EQUIP DAMAGE $2,746 M P 3 PITTSBURG SUBDIVISION",False,True,False,False,True,2746.0
41,19,11,UP,29,SEDALIA,PETTIS,WIMNTZ-01 EXPERIENCED EMERGENCY APPLICATION. CONDUCTOR WALKED TRAIN AND FOUND HZGX7015 HAD TRUCK/BO LSTER DAMAGE. LEAD WHEEL TRUCK/BOLSTER HAD BROKEN AND WAS DRAGGING ON THE GROUND ON TOP OF L3. ALL WHEELS STAYED ON THE RAIL.,False,False,True,False,True,0.0
42,19,6,NS,37,OLD FORT,MCDOWELL,"123P805 HEADED EASTBOUND, DERAILED BNGX 020086 AND BNGX 020108.",False,True,False,False,False,0.0
43,19,2,MDS,28,SHUBUTA,CLARKE,"TRAIN ME-WA07 WAS TRAVELING RAILROAD SOUTH FROM MERIDIAN TO WAYNESBORRO. THE FIRST INDICATION OF A PROBLEM WAS WHEN THE AIR BRAKES WENT TO EMERGENCY STOP. LOOKING IN THE MIRROR THE ENGINEER CAN SEE CARS FALLING OFF THE TRUCK. UPON INSPECTION, THE RAIL BROKE , PIECED THE BOTTOM OF CEFX 319391, AND LIFTED IF OFF THE TRACK. THE NEST FOUR CARS WHERE PULLED OFF THE TRACK. 4 RAILCARS ROLLED OVER. 1 RAIL CAR WAS RE-RAILED. 331 FT OF TRACK WAS DAMAGED.",False,False,True,False,True,0.0
44,19,1,KCS,28,PEARL,RANKIN,CONDUCTOR LET CARS DRIFT INSTEAD OF SHOVING TO COUPLE CARS. THIS CAUSED CARS TO ROLL OUT ON EAST EN D INTO SWITCH CARS BEING SWITCHED FROM EAST END. MP 91.4 MERIDIAN SUBDIVISION,False,False,True,False,False,0.0
45,19,1,KCS,28,JACKSON,RANKIN,CONDUCTOR LET CARS DRIFT INSTEAD OF SHOVING TO COUPLE CARS. THIS CAUSED CARS TO ROLL OUT ON EAST EN D INTO SWITCH CARS BEING SWITCHED FROM EAST END. MP 91.4 MERIDIAN SUBDIVISION,False,False,True,False,False,0.0
46,19,1,ATK,28,BROOKHAVEN,LINCOLN,TRAIN 59 OPERATING WITH LOCOMOTIVE E/173 AND 7 CARS STRUCK A TREE AT MP 778.6 CAUSING DAMAGE TO LEAD LOCOMOTIVE E/173. THERE WERE NO INJURIES TO REPORT.,True,False,False,False,True,0.0
47,19,7,CSX,37,LUCAMA,WILSON,"Q47031 TRAVELING NORTH RECEIVED A HOT BOX DEFECT DETECTOR, UPON RECEIVING THE MESSAGE THE TRAIN WENT INTO EMERGENCY, CONDUCTOR WALKED TRAIN AND FOUND THE 6TH CAR DERAILED.",False,True,False,False,False,0.0
48,19,5,MSR,28,MONTROSE,JASPER,"AT APPROX 1600 THE MSR 111 WAS HEADED SOUTH WHEN THE TRAIN WENT INTO EMERGENCY. AFTER INSPECTION OF THE TRAIN IT WAS FOUND THAT THREE CARS HAD DERAILED CAUSED BY THE BRIDGE FAILURE UNDER THE CAR. NO H AZ MATS INVOLVED. INCIDENT STILL UNDER INVESTIGATION. AMENDED FIELD 37 TO INCLUDE AMOUNT FOR BR IDGE REPAIR, ITEM 39 WAS LEFT BLANK BECAUSE THERE IS NO OTHER CONTRIBUTING FACTOR.",False,True,False,False,False,0.0
49,19,1,GRYR,28,BATESVILLE,PANOLA,THE G200 WAS PROCEEDING SOUTH ON THE BATESVILLE SIDING AND THE ENGINEER FELT A TUG ON HIS ENGINES AN D LOOKED IN HIS MIRROR AND SAW THE LEAD CAR WAS TURNING OVER AND PLUGGED THE TRAIN. UPON INVESTIGATA TION FOUND 7 CARS DERAILED. AFTER INVESTIGATATION IT WAS DETERMINED THE ROAD BED WAS SOFT DUE TO EXC ESSIVE RAIN CAUSING THE RAIL TO SPREAD.,False,True,False,False,False,0.0
50,19,9,EMRY,23,BROWNVILLE,PISCATAQUIS,"THE CREW CUT THE CARS OFF ON THE MAINLINE AT THE WEST END OF HARDY POND IN ORDER TO PICK UP ONE CAR OUT OF THE SIDING.THE CREW STATES THEY
BOTTLED THE AIR ON THE TRAIN. ONCE THE LOCOMOTIVES WERE IN T HE SIDING, THE CARS THAT WERE LEFT ON THE MAINLINE STARTED TO ROLL WESTWARD. THE CREW
QUICKLY TRIED TO GET BACK OUT OF THE SIDING ONTO THE WEST END OF THE MOVEMENT, BUT WHILE COMING OUT OF THE SIDING THE CARS STRUCK THE
LOCOMOTIVES. THE GMTX 3051, NBSR 906, 002 AND NBSR 911 HAVE DAMAGE. THE WEST E ND CAR LOADED WITH NEWSPRINT DERAILED AND IS PARTIALLY DOWN OVER THE
BANK. THE SECOND CAR A CENTER BEAM LOADED WITH LUMBER IS UPRIGHT BUT DAMAGED. THE TRACK BELOW THE DAMAGED CENTER BEAM IS BROKEN AN D HAS TIE
DAMAGE.",True,True,False,False,True,0.0
51,19,5,MNR,23,OAKFIELD,AROOSTOOK,"TRAIN 503 ON DUTY 1900 SQUAPAN. ENGINEER JAY MORSE CONDUCTOR DEVIN SITTZ. GMTX 2644, 211, 2226, TRAV ELING SOUTH HAD ONE CAR DERAIL ONE WHEEL AT MILE 170.2. CAR WAS DRAGGED TO NORTH END OF SAINT CROIX, EIGHT CARS ENDED UP ON THE GROUND.",False,True,False,False,False,0.0
52,19,7,MNR,23,FORT KENT,AROOSTOOK,"CNDR LOZIER ON THE JOB 900 REPORTED THAT THEY HAD LOST AIR AND FOREMAN DJ MICHAUD HAD ALERTED THEM T O 4 OF THEIR CARS DERAILS. 3 LOADED CHIP CARS WERE ON THEIR SIDE, AND THE FOURTH LOADED CHIP CAR WAS STILL UPRIGHT. THERE WERE NO INJURIES AND NO HAZMAT INVOLVED IN THE DERAILMENT. P PEVERETT WAS NOTI FIED WHILE WORKING WITH THE ROADMASTERS, AND RON CAMPBELL WAS NOTIFIED. THE DERAILED CARS ARE: NBSR 874041, AEX 19465, NBSR 874055, NAEX 19473. GBO WAS PLACED BETWEEN MP 244.0 AND MP 245.0 MADAWASKA S UB BY FOREMAN DM CHOUINARD.",False,True,False,False,False,0.0
53,19,2,EMRY,23,SEBOEIS,PENOBSCOT,"TRAIN STOPPED IN EMERGENCY, CONDUCTOR WALKED BACK TO FIND CARS 33-40 FROM THE HEAD END DERAILED. 4 E MPTY CLAY CARS, 2 LOADED FLUX CARS, 2 LOADED BOX CARS. THE 2 ASPHALT FLUX CARS ARE PLACARDED FOR ELE VATED TEMPRATURE.",False,True,False,False,False,0.0
54,19,6,CMQX,23,JACKMAN,SOMERSET,JOB 400 WAS PROCEEDING WESTBOUND ON THE MOOSEHEAD SUB AT APPROX. MP 66 THE CREW NOTICED A LARGE AMOU NT OF SMOKE WHILE CHECKING THE TRAIN IN THE CURVE. CREW BROUGHT THE TRAIN TO A CONTROLLED STOP AND FOUND THE BURNT OFF JOURNAL AND ONE CAR DERAILED.,False,True,False,False,False,0.0
55,19,9,EMRY,23,BROWNVILLE,PISCATAQUIS,"THE CREW DROPPED THEIR TRAIN ON THE MAINLINE AT THE WEST END OF HARDY POND IN ORDER TO PICK UP ONE C AR OUT OF THE SIDING.THE CREW STATES THEY BOTTLED THE AIR ON THE TRAIN. ONCE THE LOCOMOTIVES WERE IN THE SIDING, THE TRAIN THAT WAS LEFT ON THE MAINLINE STARTED TO ROLL WESTWARD. THE CREW QUICKLY TRIE D TO GET BACK OUT OF THE SIDING ONTO THE WEST END OF THE MOVEMENT, BUT WHILE COMING OUT OF THE SIDIN G THE TRAIN STRUCK THE LOCOMOTIVES. THE GMTX 3051, NBSR 906, AND NBSR 911 HAVE DAMAGE. THE WEST END CAR LOADED WITH NEWSPRINT DERAILED AND IS PARTIALLY DOWN OVER THE BANK. THE SECOND CAR A CENTER BEAM LOADED WITH LUMBER IS UPRIGHT BUT DAMAGED. THE TRACK BELOW THE DAMAGED CENTER BEAM IS BROKEN AND HA S TIE DAMAGE.",True,True,False,False,True,0.0
56,19,7,CRSH,26,DETROIT,WAYNE,FL40 OPERATING ON BLVD DERAILED AND SIDESWIPED CARS ON EC24.,False,True,False,False,False,0.0
57,19,3,CSX,26,DEARBORN,WAYNE,"Q32816 PULLED INTO ROUGEMERE YARD, FROM THE W/E THROUGH R07 INTO WEST 03, PD WHEEL 86TH CAR DROP IN DUE TO INSUFFICIENT RAIL FASTNERS.",False,False,True,False,False,0.0
58,19,8,LSRC,26,KAWKAWLIN,BAY,"301 SHOVING IN 22 LOADS INTO SPEC STONE SIDING. CONDUCTOR RIDING BOTTOM, ENGINEER STATED THAT CONDUC TOR SHOULD WALK THE TRAIN DUE TO COMING TO A STOP WITHOUT ADDING AIR. CONDUCTOR WALKED UP FROM THE B OTTOM AND FOUND 7 CARS OFF THE RAIL. STARTED 2 CAR LENGTHS PAST DERAIL DUE TO WIDE GAGE.",False,True,False,False,False,0.0
59,19,3,NS,26,DETROIT,WAYNE,BD91 PULLING WEST DERAILED CARS 40-46 IN THE CONSIST ACCOUNT OF RUPTURED GAGE UNDER LOAD DUE TO SATU RATED TIES FROM STANDING WATER IN THE RUNAROUND TRACK.,False,True,False,False,False,0.0
60,19,5,WC,26,ESCANABA,DELTA,"AT 1350 CDT ON MAY 30TH TRAIN L54981-30 WAS STRUCK BY A SEMI TRUCK AT THE CROSSING AT MILE 336.44 ON THE MANISTIQUE SUBDIVISION. THE TRUCK MADE CONTACT MID TRAIN, CAUSING LINES 22 TO 30 TO DERAIL UPRI GHT AND LEANING. OCCUPANT OF THE TRUCK WAS AIRLIFTED TO HOSPITAL. NO INJURIES TO CREW.",True,True,False,False,False,0.0
61,19,3,CRSH,26,DETROIT,WAYNE,"NS CONDUCTOR MAKING A MOVE TO SET OFF CARS IN EC09, LEFT REMAINING CARS ON SR01 FOUL CAUSING MULTIPL E CAR DAMAGE. NORFOLK SOUTHERN WILL FILE FORM 81 FOR THEIR CREW.",False,False,True,False,True,0.0
62,19,4,DC,26,DETROIT,WAYNE,"AT APPROX. 2230 ON 4/8/19, SUPERVISOR WAS NOTIFIED BY THE DCRR YDMSTR THAT THE B0808 HAD ONE SUB LAD LE DERAILED AT THE PIPELINE SWITCH ON ZUG ISLAND. THE YDMSTR REPORTED THE 6TH CAR WAS DERAILED IN A 6-CAR CUT OF EMPTY SUB LADLE HEADING NORTH FROM THE MAIN PLANT.
WHILE PULLING NORTHBOUND FROM GREA T LAKES WORKS TOWARDS ZUG ISLAND RCO JOB B20808 PULLING 6 SUB LADLES DERAILED ON TANGENT TRACK. THE SIXTH (REAR) CAR IN THE CONSIST, SUB LADLE #29, DERAILED 975’ SOUTH OF BALLINGER CROSSING, AFTER TRA VELING 5,213’ THE CAR CAME TO REST NORTH OF THE PIPELINE SWITCH ON ZUG ISLAND. UPON INVESTIGATION OF THE TRACK NOTES, EQUIPMENT INSPECTION, RCO STATEMENTS, AND LOCOMOTIVE DOWNLOADS THE TAPS TEAM CONCL UDED THE FOLLOWING:
THE R4 WHEEL CLIMBED THE RAIL AT THE POINT OF DERAILMENT. THE FLANGE RODE THE T OP OF THE RAIL FOR 78” BEFORE DROPPING TO THE FIELD SIDE OF THE HOT METAL LEAD. THE L4 WHEEL DROPPED INTO THE GAGE IN CORRESPONDENCE. THE RESULTS OF OUR SITE INSPECTION COMBINED WITH INSPECTION OF THE SUB LADLE #29 REVEALED EVIDENCE OF AN IMPROPERLY LOADED CAR. THE CAR WAS FOUND TO HAVE A SUBSTANTIA L AMOUNT OF SOLIDIFIED IRON POOLED TO THE WEST SIDE OF THE CAR RESULTING IMPROPER CLEARANCE OF THE S IDE BEARINGS. THE BEARINGS ON THE WEST ARE IN CONSTANT CONTACT WHILE THE BEARINGS ON THE EAST HAVE C LEARANCE MEASUREMENTS THAT EXCEED THE ALLOWABLE LIMITS BY 1.5”. THIS CONDITION PREVENTED THE CAR FRO M ARTICULATING WHILE IN MOTION AND ALLOWING THE R4 WHEEL TO CLIMB THE RAIL.",False,True,False,False,False,0.0
63,19,9,LSRC,26,FLINT,GENESEE,Y112-12 WERE MAKING A SHOVE MOVE DOWN THE LEAD INTO 33 TRACK. THE 9TH CAR FROM THE HEADEND JUMPED TH E FROG AT THE 11 SWITCH AND DERAILED. THIS CAUSED THE FOLLOWING 4 CARS TO DERAIL AS WELL. ONE OF THE CARS (ATW 318345) STRUCK A LOCOMOTIVE (LSRC 6302) IN AN ADJACENT TRACK.,True,True,False,False,False,0.0
64,19,11,CSX,26,DEARBORN,WAYNE,"WHEN PULLING OUT OF TRACK R07 AT ROUGEMERE YARD, Q38701 DERAILED LINES 70-77 OF THEIR TRAIN. INVESTI GATION REVEALED DERAILMENT WAS CAUSED BY BROKEN RAIL IN TRACK R07.",False,True,False,False,False,0.0
65,19,12,MQT,26,LUDINGTON,MASON,"WHILE SWITCHING CARS IN LUDINGTON YARD, SETTING LOADED CARS TO 13 TRACK, AN APPROXIMATELY 6 FOOT PIE CE OF RAIL BROKE UNDER THE TRAIN. CREW WAS UNAWARE OF THE BREAK AND MADE A PULLING MOVE OVER THE BRO KEN RAIL, DERAILING 1 CAR. THE CREW THEN SHOVED BACK INTO THE TRACK DERAILING ANOTHER CAR AND CLIMBI NG THE SWITCH POINT TO FALL IN BETWEEN THE STOCK RAIL AND POINT, DERAILING THE OTHER 3 CARS.",False,True,False,False,False,0.0
66,19,3,GRS,23,ENFIELD,PENOBSCOT,MAWA-29 WAS HEADING WEST WHEN THE TRAIN DERAILED 5 CARS AT APPROXIMATELY MILE POST 20.,False,True,False,False,False,0.0
67,19,4,MBTA,25,ROCKPORT,ESSEX,"TRAIN 128 DEPARTED ROCKPORT STATION AND HIT A CAR AT POOLE'S LANE. DRIVER OF VEHICLE DID NOT STOP AN D WAS STRUCK ON THE REAR BUMPER OF THE CAR. NO INJURIES REPORTED.
CORRECTED TYPE OF TRACK 7.1",True,False,False,False,False,0.0
68,19,8,CSX,18,INDIANAPOLIS,MARION,"Y39315 COUPLED INTO 027 TRACK AND PULLED LOOKING FOR ANY SEPARATION. Y39315 IDENTIFIED CARS NOT COUP LED BETWEEN LINES 15-16 IN THE TRACK AND WALKED TO SEPARATION. Y39315 SHOVED WEST, COUPLED CARS AND PULLED ON TRACK OBSERVING ALL CARS MOVING EAST. Y39315 WALKED TO HEAD END AND PROCEEDED TO PULL EAST FROM 027 TRACK DERAILING 4 CARS AT TURNOUT.",False,True,False,False,False,0.0
69,19,8,NS,18,GARY,LAKE,NS TRAIN 34JB308 STRUCK A HWY-USER AT A HWY-GRADE CROSSING.,True,False,False,False,False,0.0
70,19,8,CSX,18,ROSEDALE,PARKE,W21908 DERAILED 17 CARS DUE TO TRACK BUCKLING DUE TO SUNKINK.,False,True,False,False,False,0.0
71,19,8,WC,18,GARY,LAKE,"HUMP JOB TIED ON KC33 ON THE EAST END TO PULL IT OVER THE HILL. AFTER MAKING TWO JOINTS IN THE TRACK THE EMPLOYEE STRETCHED, HE HAD ALL OF THE CARS ON KC33 MOVING. THE OPERATOR PULLED HIMSELF TO THE T OP OF THE HILL ON THE LOCOMOTIVE AND BROUGHT THE MOVEMENT TO A COMPLETE STOP AND DETRAINED. ONCE CLE AR OF THE TRAIN THE OPERATOR CONTINUED THE MOVEMENT EAST AT THE END OF KC33. TBOX667025 AND TBOX6424 82 TRAVERSED THROUGH THE CURVE THE LATERAL FORCE CAUSED BY THE DRAWBARS BEING CROSSED BETWEEN TWO CA RS DERAILED THE REAR SET OF TRUCKS ON TBOX642482. THE TBOX667022 AND THE TWO WEST CARS DERAILED DUE TO LATERAL FORCES PUSHING THE GAUGE OF THE RAIL OUT.",False,True,False,False,False,0.0
72,19,12,UP,16,MONTPELIER,BEAR LAKE,"MPDNP-27 SHOVED INTO IX962 FROM MAIN 2. CONDUCTOR WAS RIDING THE SHOVING MOVEMENT INTO THE YARD. C ONDUCTOR FAILED TO ALIGN THE CROSSOVER FROM TRK 5 INTO TRK 6. TRK 5 WAS LINED INTO TRK 6. TRK 6 WA S LINED INTO EAST 6 VIOLATING 8.2 AND 8.12. ONCE COUPLED INTO THE PICKUP IN TRK 6 THE CONDUCTOR INS TRUCTED THE ENGINEER TO PULL THE PICKUP OUT SO HE COULD RELEASE THE HAND BRAKES AND RE-HANG THE EOT DEVICE. ONCE CONDUCTOR COMPLETED THE TASKS HE INSTRUCTED THE ENGINEER TO PULL FORWARD OUT OF THE YA RD SO HE COULD RELINE THE MAIN TRACK SWITCH AND RESTORE THE DERAIL. ONCE AT THE DERAIL, AS THE TRAI N WAS PULLING, IT WAS NOTICED 3 RAILCARS WERE ON THE GROUND. THE ENGINEER WAS IMMEDIATELY NOTIFIED TO STOP THE TRAIN, AT WHICH POINT THE ARMN170753 STRUCK SIGNAL TOWER CP115, KNOCKING IT DOWN ON TOP OF THE CARS.",True,True,False,False,False,0.0
73,19,5,UP,20,KANSAS CITY,WYANDOTTE,"THE YKS21R-09 KICKED A SET OF FOUR CARS INTO BOWL TRACK 6 AT MATTOON CREEK FROM THE WEST END. THE C ARS WERE CUT OFF ON THE LEAD AND ROLLED FREELY INTO THE 24 CARS PREVIOUSLY IN BOWL 6. THE FIRST OUT CAR IN THE CUT OF FOUR CEGX1019, AN EMPTY HOPPER CAR, CROSSED DRAWBARS WITH THE STLX5301, ANOTHER E MPTY HOPPER CAR, RESULTING IN A DERAILMENT.",False,True,False,False,False,0.0
74,19,5,UP,20,KANSAS CITY,WYANDOTTE,"THE ARLNSR-12 WAS TRAVELING EAST BOUND INTO TRACK 214 AT ARMOURDALE YARD, STAGING FOR THE NS. TRAIN WAS IN DYNAMICS WHEN CREW NOTICED THEY WERE SLOWING DOWN AND THAT THE EOT WAS READING 00. CREW WAS TOLD OVER THE RADIO TO REMAIN STOPPED BECAUSE THEY HAD CARS DERAILED. CONDUCTOR WALKED THE TRAIN A ND FOUND TWO CARS DERAILED, FIVE FROM THE REAR OF THE TRAIN. THE TTGX978450 CLIMBED THE RAIL TRAVEL ING 15 FT BEFORE DERAILING ITSELF AND THE TTGX696686. INVESTIGATION DETERMINED THAT THE DERAILMENT WAS CAUSED BY REVERSE CROSS ELEVATION IN TURNOUT.",False,True,False,False,False,0.0
75,19,8,UP,17,EAST ST LOUIS,ST CLAIR,"AASFX-08 WAS TRAVELING EAST OUT OF THE ALS YARD, ONTO TRRA MAINTAINED TRACK. THE CONDUCTOR LOOKED OU T OF THE WINDOW, SAW THEY HAD CARS ON THE GROUND, AND TOLD THE ENGINEER TO STOP. FIVE CARS DERAILED DUE TO TRACK WARP ON TRRA TRACK. TRACK WARP IS THE DIFFERENCE IN CROSS LEVEL BETWEEN ANY TWO POINTS LESS THAN 62 FEET APART. EXCESSIVE WARP CONTRIBUTES TO WHEEL CLIMB. MEASUREMENTS WERE 3 3/8 INCH WAR P UNDER LOAD (MAX OF 3), 2 1/2 INCH OF TWIST WITH A MAX OF 2 INCHES. ALS SUSTAINED TRACK DAMAGE AS W ELL. * TRRA MAINTAINS TRACK. TRRA TRACK DAMAGE = $7,847. ALS TRACK/SIGNAL DAMAGE = $9,389*",False,True,False,False,True,17236.0
76,19,8,IC,17,MARKHAM,COOK,"TRAIN M37161-16 WAS IN THE PROCESS OF SETTING OUT AT MARKHAM YARD ON THE SOUTH END OF F YARD INTO TR ACK MF14. CONDUCTOR FAILED TO ENSURE THE ROUTE TO BE USED WAS LINED RESULTING IN THE MOVEMENT GOING DOWN THE ADJACENT LEAD INTO THE SIDE OF A YARD MOVEMENT. CAR CTTX695997 DERAILED ON ITS SIDE, TTGX98 6863 DERAILED UPRIGHT, DTTX742577 NOT DERAILED WITH SIDE COLLISION DAMAGE. TRANSPORTATION, MECHANICA L AND ENGINEERING RESPONDING.",False,False,True,False,True,0.0
77,19,12,UP,6,BLOOMINGTON,SAN BERNARDINO,"YWC28R-23 WAS SHOVING WEST INTO 315 TRACK WHEN THE 91ST CAR FROM THE WEST END (AEX13728) DERAILED TH E L3, L4, R3 AND R4 WHEELS AT THE 345 SWITCH DUE TO A LADING CABLE FROM THE TTZX862474, WHICH HAD BE EN CAUGHT AND TORN FROM THE CAR AND FOULED THE 345 SWITCH.",False,True,False,False,False,0.0
78,19,12,UP,6,OAKLAND,ALAMEDA,YOA78-20 DERAILED ON SWITCH THAT WAS PREVIOUSLY RUN THROUGH BY ANOTHER JOB.,False,True,False,False,False,0.0
79,19,12,UP,6,FRENCH CAMP,SAN JOAQUIN,"CONTRACT TRAIN CREW RAN THROUGH SWITCH FROM TRACK 168 TO MAIN LINE. CREW WAS ATTEMPTING TO SWITCH P OWER OUT OF 168 ONTO THE MAIN. CONDUCTOR WAS UNTYING TWO REAR UNITS WHILE ENGINEER TOOK FIRST LOCOM OTIVE OUT OF TRACK. HE RAN HIGH OF THE SWITCH, GOT DOWN AND LINED SWITCH, THEN SHOVED LOCOMOTIVE BA CK DOWN THE MAIN LEAVING THE SWITCH LINED FOR STRAIGHT RAIL. ENGINEER THEN WALKED TO THE OTHER TWO UNITS AND PULLED AHEAD THROUGH SWITCH. CONDUCTOR WAS RIDING REAR LOCOMOTIVE AND NOTIFIED ENGINEER O F GAPPED POINTS WHEN THEY CLEARED.",False,False,True,False,False,0.0
80,19,9,BLF,12,OAKLAND PARK,BROWARD,"BLF 604 TRAVELING NB ON THE EM, WITNESSED A VEHICLE GO AROUND THE DOWNED CROSSING GATES. ENGINEER S OUNDED HORN AND BELLS, PLACED TRAIN IN EMERGENCY STRIKING VEHICLE. RESULTING IN DRIVERS FATALITY. FEC DAMAGES $7011.53",False,False,True,False,False,7011.53
81,19,9,FEC,12,MIAMI-DADE,MIAMI-DADE,"CONDUCTOR SHOVED OUT OF TRACK 1 TO PICK UP LOADS AND DID NOT LINE THE SWITCH FOR HIS MOVEMENT. NOT REALIZING HE HAD RAN THROUGH THE SWITCH, PROCEEDED TO PULL DERAILING THREE EMPTY CARS. NO INJURIES WERE SUSTAINED.",False,True,False,False,False,0.0
82,19,9,FEC,12,WEST PALM BEACH,PALM BEACH,"BLF 605 WAS TRAVELING NORTHBOUND ON THE WEST MAIN TRACK AND STRUCK A VEHICLE THAT WENT AROUND THE LO WERED GATES THAT WERE WORKING AS INTENDED AT THE WESTWOOD ROAD CROSSING. DRIVER SUSTAINED FATAL I NJURIES. BLF DAMAGES WERE $174,475.",True,False,False,False,False,174475.0
83,19,9,FEC,12,OAKLAND PARK,BROWARD,"BLF 604 WAS TRAVELING NORTHBOUND ON THE EAST MAIN AND WITNESSED A VEHICLE GO AROUND THE DOWNED CROSS ING GATES. ENGINEER SOUNDED HORN AND BELLS AND PLACED TRAIN IN EMERGENCY BUT WAS UNABLE TO STOP PRI OR TO IMPACT. DRIVER SUSTAINED FATAL INJURIES. BLF DAMAGES WERE $415,099.",False,False,True,False,False,415099.0
84,19,9,UP,6,SALINAS,MONTEREY,"LRQ31-25, LEAD LOCOMOTIVE UP1096, WAS TRAVELING WEST BOUND FROM SALINAS TO WATSONVILLE WHEN A PRODUC E TRUCK PULLED IN FRONT OF THEM ON A PRIVATE XING. INCIDENT HAPPENED AT MP 112.6 ON THE COAST SUB A T OR AROUND 1300. THE FEMALE DRIVER WAS FATALLY INJURED.",False,False,True,False,False,0.0
85,19,11,BNSF,6,SAN DIEGO,SAN DIEGO,S-SDGMEM1-15 DERAILED 19 RAILCARS WHILE PULLING OUT OF YARD TRACK 9832 DUE TO TRACK WIDE GAGE. NO HA ZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
86,19,7,UP,29,INDEPENDENCE,JACKSON,"MNA TRAIN LPHPHJ-03, WITH LEAD LOCOMOTIVE UP3201, EXPERIENCED A FIRE ON THE LOCOMOTIVE BETWEEN MILE POST 271.22 AND MILE POST 271.31 OF THE SEDALIA SUBDIVISION. *MNA EQUIPMENT DAMAGE = $40,000*",False,False,True,False,True,40000.0
87,19,7,UP,29,DE SOTO,JEFFERSON,THE WCBTGZ-23 WAS TRAVELING SOUTH ON THE DESOTO SUB AT MP 43.4 AT 22MPH WHEN THE TRAIN HIT A SOFT SP OT ON THE LEFT RAIL WHILE IT A RIGHT HAND CURVE. THE LEADING WHEELS OF THE LEAD LOCOMOTIVE DERAILED. CAR HZGX7353 ALSO DERAILED DURING RE-RAILMENT PROCESS.,False,True,False,False,False,0.0
88,19,8,KAW,29,NORTH KANSAS CITY,CLAY,"KAW610 WAS SHOVING 31 CARS DOWN LEAD 7 AT 2300 ON 8/30/2019. CONDUCTOR HOLCOMB AND STUDENT CONDUCTO R HOLMES WERE OBSERVING THE SHOVE FROM OUTSIDE OF THE CREW TRUCK. ENGINEER DAVIS FELT THE SLACK RUN IN, THROTTLED OFF AND QUICKLY CAME TO A STOP. HOLCOMB AND HOLMES DROVE TO THE POINT AND FOUND 2 CA RS, GATX 32194 AND TILX 200269, SHOVED OFF THE END OF HENKEL'S TRACK AND THROUGH A CONCRETE RETENTIO N PIT WALL. THEY SECURED THE SCENE, CONTACTED HENKEL STAFF AND GENERAL MANAGER BOLT. THERE IS NO P RODUCT (NON-HAZARDOUS) LEAKING FROM THE TANK CARS AND NO INJURIES. RJ CORMAN RE-REAILED THE CARS.",False,False,True,False,False,0.0
89,19,10,MNCW,9,NEW HAVEN,NEW HAVEN,"TRAIN 1510'S EQUIPMENT WAS SHOVING WEST TOWARDS TRACK 62 WHEN AT THE 16/67E SWITCH, THE SWITCH POINT S (FACING) WERE LINED REVERSE TOWARDS TRACK 69 (FUEL PAD). TRAIN 1510'S EQUIPMENT OPERATED APPROXIMA TELY 200 FEET WEST PAST THE 16/67E SWITCH BEFORE COMING TO A STOP.",False,False,True,False,False,0.0
90,19,5,IANR,19,CEDAR RAPIDS,LINN,"IANR TRAIN WACR-27 ARRIVED THE CEDAR RAPIDS NORTH YARD ON TRACK 13. THE CREW HAD INSTRUCTIONS TO SET OUT UP INTERCHANGE CARS ON 14 TRACK BEFORE HEADING THROUGH THE YARD TO THE CEDAR RAPIDS IOWA CITY R AILROAD (CIC).
IANR WACR-27 CUT OFF THE 10 REAR CARS FOR CIC ON TRACK 13 AND THEN PULLED FORWARD WITH 5 CAR LOADS OF OATS RIGHT BEHIND THEIR ENGINE CONSIST (FIVE LOCOMOTIVES ? FOUR OF WHICH WERE O N LINE) FOLLOWED BY 10 EMPTY FLAT CARS AND 20 MORE OAT LOADS ON THE REAR OF THE CUT. AFTER PULLING A HEAD TO CLEAR THE TRACK 13 SWITCH THE ENGINEER COMPLETED A STOP USING AN AUTOMATIC BRAKE PIPE REDUCT ION. THE ENGINEER THEN RECEIVED RADIO INSTRUCTIONS TO MAKE A REVERSE MOVE IN ORDER TO COMPLETE THE I NTERCHANGE SET OUT INTO TRACK 14. AT THIS POINT IN TIME, THE ENGINEER APPLIED EXCESSIVE POWER TO THE ENGINE CONSIST WITHOUT ALLOWING ADEQUATE TIME FOR THE CUT OF CAR’S AIR BRAKES TO RELEASE. IN DOING SO THIS CREATED EXCESSIVE LATERAL DRAWBAR FORCE WHICH SUBSEQENTLY CAUSED THE LEAD AXLE OF OTTX 93545 TO DERAIL. THE MOVEMENT CONTINUED UNTIL A COUPLING WAS MADE ON TRACK 14. AFTER THE JOINT WAS MADE T HE REVERSE MOVE INTO TRACK 14 WAS AGAIN INITATED. AS THE SHOVING MOVEMENT CONTINUED THE AFORE MENTIO NED DERAILED CAR TRAVERSED OVER AND SPLIT THE TRACK 14 SWITCH. ONCE THIS SWITCH WAS SPLIT IT SUBSEQU ENTLY DAMAGED THE TURNOUT AND TRACK TO SUCH A DEGREE THAT IS CAUSED SIX ADDITIONAL CARS TO DERAIL.",False,True,False,False,True,0.0
91,19,12,UP,6,CALIENTE,KERN,MWCEU-26 WAS TRAVERSING ON HEAVY MOUNTAIN GRADE WHEN THE CREW RECEIVED A TONE DEFECT FROM A DRAGGING DETECTOR AT MP337.2. THE TRAIN WAS TRAVELING AT 21MPH ON APPROXIMATELY 2.3% DESCENDING GRADE WHEN ENGINEER BROUGHT THE TRAIN TO A STOP FOR INSPECTION. ONE SET OF TRUCKS WAS FOUND DERAILED 31 CARS F ROM THE HEAD END ON CAR NUMBER ROIX58052 AND TRAVELED 1.3 MILES ON THE GROUND. THE POD WAS NOTED AT MP337.9 INSIDE TUNNEL 2.,False,True,False,False,False,0.0
92,19,12,TSWS,6,FRENCH CAMP,SAN JOAQUIN,"LLT3 MOVED LOCOMOTIVES IN THE CLEAR EAS OF THE MAIN SWITCH. THE CREW THEN MADE A FORWARD FACING MOVE WITH LOCOMOTIVES IN THE WEST SHARPS LEAD ONTO THE MAIN, BUT DIDN'T NOTICE THAT THE MAIN SWITCH WAS IMPROPERLY LINED. THE ENINGEER RAN THROUGH THE IMPROPERLY LINED SWITCH, DAMAGING IT.",False,False,True,False,False,0.0
93,19,8,MNCW,9,BRIDGEPORT,FAIRFIELD,"TRAIN 1101 WAS SHOVING 9 CARS EAST INTO BRIDGEPORT YARD ONTO TRACK 14 WHEN THE 2014W SWITCH WAS THRO WN UNDERNEATH THE 7TH AND 8TH CARS OF THE CONSIST, CAUSING TWO TRUCKS TO DERAIL. TRAINMAN WAS ON THE GROUND, CONDUCTOR ON THE LEAD END, AND ENGINEER ON THE REAR. TRAINMAN OPERATED THE 2014W SWITCH AS EQUIPMENT WAS PASSING HIS LOCATION, AND 3 OF 9 CARS HAD NOT CLEARED THE SWITCH.",False,True,False,False,False,0.0
94,19,8,MNCW,9,NEW HAVEN,NEW HAVEN,"TRAIN 6558 WAS GIVEN PERMISSION TO TRACK 56 IN NEW HAVEN YARD AND TRAVELED WEST ON UNINTENDED TRACK 45 AND OPERATED PAST THE `END OF WIRE` SIGN ON TRACK 45, CAUSING 1 PANTOGRAPH TO FLIP AND BECOME DAM AGED. AT TIME OF INCIDENT, CONDUCTOR WAS ON THE LEADING END OF THE MOVE. CONDUCTOR UNFAMILIAR WITH M OVE IN THE YARD TO TRACK 56 AND DID NOT LINE THE SWITCH FOR EQUIPMENT TO TRAVEL ON TO INTENDED TRACK .",False,False,True,False,False,0.0
95,19,7,SFRV,12,MIAMI-DADE,MIAMI-DADE,"AT AROUND 1400 HOURS, AN INCIDENT OCCURRED IN WHICH PTC, TMDS, AND EQUIPMENT MALFUNCTIONS WERE THE C ONTRIBUTING CAUSE OF PROPERTY DAMAGE ON A MAIN TRACK SWITCH IN MIAMI. SFRTA CONCLUDED THAT THE INCID ENT WAS NOT A HUMAN FACTOR INCIDENT.
",False,False,True,False,True,0.0
96,19,7,FEC,12,MIAMI-DADE,MIAMI-DADE,"AS 11:00 AM JOB WAS LEAVING THE YARD, LEAD MOTOR, FEC 508, DERAILED WHILE GOING THROUGH THE GATOR SW ITCH.",False,True,False,False,False,0.0
97,19,4,SFRV,12,HIALEAH,DADE,TRAIN P604 WAS PULLING OUT OF HIALEAH YARD AND RAN THROUGH A DERAIL. THERE WERE NO INJURIES SUSTAINE D DUE TO THE INCIDENT. SUPERVISION IS INVESTIGATING THE INCIDENT AND WILL SUBMIT APPROPRIATE DOCUMEN TATION AND RECOMMENDED DISCIPLINE.,False,True,False,False,False,0.0
98,19,3,NS,17,DECATUR,MACON,YARD ASSIGNMENT DB28 WAS PULLING EASTBOUND OUT OF THE EAST END OF WB19 WITH A CONSIST OF 15X6 - 2182 TONS 1324 FEET WHEN LINES 17 THROUGH 20 OF THE CONSIST DERAILED ACCOUNT WIDE GUAGE DUE TO WEAK TIMB ES,False,True,False,False,False,0.0
99,19,3,UP,17,DOLTON,COOK,TRAIN MASCHX-15 DERAILED TWO AUTORACKS DUE TO BROKEN RAIL IN TRACK 20.,False,True,False,False,False,0.0
100,19,4,IAIS,17,CREVE COEUR,TAZEWELL,"IAIS SIPE-14 WAS PULLING 41 CARS INTO TZPR YARD TRACK A-36 WHEN 6 CARS DERAILED. ****TZPR MAINTAINS TRACK. TRACK DAMAGE = $40,710 ESTIMATE****",False,True,False,False,True,40710.0
101,19,10,KJRY,17,BURNSIDE,HANCOCK,"PREX 3069 HAD A TURBO FAILURE CATCHING THE AIR BOX FILTERS ON FIRE, BURNING A CONNECTOR HOSE BETWEEN THE BLOCK AND TURBO. TURBO BACK FIRED INTO AIR BOX.",False,False,True,False,False,0.0
102,19,2,BNSF,17,CHICAGO,COOK,Y-CHI2031-03 DERAILED 1 RAILCAR WHILE PULLING OUT OF YARD TRACK 902 DUE TO TRACKBROKEN RAIL. NO HAZ ARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
103,19,8,WC,18,GARY,LAKE,"REPORTS YKPS04-11 HUMPED TWO CARS TOWARD KC48 (TILX310154 AND TILX210152, EMPTY CLEAN TANK CARS). TH ESE ROLLED BACK TOWARD THE ASSIGNMENT, SIDESWIPING THE FOLLOWING CARS: AGT 78938 (LOAD FIBREBOARD), GATX 29574 (LOAD METHANOL), DBCX 201471 (LOAD GLYCOL), UTLX 666538 (LOAD FORMALDEHYDE), UTLX 682488, GATX 224991 (EMPTY, SOY OIL), NKCR 1263 (EMPTY INTERMODAL CAR). FIRST CAR EX KC48, TILX 310154, DER AILED UPRIGHT.",False,False,True,False,False,0.0
104,19,10,CFE,18,FORT WAYNE,ALLEN,"FWRY-21 SHOVED 54 CARS INTO TRACK #1 AND UNKNOWINGLY RAN THROUGH A SWITCH, LEAVING CARS IN THE FOUL. CREW TAXI'D OUT TO DO OTHER WORK FOR ROUGHLY 6 HOURS AND CAME BACK AFTERWARDS. WHILE MAKING ANOTHER SHOVE MOVE, BEING UNDER THE IMPRESSION THE CUT OF CARS THEY HAD LEFT WERE IN THE CLEAR, THEY STRUCK THEIR CARS THEY HAD SHOVED OUT PREVIOUSLY.",True,False,False,False,False,0.0
105,19,10,IHB,18,WHITING,LAKE,CREW OF TRAIN KG23 WAS PULLING OUT OF WHITING YARD SOUTH ON MW01 WHEN THE WEST RAIL BROKE DUE TO A T RANVERSE /COMPOUND FISSURE CAUSING THE REAR 2 TANK CARS TO DERAIL TO THE WEST SIDE AND SEPERATE FROM THE TRUCKS.,False,True,False,False,False,0.0
106,19,6,SKOL,20,NEODESHA,WILSON,"AT APPROXIMATELY 0130 ON 6/27/2019 THE SKOL 206 CREW ( ENGINEER WITH 2.2 YRS, CONDUCTOR WITH 1.2 YRS AND FIREMAN WITH 1.2 YRS ) REPORTED A DERAILMENT IN NEODESHA WHILE ASSISTING THE SKOL 301 ENGINEER WITH 7 YRS OUT OF THE YARD . CREW HAD STOPPED TOO PICK UP 11 CARS FROM 5 TRACK NEODESHA AND DOUBLED BACK TO TRAIN. AS THEY WHERE DRAGGING TRAIN AHEAD TO DO AN AIR TEST THE DOORS OPENED ON SKOL 925119 CAUSING THE 5 CARS BEHIND IT TO DERAIL. SKOL 78789, SKOL 78585, SLWC 106, AEX 13264 AND SKOL 78790 .",False,True,False,False,False,0.0
107,19,4,UP,20,WICHITA,SEDGWICK,"THE MWTER-16 WAS BUILDING THEIR TRAIN ON THE SOUTH END OF THE WICHITA YARD. WHILE MAKING THE DOUBLE OVER, THE CREW RAN THROUGH THE SWITCH THEN REVERSED THE MOVE CAUSING THE DERAILMENT OF 4 CARS. NO INJURIES AND NO HAZMAT RELEASES REPORTED.",False,True,False,False,False,0.0
108,19,7,BNSF,20,KANSAS CITY,WYANDOTTE,RCO Y-KCK3012-13 DERAILED 9 RAILCARS WHILE PULLING INTO YARD TRACK 6097 DUE TO A PREVIOUSLY RUN THRO UGH SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
109,19,9,UP,20,KANSAS CITY,WYANDOTTE,"YKS41R-19 KICKED A CUT OF TWO CARS INTO NORTH 2. THE EAST CAR IN THE CUT CROSSED DRAWBARS WITH THE M WCX500585 THAT WAS IN THE RAIL. AS CARS WERE ADDED TO THE TRACK, THE PRESSURE FROM THE CROSSED DRAWB ARS CAUSED THE HKRX160044 AND THE MWCX500585 TO DERAIL. IN DERAILING, THE CARS ALSO CAUSED THE RAIL TO ROLL, CAUSING THE CMO23132 THAT WAS EAST OF THE MWCX500585 AND THE MWNX10810 THAT WAS WEST OF THE HKRX160044 TO DERAIL. THE DERAILMENT WAS FOUND AT APPROXIMATELY 05:55 ON THE 20TH AS THE LEAD JOB W AS TRIMMING OUT THE YKS87. CREW NOT HELD RESPONSIBLE.",False,True,False,False,False,0.0
110,19,12,UP,20,COFFEYVILLE,MONTGOMERY,"YCV53-23 WAS BUILDING THE MFWCBB-21 IN COFFEYVILLE YARD. AS THEY PULLED THE CARS IN 8 TRACK NORTHWA RD, THE CUT TRAVERSED THE 8/9 TRACK SWITCH THAT HAD BEEN PREVIOUSLY RUN THROUGH BY THE MNLAM-22 AT A PPROXIMATELY 04:40 ON 12/23/2019. AS THE CARS WENT OVER THE RUN THROUGH SWITCH, THEY BEGAN DERAILIN G. A TOTAL OF 7 CARS DERAILED.",False,True,False,False,False,0.0
111,19,12,UP,20,COFFEYVILLE,MONTGOMERY,"MSANP-16 WAS MAKING THEIR FINAL MOVE BY SETTING OUT CARS. WHEN THE CREW SHOVED INTO TRACK 3 TO CUT THE CARS OFF, THE TRAIN WENT TO PULL NORTH AND DEPARTED COFFEYVILLE. THE TIMX65856 HAD DERAILED THE SOUTH SET OF TRUCKS ON THE CAR. THIS WAS NOT FOUND UNTIL THE TRAIN HAD TRAVELED 709 FEET (ACCORDIN G TO THE DOWNLOAD) AND WENT INTO EMERGENCY, DERAILING THE FOLLOWING EIGHT CARS FROM ROLLED RAIL CAUS ED BY THE TIMX65856. DOWNLOADS SHOW TRAIN PULLING AT 3 MPH WITH 85-100 AMPS IN THROTTLE 3. DERAILM ENT OCCURRED AT A JOINT WITH IRREGULAR CROSS LEVEL.",False,True,False,False,False,0.0
112,19,8,UP,20,ONAGA,POTTAWATOMIE,"THE GSGOLC-31 WAS ON THE MAIN, MEETING THE ACXNP-31. THE ACXNP-31 WENT INTO THE SIDING AND ABOUT 30 CARS INTO IT, CAR TTPX82304 DUMPED A LOAD OF PIPE. THE GSGOLC-31 STARTED TO PULL, BUT ONE WHEEL WAS STRUCK BY THE PIPE AND DERAILED. THE CAR'S WHEEL WAS ON THE GROUND UNTIL IT RERAILED ON THE FROG AT CIRC Z117, BUT THE OTHER WHEEL STAYED ON THE GROUND FOR APPROXIMATELY 3 MILES BEFORE THE TRAIN WENT INTO EMERGENCY.",True,True,False,False,False,0.0
113,19,8,KYLE,20,JAMESTOWN,CLOUD,"KYLGOSA1-21 WAS PULLING THE TRAIN OFF OF YUMA SUB ONTO CONCORDIA SUB AROUND THE WEST ELG OF THE WYE WITH 4 LOCOMOTIVES WITH 92X8. WHEN THE 9TH CAR FROM THE HEAD END DERAILED AT THE NORTH WYE SWITCH, I T CAUSED 4 ADDITIONAL CARS TO DERAIL.",False,True,False,False,False,0.0
114,19,8,BNSF,20,KANSAS CITY,WYANDOTTE,FOREIGN TRAIN F-NS 1121-10 DERAILED 2 RAILCARS WHILE PULLING INTO YARD TRACK 6012 DUE TO A SPRING/PO WER SWITCH MECHANISM MALFUNCTION. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
115,19,3,UP,20,KANSAS CITY,WYANDOTTE,"THE YKS41R-25 WAS PULLING CAR CR628134 FROM THE WEST END OF THE 204 SWITCH. AFTER LINING SWITCH TO COUPLE INTO SOUTH TRACK 8, THE TRAIN WAS SHOVING BACK TWO CAR LENGTHS WHEN THE UP1925 AND CR628134 D ERAILED DUE TO COUPLER CARRIER BEING BROKEN.",False,False,True,False,False,0.0
116,19,7,KYLE,20,BELOIT,MITCHELL,"A TRAIN OPERATED THROUGH THE EAST LEG OF THE WYE AT BELOIT, KS. WHILE TRAVERSING THAT LEG OF THE WYE , ONE WHEEL OF A CAR DERAILED AND WAS DRAGGED ABOUT 1,100 FEET WHERE IT RERAILED ITSELF AT THE HEAL BLOCK OF THE SOUTH WYE SWITCH. AN INSPECTION DETERMINED: (1) THAT THE TRACK WAS WITHIN CLASS 1 STAND ARDS. (2) THERE WAS SOME EVIDENCE AT THE SITE THAT THERE WAS A HIGH FLANGE ON ONE CAR, AND THE WAY T HE WHEEL CLIMBED THE RAIL WOULD INDICATE A SLIGHTLY STIFF TRUCK (TRAIN WAS INTERCHANGED TO THE UP BE FORE THE DERAILMENT WAS DISCOVERED. UP WAS INFORMED AND STATED THE CARS HAD LEFT THE INTERCHANGE BUT HAD BEEN INSPECTED AND NO DEFECT NOTED. FOR THIS REASON, WE COULD NOT DETERMINE WHICH CAR DERAILED AND GET A MEASUREMENT OFF THAT CAR). (3) THE DOWNLOAD SHOWED THAT THE TRAIN MAINTAINED A STEADY FIVE MILE PER HOUR PULL THROUGH THE DERAILMENT LOCATION. BASED ON ALL AVAILABLE INFORMATION, THE DERAILM ENT WAS CAUSED WHEN A HIGH FLANGE CAUGHT A JOINT BAR AND STARTED TO CLIMB THE RAIL, THIS COMBINED WI TH THE SLIGHT PROFILE AND GAUGE NARROWED BY THE ROLLOVER ALLOWED THE WHEEL TO CLIMB THE RAIL AND DER AIL. L/V (LATERAL OVER VERTICLE). THE DERAILMENT WAS NOT DISCOVERED UNTIL THE NEXT TRAIN CREW REPORT ED THAT THERE WERE SEVERAL BROKEN TIES IN THAT AREA AT ABOUT 2100 ON JULY 29, 2019.",False,True,False,False,False,0.0
117,19,10,KYLE,20,COURTLAND,REPUBLIC,CREW WAS SHOVING CARS INTO A HOUSE TRACK. THE CONDUCTOR STOOD AT THE EAST END OF THE TRACK AND SHOVE D CARS TO THE WEST. THE CARS BEING SHOVED COLLIDED WITH CARS IN ANOTHER HOUSE TRACK THAT WERE TRAILI NG OUT AND COVERING THE SWITCH ON THE WEST END OF THE HOUSE TRACKS CAUSING 2 CARS TO DERAIL AND DAMA GE TO 3 TOTAL CARS.,False,True,False,False,False,0.0
118,19,12,KCS,22,LEESVILLE,VERNON,"CREW WAS SWITCHING TRACK 9 IN LEESVILLE YARD. THEY SET 3 CARS TO TRACK 4; 5 CARS CAME BACK TO #9; & MOVED TO TRACK 2 TO SWITCH. STARTED TO PULL TRACK 2 & SAW CARS MOVING IN #9 & WAS UNABLE TO STOP, RESULTING IN DERAILMENT. MP 669 BEAUMONT SUB",False,True,False,False,False,0.0
119,19,2,UP,22,LAKE CHARLES,CALCASIEU,THE UP4973 (3RD LOCOMOTIVE) ON THE MLKBT-13 HAD AN ENGINE FIRE. FIRE WAS EXTINGUISHED WITH EXTINGUI SHER ON LOCOMOTIVE. MACHINIST INSPECTED THE LOCOMOTIVE AND FOUND THE CONNECTING ROD FAILED.,False,False,True,False,False,0.0
120,19,11,UP,22,LIVONIA,POINTE COUPEE,"LLM13R-24, AFTER SHOVING FIRST CUT OF CARS INTO TRACK 304, PULLED BACK UP HIGH ON THE OLD SHOVE LEAD GOING SOUTH, THEN BEGAN MOVING NORTH BACK INTO TRACK 306. WHILE SHOVING INTO TRACK 306, CONDUCTOR WAS NOTIFIED OF POSSIBLE ISSUES WITH THE CUT OF CARS. THE MOVE WS STOPPED WITH TWO CARS CEFX76536 A ND CAIX661 BEING DERAILED AND SEPARATED. CEFX76536 ALONG WITH 21 OTHER CARS WERE STOPPED, ATTACHED TO LOCOMOTIVES. THE CAIX661, WHICH HAD SEPARATED AND DERAILED, CONTINUED ROLLING TO A JOINT IN TRAC K 306. AT THIS POINT IT WAS DETERMINED THAT BOTH CARS WERE DERAILED. CEFX76536 WAS DETERMINED TO H AVE DRAGGING BRAKE RIGGING CAUSING CARS TO DERAIL.",False,True,False,False,False,0.0
121,19,11,KCS,22,SHREVEPORT,CADDO,CREW SHOVED CUT OF 20 CARS. CARS CAME UNCOUPLED & TRAVELLED SOUTH & IMPACTED MQKCSH-02 THAT WAS ST ANDING & CARS DERAILED. MP 553.4 SHREVEPORT TERMINAL SUBDIVISION,False,True,False,False,False,0.0
122,19,5,DREI,18,TERRE HAUTE,VIGO,"NEAREST TOWN AND COUNTY DO NOT MATCH BECAUSE IT HAPPENED IN A DIFFERENT CITY AND COUNTY. THERE IS N O CONTRIBUTING CAUSE.
SHOVING BACK WITH 51 CARS , DERAILED THE LEADING 6 CARS OF THE SHOVE. BROKEN RAIL WAS THE DETERMINED TO BE THE ROOT CAUSE. WATCO CREW WAS HANDLING TRAIN WHEN DERAILMENT OCCURRED . RAIL CARS - BNGX 31753, CEFX 11110, CSYX 13461, CSYX 13339, BNGX 31489, CSYX 12512. LAST SIX CAR S DERAILED",False,True,False,False,False,0.0
123,19,7,WC,18,GARY,LAKE,"PULLDOWN ASSIGNMENT WAS SHOVING EASTWARD IN TRACK KS02 OF KIRK YARD WHEN THEY RAN THROUGH THE DIXIE LEAD SWITCH, DERAILED TANK CARS (INCLUDING FOUR RESIDUE HAZMAT CARS). GACX 11321 (NON-HAZMA, ON SIDE ), GACX 11320 (NON-HAZMAT, ON SIDE) NCIX 8551 (NON-HAZMAT, ON SIDE), UTLX 500004 (LAST CONTAINED PET ROLEUM DISTILLATES, ON SIDE), GATX 1495 (LAST CONTAINED STYRENE MONOMER, ON SIDE), GATX 1504 (LAST C ONTAINED STYRENE MONOMER, ON SIDE), PROX 24052 (LAST CONTAINED STYRENE MONOMER, ON SIDE) AND CGTX 23 538 (NON-HAZMAT, LEANING). NO INJURIES, NO LEAKS AND NO EXPOSURES.",False,True,False,False,False,0.0
124,19,7,CSX,18,BATTLE GROUND,TIPPECANOE,J77305 STRUCK AN OCCUPIED TRACTOR TRAILER THAT PREEMPTED THE GATES. IT GOT STUCK ON THE CROSSING DUE TO THE TRAILER BEING TOO LOW. PROTECTION ALSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS (S TOP LINES & RR XING SYMBOLS).,True,False,False,False,False,0.0
125,19,1,NS,18,GARY,LAKE,AMTRAK TRAIN MATK 365 STRUCK HWY VEHICLE AT HWY GRADE CROSSING. NO INJURIES. NS CREW NOT INVOLVED.,True,False,False,False,False,0.0
126,19,5,CSX,18,INDIANAPOLIS,MARION,Y19311 WAS PULLING A CUT OF CARS OUT OF 001 CLASS TRACK IN THE BOWL. CARS WERE PULLED OUT OF 001 TR ACK AND AT THAT TIME 002 TRACK CUT OF CARS FAILED TO BE STOPPED BY THE INERT RETARDERS AND 2 TRACK S KATES CAUSING A SIDESWIPE. ONE CAR DERAILED.,False,True,False,False,False,0.0
127,19,5,CSX,18,INDIANAPOLIS,MARION,DURING NORMAL HUMP OPERATIONS THE RETARDER FAILED TO SLOW CUT OF CARS DUE TO CONTAMINATION ON WHEELS OF CAR. :CONFIRMED OVER SPEED,False,False,True,False,False,0.0
128,19,6,NS,18,DAYTON,TIPPECANOE,"14E SHOVING 52 LOADS INTO SB02 WHEN GAGE OPENED UNDER MOVMENT CAUSING THE KBSR 47168 (R3,R4,L3,L4) K BSR 76594 (ALL WHEELS) KBSR 76465 (R2,L2) KBSR 470144 (L3) KBSR 47390 (R1,L2,L3,L4) KBSR 23522 (L1,L 3,L4,R2,R3,R4) KBSR 470064 (L1,L2,R1,R2) TO DERAILL.",False,True,False,False,False,0.0
129,19,11,CSS,18,MICHIGAN CITY,LA PORTE,"AT APPROXIMATELY 1715 HOURS TWO (2) NICTD TERMINAL CAR MEN POSITIONED THE CSS-2001 (WEST) AND THE CS S-2008 (EAST) ON THE NEW CONNECTION TRACK JUST EAST OF CARROL AVE. YARD. AT APPROXIMATELY 1838 HOURS PF-10 WAS PERFORMING SWITCH MOVES ON THE NORTH TRACK IN CARROLL AVE YARD WHEN THE ENGINEER NOTICED A LITE ENGINE CONSIST ROLLING IN HIS DIRECTION. THE ENGINEER FOR PF-10 WAS ON THE CSS-2002 IN THE LE AD FACING EAST AND THE CSS-2009 TRAILING. THE CREW WAS COUPLED TO A TRAIN CONSIST OF 17 LOADS AND 0 EMPTIES. THE ENGINEER REPORTED TO HIS CREW TO STEP AWAY FROM THEIR TRAIN AS THE LITE ENGINES ROLLING TOWARDS THEM WERE NOT OCCUPIED AND ABOUT TO COLLIDE WITH THEIR TRAIN. THE ENGINEER DISEMBARKED THE CSS-2002 AND STEPPED AWAY MOMENTS BEFORE THE LITE ENGINE CONSIST (2001/2009) COLLIDED WITH THEIR TRA IN. FURTHER INVESTIGATION REVEALED THAT WHEN THE ENGINES WERE STAGED BY THE NICTD TERMINAL CAR MEN, NEITHER ENGINE HAD A HAND BRAKE APPLIED RESULTING IN THE ENGINES ROLLING OUT AND COLLIDING WITH THE TRAIN. DOWNLOAD REVIEW INDICATES THE CONSIST COLLIDED WITH THE TRAIN OF PF-10 AT 8.4 MPH RESULTING I N EXTENSIVE DAMAGE TO BOTH THE 2001 AND 2002. ESTIMATED DAMAGE ON THE CSS-2001 IS $50,000.00 AND THE CSS-2002 IS $78,000.00. NRC REPORT NUMBER 1264123.",False,False,True,False,True,128000.0
130,19,5,CSX,18,TERRE HAUTE,VIGO,"DECATUR AND EASTERN ILLINOIS RR WAS SHOVING BACK WITH 51 CARS , DERAILED THE LEADING 6 CARS OF THE S HOVE. BROKEN RAIL WAS THE DETERMINED TO BE THE ROUTE CAUSE. DECATUR AND EASTERN ILLINOIS RR SUSTAIN ED $186,910 IN EQUIPMENT DAMAGES.",False,True,False,False,False,186910.0
131,19,5,WC,18,GARY,LAKE,"DURING NORMAL, HUMPING OPERATIONS THE YARDMASTER PLACED THE HUMP SYSTEM INTO TRIM MODE, AND MANUALLY OPERATED THE RETARDERS, WHICH CAUSED GLCK8059 TO ROLL DOWN THE HILL UNRETARTED INTO TILX891969 STAL LED ON THE LEAD. DAMAGE TO GLCK8059 WAS REPORTED.",False,False,True,False,True,0.0
132,19,10,NICD,18,MICHIGAN CITY,LA PORTE,A MOTOR VEHICLE WAS TRAVELING ON THE SOUTH SIDE OF THE TRACKS AND WENT AROUND THE GATES AT GRACE STR EET HEADING NORTH AND COLLIDED WITH TRAIN 20.,False,False,True,False,False,0.0
133,19,5,WC,18,GARY,LAKE,"CN3209 AND CREX1508 WERE SHOVED OFF THE SOUTH PIT GOING WEST, AND WERE NOT COUPLED INTO THE SHOVING UNIT CN2658. CN3209 AND CREX1508 ROLLED DOWN THE SOUTH TRK CAUSING CN3209 TO COLLIDE.",False,False,True,False,False,0.0
134,19,7,NS,18,CHESTERTON,PORTER,61WB303 MAINLINE DERAILMENT OF 2 CARS AT MP CD 481.2,False,True,False,False,False,0.0
135,19,9,NS,18,LAFAYETTE,TIPPECANOE,"NS TRAIN 18KD128 DERAILED TILX 270627 (A-END, ALL WHEELS) DURING A STRAIGHT EASTWARD PULL.",False,True,False,False,False,0.0
136,19,2,RASX,18,INDIANAPOLIS,MARION,"ON 2-11-19, IT WAS DISCOVERED THAT SEVEN CARS THAT HAD BEEN SITTING ON TRACK 642 SINCE FRIDAY THE 8T H OF FEBRUARY, HAD ROLLED OUT AND RAN OVER A DERAIL AND STRUCK TWO CARS ON THE PARALLEL TRACK. THE C UT OF SEVEN CARS HAD FOUR HAND BRAKES APPLIED. THE CUT OF SEVEN CARS SAT IN PLACE FOR OVER 48 HOURS BEFORE THE ROLL OUT OCCURRED. FOLLOWING AN INVESTION AND AN INSPECTION OF THE CARS, IT WAS FOUND THA T THE BRAKES ON THREE OF THE FOUR CARS THAT WERE SET WERE FAULTY.",True,True,False,False,False,0.0
137,19,3,CSX,18,AUSTIN,SCOTT,"Q57611 STRUCK A VEHICLE STOPPED ON THE TRACKS AT AUSTIN, IN ON THE LIRC RAILROAD. LIRC REPORTS $18K IN DAMAGES. PROTECTION ALSO AT CROSSING: ADVANCE WARNING.",True,False,False,False,False,18.0
138,19,11,NS,18,ELKHART,ELKHART,WHILE ROLLING WEST DOWN THE HUMP THE WEST KNUCKLE FROM CAR TILX 252286 FELL OUT IN THE FROG. THE CAR THEN IMPACTED THE KNUCKLE AND CLIMBED UP AND OVER THE RAIL DERAILED ALL 4 AXLES CAUSING THE CAR TO STOP. THE TILX 252298 THAT WAS ROLLING DOWN THE HIILL BEHIND THE TILX 252286 BYPASSED COUPLERS WHEN IT TRIED TO COUPLE AND PUNCTURED THE END OF TILX 252286.,False,True,False,False,False,0.0
139,19,7,UP,17,EAST ST LOUIS,ST CLAIR,"THE AASAR-06 DEPARTING 1 PERIMETER FOR COTTONBELT YARD TRAVELING AT 5MPH, WAS PULLING 2 ENGINES AND 19 CARS PAST THE EAST END OF COTTONBELT TRACK 3 WHEN THE SWITCH ROD BROKE. IT WAS DETERMINED THAT T HE SWITCH ROD HAD APPROXIMATELY AN 85% OLD BREAK. THE NEXT SWITCH WAS DAMAGED AS WELL. ALS MAINTAIN S TRACK. ALS TRACK DAMAGE = $47,465. UP TRACK DAMAGE = $7,988. ALS EQUIPMENT DAMAGE = $22,250. U P EQUIPMENT DAMAGE = $8,409.",False,False,True,False,True,86112.0
140,19,4,UP,17,MELROSE PARK,COOK,"THE YPR33-25 WAS TRIMMING OUT BOWL TRACKS 64, 59, AND 63 WHEN THEY DERAILED 3 CARS DUE TO COUPLER MO UNTED BRACKET IN THE FLANGEWAY ON SWITCH 63. 1 DRUG POSITIVE - NOT DETERMINED TO BE A CAUSAL FACTOR .",False,True,False,False,False,0.0
141,19,4,UP,17,DUPO,ST CLAIR,"THE LOCOMOTIVE DEPARTMENT IMPROPERLY PLACED A DERAIL WITH NO BLUE FLAG ON TRACK 305 IN DUPO YARD, RE SULTING IN THE YDU31-17 GOING OVER THE DERAIL. THIS IS NOT A TRANSPORTATION CAUSED DERAILMENT BUT L OCOMOTIVE DEPARTMENT CAUSED DERAILMENT ACCOUNT MISUSE OF A DERAIL.",False,True,False,False,False,0.0
142,19,7,IC,17,UNIVERSITY PARK,WILL,"SB AMTRAK TRAIN, P39391-28 STRUCK A PICKUP TRUCK AT STUENKEL ROAD (DOT # 289680Y).",True,False,False,False,False,0.0
143,19,3,UP,17,MELROSE PARK,COOK,"YPR20R-21 DERAILED 2 RAILCARS IN BOWL TRACK 6. CGCX20382 SUSTAINED DAMAGE TO THE B-END CROSSOVER, I T WAS BENT DUE TO HARD IMPACT FROM ARMN933921. ARMN933921 HAD A-END MINOR DERAIL AND COMPLETE DESTR UCTION OF SLIDING SILL. WEPX3668 - A/B MINOR DERAIL. THE B-END COUPLER IS BROKEN TO INCLUDE END SI LL DAMAGE.",False,True,False,False,True,0.0
144,19,3,UP,17,MELROSE PARK,COOK,THE YPR36R-30 DERAILED DUE TO IMPROPER TRAIN HANDLING WHILE OPERATING IN YARD 9.,False,True,False,False,False,0.0
145,19,7,UP,17,MELROSE PARK,COOK,"WHILE SHOVING FROM YARD 2 TO COUNTY LINE 2 MAIN, THE YPR23R-02 WAS STRUCK BY A CUT OF CARS ROLLING O UT OF TRACK 805 IN YARD 01.",True,False,False,False,False,0.0
146,19,7,UP,17,NORTHLAKE,COOK,"YPR32R-06, FOUND ETTX700134 WAS CROSS-COUPLED WITH THE SOU88583 IN TRACK 42 DURING NORMAL HUMPING OP ERATION. NO DERAILMENT.",False,False,True,False,False,0.0
147,19,5,BRC,17,CHICAGO,COOK,"Q64708 TIED ONTO TRACK #39 AND ATTACHED A UTILITY MAN FROM BRC. CONDUCTOR GOT ON HEAD END AND THE CR EW BEGAN TO PULL EAST ON 5 LEAD. WHILE PULLING DOWN THE LEAD THE CREW DID NOT NOTICE THAT THE #35 SW ITCH WAS LINED AGAINST THEM . Q64708 CREW RAN THRU THE #35 AND CAME TO A STOP, THE CREW THEN WAS INS TRUCTED TO SHOVE BACK TO DOUBLE TRACK #38 AND WHILE SHOVING BACK, 4 CARS DERAILED.",False,True,False,False,False,0.0
148,19,9,UP,17,MELROSE PARK,COOK,"THE YPR43R-01 WAS KICKING CARS FROM THE WEST END OF YARD 4, WHEN THEY KICKED 3 LOADED TANK CARS INTO TRACK 339. UPON MAKING A JOINT WITH THE 15 OTHER CARS IN TRACK, ONE SET OF TRUCKS ON THE UTCX048324 DERAILED AND DAMAGED THE WEST END OF THE CAR.",False,True,False,False,True,0.0
149,19,9,UP,17,CHICAGO,COOK,"THE LYCG1R-01 CREW WAS MOVING ONTO THE BNSF FOR HEAD ROOM IN ORDER TO SHOVE BACK INTO TRACK 108. THE CREW FAILED TO STOP WITHIN HALF RANGE OF VISION FOR IMPROPERLY LINED SWITCH, THEY THEN RAN THROUGH 9 MAIN SWITCH. UPON SHOVING WESTWARD FOR TRACK 108 THE SWITCH WAS DAMAGED AND IT CAUSED CARS TO DERA IL AS WELL AS DAMAGE TO THE TRACK.",False,False,True,False,True,0.0
150,19,9,UP,17,NORTHLAKE,COOK,"YG204-14, WHILE SHOVING INTO TRACK 802 FROM THE EAST END, HAD THE RAIL BRAKE BENEATH THE ENGINE AND HEAD 4 CARS, DERAILING 2 CARS.",False,True,False,False,False,0.0
151,19,4,UP,20,HERINGTON,DICKINSON,THE LMF42-19 WAS MAKING A NORTHWARD SHOVING MOVEMENT WITH 91 CARS IN 003 TRACK WHEN 17 CARS ROLLED O UT THE NORTH END OF 003. THIS RESULTED IN 17 CARS RUNNING THROUGH THE 003 SWITCH AND 3 CARS RUNNING THROUGH MAIN 2 SWITCH BEFORE THE 17 CARS CHANGED DIRECTION AND DERAILED 2 CARS ON THE MAIN 2 SWITCH .,False,True,False,False,False,0.0
152,19,4,UP,20,KANSAS CITY,WYANDOTTE,IG4TU-26 WAS TRAVELING WEST PULLING INTO SIDING 210 WHEN RAIL CAR DTTX742810 AND THREE OTHER CARS DE RAILED.,False,False,True,False,False,0.0
153,19,7,UP,20,HAYS,ELLIS,"EMPLOYEE WAS RIDING A CUT OF 22 CARS SHOVING WEST WHEN THE 2ND CAR FROM WEST END DERAILED, CAUSING 4 CARS TO DERAIL. THE EMPLOYEE JUMPED FROM WEST REAR CAR TOWARD SOUTH SIDE OF TRACK IN ORDER TO AVOID BEING STRUCK BY MOVING CARS THEN RAN TO SAFETY.",True,True,False,False,False,0.0
154,19,8,UP,20,KANSAS CITY,WYANDOTTE,"THE MNPINP-19 WAS COMPLETING A SET OUT AT ARMOURDALE YARD. AFTER CUTTING AWAY FROM THE REAR PORTION OF THE TRAIN, THE TRAIN PULLING AHEAD TO CLEAR THE SWITCHES ON THE LEAD. THE ENGINEER BROUGHT THE TR AIN TO A STOP USING THE IDEPENDENT BRAKE AT 3MPH. THIS CAUSED EXCESSIVE BUFF FORCES IN THE TRAIN RES ULTING IN THE DERAILMENT OF THE A END OF THE MTNR175009. *KCT MAINTAINS TRACK. KCT TRACK DAMAGE = $3 ,900*",False,True,False,False,True,3.0
155,19,12,CSX,13,ATLANTA,FULTON,EMPLOYEE FAILED TO APPLY SUFFICIENT AMOUNT OF HANDBRAKES ON CARS TO BE LEFT UNATTENDED RESULTING IN A DERAILMENT.,False,True,False,False,False,0.0
156,19,11,NS,13,ATLANTA,FULTON,"119A113 DERAILED DTTX 787423, DTTX 646386, DTTX 732773, AOK 55172, DTTX 680004, BNSF 253085 AND DTTX 787954 WHILE PULLING NORTH IN FT07.",False,True,False,False,False,0.0
157,19,11,NS,13,ATLANTA,FULTON,"207G215 DERAILED DTTX 760950, DTTX 457845 AND DTTX 760585 WHILE PULLING NORTH THROUGH THE #2 CROSSOV ER OUT OF RECEIVING TRACK #2.",False,True,False,False,False,0.0
158,19,11,CSX,13,WAYCROSS,WARE,Y19729 FAILED TO STOP LIGHT LOCOMOTIVE IN TRACK R07 CAUSING IT TO STRIKE Q45228 INBOUND TRAIN.,False,False,True,False,False,0.0
159,19,11,SERX,13,RINCON,EFFINGHAM,"NS TRAIN 724G517, PULLING NORTH WITH 3 LOCOMOTIVES AND 95 LOADED COAL CARS, DERAILED 2 TRAIL LOCOMOT IVES AND 6 HEAD CARS. DERAILMENT BEGAN AT A LOCATION JUST BEFORE THE SERX/CSX CROSSING DIAMOND. TRAI LING TRUCK OF 2ND LOCOMOTIVE CLIMBED CLOSED POINT OF APPROACH DSP DERAIL ON HIGH RAIL, EXACT AXLE UN KNOWN. DERAILED AXLE(S) CONTINUED ACROSS FROGS OF SERX/CSX DIAMOND, PAST THE TRAILING DSP DERAIL AND INTO THE TURNOUT OF THE SOUTH CSX WYE TRACK. (NOTE: CSX INSTALLED 2 DSP DERAILS IN SERX TRACK ON EI THER SIDE OF SERX/CSX DIAMOND SOMETIME BETWEEN 9/25/19 TRACK INSPECTION AND 10/28/19 TRACK INSPECTIO N. AS A RESULT OF DISCUSSIONS WITH CSX AFTER THE DERAILMENT, SERX UNDERSTANDS THAT CSX INSTALLED TH E DERAILS ON SERX AS PART OF IMPLEMENTING PTC ON CSX. PURSUANT TO AN AGREEMENT WITH SERX, CSX ALSO HAS THE OBLIGATION TO MAINTAIN THE CROSSING. EXACT DATE OF DSP DERAIL INSTALLATION IS UNKNOWN BY SE RX. CSX PERFORMED THIS WORK ON SERX WITHOUT PERMISSION OR DESIGN APPROVAL OF SERX. SERX WAS NEVER CONTACTED BY CSX TO TAKE TRACK OUT OF SERVICE FOR INSTALL NOR TO COMMUNICATE PLANS OR NEED TO INSTAL L DSP DERAILS. DSP DERAILS WERE DISCOVERED DURING MONTHLY TRACK INSPECTION ON 10/28/19. APPROACH (N ORTHBOUND) DSP DERAIL HAD BEEN INSTALLED IN A CURVE AND THEREFORE DID NOT MEET CSX ENGINEERING STAND ARDS. ON 10/28/19 SERX INSPECTOR FOUND GAPS BETWEEN RAIL ENDS IN NEW BOLTED JOINTS, AND CURVATURE V ARIATIONS IN AREA OF NEW DSP DERAILS. NO FRA DEFECTS WERE NOTED BY THE INSPECTOR ON 10/28/19.)",False,True,False,False,False,0.0
160,19,9,ATK,9,STAMFORD,FAIRFIELD,BROKEN RAIL ON MNRR: TRAIN 2190 WITH SET 17 PC/2022 AND PC/2011 WAS DELAYED ON THE NEW HAVEN LINE D UE TO HAVING A TRUCK AND PROPULSION FAULTS AFTER OPERATING OVER A BROKEN RAIL AT CP 235. MNRR MECHA NICAL FORCES WERE ON THE SCENE AND CLEARED THE FAULTS AND OKAYED THE EQUIPMENT. DAMAGE TO BOTH TRUC KS ON REAR POWER CAR 2011.,False,False,True,False,True,0.0
161,19,2,ATK,9,NEW HAVEN,NEW HAVEN,"BOSTON CETC REPORTED THAT MECHANICAL FORCES WERE MAKING A SHOP MOVE WITH CDOT EQUIPMENT E/CT840 IN T HE LEAD, 4 COACHES AND E/CT1740 TRAILING. WHILE MOVING OUT OF THE SHOP ON 26 TRACK E/CT840 WENT OVE R A DERAIL IN THE DERAILING POSITION. E/CT840 DERAILED AXLE NUMBER ONE AND THE LOCOMOTIVE STAYED UP RIGHT. THERE WERE NO INJURIES TO REPORT. NRC REPORT # 1238119 WAS COMPLETED FOR THIS EVENT.",False,True,False,False,False,0.0
162,19,1,UP,8,DENVER,DENVER,CAR NW182553 WAS FOUND WITH A SHIFTED LOAD AND THE LOAD HAD TURNED INTO A SOLID PIECE OF LIME STONE OVER A PERIOD OF YEARS. NO DERAILMENT.,False,False,True,False,False,0.0
163,19,10,FEC,12,JACKSONVILLE,DUVAL,"CONDUCTOR ON JOB 10 TOLD ENGINEER TO BACK UP THAT HE WAS CLEAR 20 CARS AND FAILED TO PROTECT THE POI NT. SHOVED THE BOTTOM CAR, CNA 712436 INTO A FLAT, TTRX 360423, THAT WAS ON TRAIN 218-09 ON THE SOU TH END OF B-YARD LADDER. PRIOR TO INCIDENT, TRAIN 218-09 HAD ARRIVED AT FINAL DESTINATION, TRAIN SE CURED AND CREW REMOVED.",False,False,True,False,False,0.0
164,19,11,BLF,12,NORTH MIAMI BEACH,MIAMI-DADE,"BLF605 TRAVELING SOUTH BOUND ON THE EAST MAIN, WITNESSED A VEHICLE FOULING THE CROSSING AT NE 172ST. ENGINEER SOUNDED THE HORN AND BELL AND PLACED THE TRAIN IN EMERGENCY STRIKING THE VEHICLE. NO INJ URIES REPORTED. FEC DAMAGES: $353.08",False,False,True,False,False,353.08
165,19,3,CSX,12,MULBERRY,POLK,"WHILE TRAVERSING A TURNOUT, THE 71ST CAR (FURX 815348) OF TRAIN O73029 DERAILED DUE TO BEING IMPROPE RLY LOADED. THIS RESULTED IN THE 3 ADDITIONAL TRAILING CARS BEING DERAILED. LOAD ENGINEERING GROUP I NVESTIGATED AND DOCUMENTED THE IMPROPERLY LOADED CAR WITH SHIPPER.",False,True,False,False,False,0.0
166,19,6,MNCW,9,NORWALK,FAIRFIELD,"EASTBOUND TRAIN 1504 ON TRACK 2 STRUCK THE LEFT WING OF HERZOG'S BALLAST REGULATOR BR860-567 THAT WS A STATIONARY ON TRACK 4. DAMAGED CAUSED TO 7/8 CARS IS CONSIST. THE LEFT WING OF THE BALLAST REGULAT OR WAS NOT FULLY LOCKED AND SECURED BY OPERATOR, ALLOWING THE WING TO FOUL TRACK 4.",True,False,False,False,True,0.0
167,19,6,MNCW,9,NEW HAVEN,NEW HAVEN,"TRAIN 6524 WAS GIVEN PERMISSION TO TRACK 63 IN NEW HAVEN YARD AND TRAVELED WEST ON UNINTENDED TRACK 38, 41 TO 45, THEN OPERATED PAST THE `END OF WIRE` SIGN ON TRACK 45, CAUSING DAMAGE TO 4 PANTOGRAPHS IN THE CONSIST DUE TO HITTING A SPAN WIRE AND LOSING CONTACT WITH THE OVERHEAD WIRE. THE LOCOMOTIVE ENGINEER AND CONDUCTOR WERE UNFAMILIAR WITH THE YARD PHYSICAL CHARACTERISTICS AND THE GIVEN MOVE BY THE YARDMASTER.",False,False,True,False,True,0.0
168,19,4,ATK,9,NEW HAVEN,NEW HAVEN,"NORTHBOUND CSO-1, WITH TWO LOCOMOTIVES AND 17 CARS, DERAILED AND THEN RE-RAILED ONE CAR NORTH OVER A SWITCH. THERE WAS SIGNIFICANT DAMAGE TO THE SWITCH, RAIL AND TIES.",False,True,False,False,True,0.0
169,19,12,UP,6,ROSEVILLE,PLACER,"MPDWC-01 COMING IN THE YARD FROM THE EAST END 206, TIED DOWN 7 CARS AND THEIR DUPS IN THE RAIL. AFT ER CUTTING AWAY FROM THE CARS THE CREW PROCEEDED WEST IN ORDER TO SHOVE THEIR SET OUT IN 207. THE C ONDUCTOR WAS ON THE GROUND AT THE HOOK, WHILE THE ENGINEER IS PULLING OUT OF 206. THE ENGINEER STATE D THAT HE THOUGHT THE POINT WAS LINED FOR HIS ROUTE. THE ENGINEER PROCEEDED TO SHOVE BACK INTO 207 NOT AWARE OF THE 204 SWITCH BEING LINED AND DERAILED 3 CARS.",False,True,False,False,False,0.0
170,19,10,SCXF,12,PAHOKEE,PALM BEACH,A SEMI TRUCK AND TRAILER FAILED TO STOP AT THE WARNING STOP SIGN FOR A PRIVATE DIRT ROAD CROSSING A ND CROSSED IN FRONT OF ON-COMING TRAIN AND WAS STRUCK IN THE TRAILER BY THE CONTROLLING LOCOMOTIVE D ERAILING IT AND 3 FREIGHT CARS.,True,False,False,False,False,0.0
171,19,8,FEC,12,LANTANA,PALM BEACH,"BLF TRAIN 609 WAS HEADING SOUTHBOUND ON THE WEST MAIN TRACK AND OBSERVED A VEHICLE NOT IN THE CLEAR AT THE CROSSING AND STRUCK UNOCCUPIED VEHICLE. NO INJURIES WERE REPORTED. BLF DAMAGES WERE $13,852 .",True,False,False,False,False,13852.0
172,19,8,FEC,12,BOYNTON BEACH,PALM BEACH,"BLF 604 WAS TRAVELING SOUTHBOUND ON THE EAST MAIN WHEN THEY OBSERVED A VEHICLE GOING AROUND THE CROS SING GATES. THE ENGINEER PLACED THE TRAIN IN EMERGENCY BUT WAS UNABLE TO STOP PRIOR TO IMPACT. BLF DAMAGES WERE $26,339.",False,False,True,False,False,26339.0
173,19,8,FEC,12,DEERFIELD BEACH,BROWARD,"BLF 703 WAS TRAVELING SOUTBOUND ON THE WEST MAIN TRACK WHEN THEY OBSERVED A TRESPASSING VEHICLE GO A ROUND THE CROSSING GATES AT THE CROSSING. TRAIN STRUCK VEHICLE AND DRIVER/TRESPASSER SUSTAINED FATA L INJURIES. BLF DAMAGES WERE $40,457.",True,False,False,False,False,40457.0
174,19,1,UP,19,AMES,STORY,"WJSJSA-10, WHILE TRAVELING WEST TO DUMP BALLAST, THE TENTH CAR BACK STARTED TO DUMP ITS LOAD. THESE ARE AIR POWERED SIDE DUMP MOW BALLAST CARS. WITH THE CAR IN THE DUMPING POSITION, THE SIDE DOOR ST ARTED CLIPPING THE MDMBO-10 TRAIN THAT WAS ON ADJACENT TRACK. CAUSE WAS DETERMINED TO BE THE RELEAS E HANDLE VIBRATED OUT OF THE EXHAUST POSITION INTO THE DUMP POSITION WHILE TRAVELING DOWN THE TRACK. NO DERAILMENT.",False,False,True,False,False,0.0
175,19,2,IANR,19,WATERLOO,BLACK HAWK,"FEBRUARY 20, 2019
WATERLOO, IA., BRYANT YARD (SOUTH END LEAD)
HEAVY SNOW AND BLOWING SNOW -NEAR B LIZZARD CONDITIONS
AT APPROXIMATELY 12:57 PM, THE EXTRA XIANR4003N, ARRIVED BRYANT YARD WITH FIV E LOCOMOTIVES AND A 123-CAR TRAIN. THE CREW WAS INSTRUCTED TO BRING THEIR TRAIN DOWN TRACK 2. AS STA TED ABOVE, THERE WAS HEAVY SNOW AT THE TIME AND VISIBILITY WAS POOR. THE CONDUCTOR HAD DISMOUNTED FR OM THE TRAIN IN ORDER TO MAKE A CUT ON THE REAR PORTION OF THE TRAIN. AS THE MOVE PROGRESSED, THE E NGINEER WAS HAVING TROUBLE IDENTIFYING THE POSITION OF THE SWITCH POINTS / SWITCH TARGETS AND IN ADD ITION, THERE WAS AN “OFF TRACK” END-LOADER CLEARING SNOW FROM NEXT TO THE TRACKS. ONCE CLOSE ENOUGH TO SEE THE SWITCHES HE SAW THAT THE ROUTE WAS IN FACT LINED FOR HIS MOVEMENT.
AT THIS MOMENT, THE ENGINEER ALSO NOTICED THAT THE HEAD CAR ON THE MAIN TRACK WAS FOULING THE LEAD. HE APPLIED AN EMERGE NCY BRAKE APPLICATION; HOWEVER, HE WAS UNABLE TO STOP SHORT OF THE FOULING CAR, WHEREIN THE LOCOMOTI VES SIDESWIPED THE CAR, CAUSING LADDER AND HANDHOLD SAFETY APPLIANCES TO THE CAR AND THREE LOCOMOTIV ES.
UPON FURTHER INVESTIGATION AS TO HOW AND WHY THE CAR WAS LEFT OUT TO FOUL, IT WAS DETERMINED T HAT THE LOCAL TRANSPORTATION DEPARTMENT MANAGER HAD EARLIER INSTRUCTED A CREW TO LEAVE THE CAR AS IT WAS POSITIONED, WITH THE INTENT OF HAVING THE ABOVE MENTIONED INBOUND TRAIN CREW STOP AND PLACE THE CAR INTO THE CLEAR. THE MANAGER HOWEVER FAILED TO CONVEY THESE INSTRUCTIONS TO (SEE ATTACHED SHEET)",False,False,True,False,False,0.0
176,19,4,CSO,9,NEW HAVEN,NEW HAVEN,AMTRAK CALLED TO INFORM THAT THEY FOUND WHAT APPEARED TO BE DERAILMENT MARKS NEAR A TURNOUT. CSO 1 REPORTED NOTHING OUT OF THE ORDINARY WITH THEIR TRAIN IN THAT AREA AND AFTER INSPECTING THE CARS BEI NG DELIVERED TO CSX FOUND THAT THE FICX 8735 MAY HAVE DERAILED BUT HAD NO DAMAGE AND WAS BEING SHIPP ED TO BE SCRAPPED.,False,True,False,False,False,0.0
177,19,7,GRS,9,BRISTOL,HARTFORD,WHILE TRAVELING EAST ON WATERBURY BRANCH TRAIN CREW FELT A TUG AND BROUGHT TRAIN TO A STOP - INSPECT ED AND FOUND 6 CARS HAD DERAILED,False,True,False,False,False,0.0
178,19,9,MNCW,9,NEW HAVEN,NEW HAVEN,"TRAIN 1542 WAS OPERATING ON NEW HAVEN LINE TRACK 2 WHEN THE ENGINEER PASSED A STOP SIGNAL. THIS CAUS ED THE EQUIPMENT TO TRAVEL AN IMPROPERLY LINED SWITCH BEFORE STOPPING, CAUSING DAMAGE TO THE SWITCH AND COMPONENTS.",False,False,True,False,True,0.0
179,19,1,ARR,2,CANTWELL,DENALI,"AT APPROX. 0315 JANUARY 15, 130N KEY TRAIN EXPERIENCED UDE MP 317 TRAVELING 45 MPH. WHEN AIR DID NOT COME BACK UP THE CONDUCTOR WALKED BACK TO INSPECT FOUND THE GATX 72470 (B END) SOUTH SET OF TRUCKS WERE ON THE GROUND. TRAIN SEPARATED BETWEEN 36TH AND 37TH CAR. 37TH CAR BEING THE DERAILED GATX 7247 0. INITIAL INSPECTION REVEALED A HEAT DAMAGED R1 BEARING OF THE GATX 72470 ON THE GROUND AT APPROX. MP 309.5. DAMAGE TO THE TRACK WAS NOTED FROM MP314-MP 314.6.",False,True,False,False,True,0.0
180,19,11,NS,13,RINCON,EFFINGHAM,"724G517 PULLING NORTH WITH 3 LOCOMOTIVES AND 95 CARS, DERAILED 2 TRAIL LOCOMOTIVES AND 6 HEAD CARS .",False,True,False,False,False,0.0
181,19,12,UP,6,LATHROP,SAN JOAQUIN,"CONTRACT CREW WAS PLACING CONSIST IN TRACK FOR OUTBOUND DEPARTURE. CONTRACT ENGINEER PULLED INTO TR ACK AND STOPPED SHORT OF DERAIL AS IS PROCEDURE. ENGINEER CLAIMS TO HAVE LOOKED AT DERAIL AND NOT A T THE SWITCH TARGET, WHEN HE LOOKED HE THOUGHT THE DERAIL WAS DOWN. ENGINEER BEGAN PULLING INTO TRA CK AND WENT OVER DERAIL IN DERAILING POSITION. ONE SET OF TRUCKS ON UP8769 IN THE DIRT.",False,True,False,False,False,0.0
182,19,7,CSX,12,OXFORD,SUMTER,Q45318 STRUCK TRAILER DUE TO THE TRAILER BEING TOO LOW AND GETTING STUCK ON CROSSING. AGE UNKNOWN.,True,False,False,False,False,0.0
183,19,8,CSX,12,HIALEAH,MIAMI-DADE,"Y12018 PULLED THROUGH H01 SWITCH RAN THROUGH THE SWITCH AND MADE A REVERSE MOVEMENT RESULTING IN A 3 CAR DERAILMENT. SFRV IS REPORTING 14,550 IN DAMAGES.",False,True,False,False,False,0.0
184,19,10,FEC,12,JACKSONVILLE,DUVAL,"CONDUCTOR ON JOB 10 TOLD ENGINEER TO BACK UP THAT HE WAS CLEAR 20 CARS AND FAILED TO PROTECT THE POI NT. SHOVED THE BOTTOM CAR, CNA 712436, INTO A FLAT, TTRX 360423, THAT WAS ON TRAIN 218-09 ON THE SO UTH END OF B-YARD LADDER. PRIOR TO INCIDENT, TRAIN 218-09 HAD ARRIVED AT FINAL DESTINATION, TRAIN S ECURED AND CREW REMOVED.",False,False,True,False,False,0.0
185,19,10,FEC,12,MIAMI-DADE,MIAMI-DADE,"WHILE SHOVING AN EMPTY CUT OF HOPPERS INTO A CUSTOMER'S TRACK, THE LEAD WHEEL DERAILED IN A CURVE ON COMPACTED DIRT THAT WAS CAUSED BY A FRONT END LOADER THAT HAD JUST CLEANED THE TRACK.",False,True,False,False,False,0.0
186,19,10,SFRV,12,FORT LAUDERDALE,BROWARD,"AT 1654 HRS, P632 REPORTED STRIKING A TRACTOR TRAILER THAT WAS FOULING CROSSING AT MPSX 1007.8 WHILE TRAVELING NORTH ON #2 TRACK.",False,False,True,False,False,0.0
187,19,12,UP,6,ROSEVILLE,PLACER,"YRV12R-06 WAS PULLING OUT A CUT OF 123 CARS FROM RECEIVING TRACK 204 TO THE HUMP LEAD, WHEN IT DERAI LED 5 CARS. THE TRAIN PULLED 56 CARS OVER TRACK 108 CROSSOVER WHEN 5 CARS DERAILED IN THE MIDDLE O F THE CUT AT THE SWITCH POINT. NO HAZMAT OR ANY INJURIES.",False,True,False,False,False,0.0
188,19,10,UP,6,VERNON,LOS ANGELES,"BNSF TRAIN WAS PULLING OUT OF LOS ANGELES JUNCTION RAILROAD AND RAN THROUGH THE RED SIGNAL AND OVER THE DERAIL AT BANDINI ROAD CROSSING. BNSF EQUIPMENT DAMAGE = $30,000",False,True,False,False,True,30000.0
189,19,1,TASD,1,MOBILE,MOBILE,TASD 8 PULLING 3 BOXCARS TOWARDS THE BANDA VESSEL LOWER DECK WHEN THE CONNECTING COUPLERS BETWEEN TA SD TRACKMOBILE AND ATW 7507 FAILED TO ARTICULATE ALLOWING LATITURAL FORCES DERAILING TRACKMOBILE AT THE FROG. INVESTIGATION RESULT WAS THE TRACKMOBILE COUPLING DID NOT ARTICULATE.,False,True,False,False,False,0.0
190,19,10,UP,6,STIRLING CITY,SAN JOAQUIN,LRS51-21 COLLIDED WITH AN UNOCCUPIED VEHICLE AT MP 90.37 / OAKLAND SUB / AT CROSSING INDUSTRIAL & MC KINLEY.,False,False,True,False,False,0.0
191,19,2,CSX,1,HELENA,SHELBY,Q52006 MOVING NORTH ON THE MAINLINE STRUCK UNOCCUPIED TRACTOR TRAILER STUCK ON THE TRACK. PROTECTION ALSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS (STOP LINES & RR XING SYMBOLS).,True,False,False,False,False,0.0
192,19,2,NS,1,VANCE,TUSCALOOSA,"A39 WAS PULLING CARS NORTH OUT OF KYKENKEE TO GO BACK TO THE MAINLINE. THEY HAD 2 ENGINES AND 17 CAR S. AS THEY WERE PULLING OUT, THE BRAKEMAN THREW THE SWITCH POINT DERAIL UNDER THE 16TH CAR CAUSE TRA VERSE THE DERAILING ROUTE. THIS RESULTED IN THE BOOTTOM 7 CARS OF THE TRAIN TO DERAIL.",False,True,False,False,False,0.0
193,19,9,NS,1,IRONDALE,JEFFERSON,"NS TRAIN M5TA608 WAS SHOVING NORTH INTO RT06 AND DERAILED THE R3/L3 WHEEL ON TBOX 666913 AND THE R3/ L3, R4/L4 WHEELS (A END TRUCK) ON TBOX 660526 DUE TO EXCESSIVE FORCE ON THE DRAWBARS.",False,True,False,False,False,0.0
194,19,9,NS,1,IRONDALE,JEFFERSON,"WHILE SHOVING SOUTH ON THE WEST PULLBACK, NS CREW AB17 DERAILED NS 120203 (ALL WHEELS) AND JTSX 9000 06 (B-END TRUCKS) DUE TO DEBRIS IN THE FLANGEWAY.",False,True,False,False,False,0.0
195,19,9,AGR,1,MOBILE,MOBILE,"411R DERAILED THREE (3) LOCOMOTIVES IN TASD TRACK 27.
AGR CREW, AGR EQUIPMENT ($1000), TASD TRACK ( $15385)
12-09-19 REVISED BLOCKS 30/TYPE OF TERRITORY, 31(2-A, B, C)/CAUSING, 50/LATITUDE, 51/LONGIT UDE",False,True,False,False,False,16385.0
196,19,8,CSX,1,DECATUR,MORGAN,Y10105 DID NOT MAKE SURE CAR WAS IN CLEAR WHILE IN SWITCHING OPERATION AND STRUCK SINGLE STANDING CA R.,True,False,False,False,False,0.0
197,19,4,NS,13,MACON,BIBB,"GM42 PULLING NORTH ON EAST PULLBACK WITH 41 CARS HAD THE BOTTOM 32 CARS SEPARATE AT TILX 290206, DUE TO A BYPASS COUPLING OF TILX 290206 AND ADMX 63258. TILX 290206 AND THE TRAILING CARS ROLLED SOUTH, STRIKING EQUIPMENT IN FT03, FT04, ANF FT05. THHE IMPACTS CAUSED CCBX 71669, GATX 31261, CPCX 815316 AND NS 994646 IN THE FREE-ROLLING CUT TO DERAIL, ALONG WITH DERAILING NW 196084 IN FT05 AND MWCX 82 0085 AND PMRX 5690 IN FT03. ADMX 28792 IN FT04 WAS STRUCK AND DAMAGED, BUT NOT DERAILED.",True,False,False,False,True,0.0
198,19,6,BNSF,17,GALESBURG,KNOX,RCO Y-GAL2022-16 HAD RAILCARS IMPACT EACH IN YARD TRACK 2003 DURING HUMP OPERATIONS DUE TO AUTOMATIC HUMP RETARDER FAILURE TO SUFFICIENTLY SLOW RAILCARS. THE IMPACT RESULTS IN 2 RAILCARS DERAILED AND EQUIPMENT DAMAGES. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
199,19,9,ALS,17,EAST ST LOUIS,ST CLAIR,"AASFX-05 WAS PULLING OUT OF GATEWAY YARD IN WHEN 6 CARS DERAILED. THE CAUSE OF THE DERAILMENT WAS FR OM THE FLANGE CUTTING INTO AND CLIMBING THE LOW SIDE OF THE RAIL AT A POINT WHERE THE GAUGE OF THE R AIL WENT FROM 57.5 INCHES TO 56 INCHES IN A 10 FOOT SPAN. THE WHEEL WAS HUNTING TO NEGOTIATE THE ARE A WHEN IT CLIMBED UP THE RAIL RESULTING IN THE DERAILMENT. **ALS MAINTAINS TRACK. ALS TRACK DAMAGE=$ 26, 455**
REVISED ON 11/25/19",False,True,False,False,False,0.0
200,19,9,ALS,17,EAST ST LOUIS,ST CLAIR,"AASFX-12 CREW DEPARTED OFF OF 6 PERIMETER. THE CREW PULLED APPROXIMATELY 40 CARS THRU THE ST. LOUIS HORN WHEN 13 CARS DERAILED
REVISED ON 11/25/19",False,True,False,False,False,0.0
201,19,8,UP,17,VENICE,MADISON,"THE MNLTR-01 WSA YARDING THEIR TRAIN INTO THE TRRA YARD IN TRACK TWO. CONDUCTOR MADE THE CUT AND PUL LED TRAIN AHEAD. AFTER TRAVELING TWO CAR LENGTHS, THE TRAIN WENT INTO EMERGENCY. CONDUCTOR FOUND CAR FTTX961443 DERAILED. CAUSE WAS DUE TO WIDE GAGE. TRRA MAINTAINS TRACK. TRRA TRACK COST = $6,072",False,True,False,False,False,6072.0
202,19,10,NS,1,JONES,DALLAS,"WHILE WORKING INTERNATIONAL PAPER, A86 DERAILED 3 CARS AS A RESULT OF A BROKEN SWITCH POINT. CAR CRD X 18015 RELEASED APPROXIMATELY 100 LBS OF SODIUM CHLORATE CLASS 5.1 UN14.",False,True,False,False,False,0.0
203,19,4,NS,1,IRONDALE,JEFFERSON,"AB20 HUMPING IN FULL AUTOMATIC CUT 1X1 INTO CT35 WHEN THE GATX 5335 ROLLED OUT OF THE CT35 AND STRUC K AB41 ON THE EAST LADDER, DERAILING THE GATX 5335",False,True,False,False,False,0.0
204,19,6,NS,1,GADSDEN,ETOWAH,"A54 WAS SHOVING 2 ENGINES, 19 CARS AND 1,627 TONS DOWN THE GS BRANCH. CARS 10-14 DERAILED DUE TO RAI L ROLLING UNDER THE MOVEMENT. NO EXCEPTION TAKEN TO TRAIN HANDLING.",False,True,False,False,False,0.0
205,19,8,NS,18,ELKHART,ELKHART,"DUE TO REPETITIVE IMPACT FROM HUMPING INTO CT31, ADMX 31001 WAS PUSHED OUT OF THE SKATES AND ROLLED INTO THE FOUL OF THE LEAD.IT WAS STRUCK BY RCO UNIT NS 6142, PULLING OUT OF CT38, CAUSING A SIDE SWI PE DERAILMENT AND ADMX 31001 TO ROLL ONTO ITS SIDEE. 5,000 GALLONS OF ALCOHOLS, N.O.S. CLASS 3 UN198 WERE RELEASED.",True,True,False,False,False,0.0
206,19,8,NS,18,ELKHART,ELKHART,BE23 RCO FOREMAN MADE AN OVER SPEED COUPLING IN CT65 DAMAGING NS 6143.,False,False,True,False,False,0.0
207,19,6,NS,1,RANDOLPH,BIBB,"CREW KICKED A GATX 063364 CAR INTO NY04 AND THEN KICKED AN UTLX 641942 INTO THE SAME TRACK RESULTING IN THE CARS MISMATCH, MISSING THE COUPLER AND HITTING THE PLATFORM OF UTLX 641942 CAUSING THE EAST RAIL TO ROLL AND DERAILING L1, L2, R1 & R2 OF THEUTLX 641942 AND R1 & R2 OF THE GATX 063364",False,True,False,False,False,0.0
208,19,6,NS,1,IRONDALE,JEFFERSON,"AB41 WITH 3 UNITS AND 28 CARS WERE SHOVING ON THE WEST PULLBACK TO WF02 WHEN THE RAIL BROKE UNDER MO VEMENT. SUBSEQUENTLY, DERAILING CARS NW 189350, CKIX 410060, AND FURX 839343",False,True,False,False,False,0.0
209,19,12,NS,1,IRONDALE,JEFFERSON,"AB21 PULL BACK JOB PULLED INTO TRACK CT03 AND DERAILED THE LEAD SET OF TRUCKS OVER THE CT03 SWITCH I N THE CLASS YARD DUE TO SWITCH POINTS BREAKING UNDER MOVEMENT NS 3345 DERAILED THE L4, L5, L6, R4, R 5, R6 WHEELS.",False,True,False,False,False,0.0
210,19,12,NS,1,MUSCLE SHOALS,COLBERT,"YARD JOB AH05 SHOVED A CUT OF 39 CARS WESTWARD INTO CLASS TRACK 14. MIDWAY THROUGH THE SHOVE, THE 13 TH, 14TH, 15TH, 16TH AND 17TH HEAD CARS DERAILED ON THE WEST CROSS OVER OF THE CLASS YARD HEADING IN TO CLASS TRACK 14.",False,True,False,False,False,0.0
211,19,9,CSX,1,CHILDERSBURG,TALLADEGA,A73604 CSX CREW DERAILED DUE TO WIDE GAGE ON NORFOLK SOUTHERN MAINTAINED TRACK. NS ESTIMATED DAMAGES : $1561.94,False,True,False,False,False,1561.94
212,19,10,NS,1,IRONDALE,JEFFERSON,"NS CREW AB40 WAS HUMPING PMRX 867389 AND 867367 INTO CT08 WHEN THEY ROLLED OUT AND STRUCK NS TRAIN A B884 THAT WAS PULLING OUT OF CT05, DERAILING PMRX 867389.",True,True,False,False,False,0.0
213,19,7,ABS,1,GORDO,PICKENS,***SEE ATTACHED DESCRIPTION***,False,False,True,False,False,0.0
214,19,10,NS,1,IRONDALE,JEFFERSON,"NS CREW AB10 WAS HUMPING GATX 212845 INTO CT10 WHEN IT OVERSPED AND STRUCK NS TRAIN AB21 IN THE WEST PULLBACK THAT WAS PULLING OUT OF CT35, DERAILING GATX 212845.",True,True,False,False,False,0.0
215,19,8,ABS,1,REFORM,PICKENS,"ABS HY-RAIL 4615 WAS TRAVELING WEST BEHIND SPERRY UNIT#974, UNIT 974 WAS STOPPED ON THE TRACK AT MP3 9.7 ON THE TUSCALOOSA SUB LOOKING AT A POSSIBLE RAIL DEFECT. DURING THIS TIME THE OPERATOR OF ABS UN IT 4615 WASN'T PAYING ATTENTION TO HIS SURROUNDINGS RESULTING IN THE TWO UNITS TO COLLIDE. THE ABS H Y-RAIL DID HAVE ANOTHER WATCO TEAM MEMBERS PRESENT IN THE VEHICLE, THIS TEAM MEMBER STATED THAT HE W AS LOOKING AT HIS PHONE WORKING ON SENDING HIS SUPERVISORS TWO DEFECTS THAT WHERE PREVIOUSLY FOUND F OUR MILES BACK DOWN THE TRACK.",False,False,True,False,False,0.0
216,19,5,NS,39,CINCINNATI,HAMILTON,UTILITY BRAKEMAN FAILED TO ENSURE EQUIPMENT WAS SECURED PRIOR TO KICKING OTHER CARS INTO TRACK RESUL TING IN EQUIPMENT ROLLING OUT AND STRIKING OTHER CARS. THIS RESULTED IN A TWO CAR DERAILMENT.,False,True,False,False,False,0.0
217,19,3,RRVW,38,GWINNER,SARGENT,PULLING CUT OF CARS FROM TREAM TRACK. 3 EMPTY CARS DERAILED IN THE TURN OUT DUE TO SNOW AND ICE COND ITIONS,False,True,False,False,False,0.0
218,19,3,RCPE,31,CHADRON,DAWES,TRAIN WENT OVER A BROKEN RAIL AND 8 CARS DERAILED. 6 WERE ON THEIR SIDD OFF OF THE RIGHT OF WAY AND 2 WERE HANGING BY THEIR COUPLERS.,False,True,False,False,False,0.0
219,19,4,IC,22,GEISMAR,ASCENSION,"AT 0055 CDT ON APRIL 17TH GEISMAR YARD ASSIGNMENT R98271-16, WHILE IN THE PROCESS OF PULLING OUT OF THE NORTH LEAD OF GEISMAR YARD WITH GTW 5827, MADE CONTACT WITH EMPTY CARS PTTX 146767 AND PTTX 1361 93 ON L58271-16. PTTX 146767 DERAILED ONE SET OF TRUCKS ON THE B-END, PTTX 136193 DERAILED ONE SET O F TRUCKS ON THE A-END AND UNIT GTW 5827 DERAILED ALL WHEELS. NO INJURIES AND NO DANGEROUS GOODS INVO LVED.",False,True,False,False,False,0.0
220,19,4,IC,22,GEISMAR,ASCENSION,"AT 0055 CDT ON APRIL 17TH GEISMAR YARD ASSIGNMENT R98271-16, WHILE IN THE PROCESS OF PULLING OUT OF THE NORTH LEAD OF GEISMAR YARD WITH GTW 5827, MADE CONTACT WITH EMPTY CARS PTTX 146767 AND PTTX 1361 93 ON L58271-16. PTTX 146767 DERAILED ONE SET OF TRUCKS ON THE B-END, PTTX 136193 DERAILED ONE SET OF TRUCKS ON THE A-END AND UNIT GTW 5827 DERAILED ALL WHEELS. NO INJURIES AND NO DANGEROUS GOODS INV OLVED.",False,True,False,False,False,0.0
221,19,3,LSI,26,PALMER,MARQUETTE,"0700 WEIGHER JOB WAS IN THE PROCESS OF RUNNING AROUND THEIR TRAIN ON THE TILDEN MAIN WITH A SET OF L IGHT LOCOMOTIVES, WHEN THE LEAD LOCOMOTIVE (CEFX 1005) DERAILED DUE TO SNOW/ICE/PELLET BUILD-UP ON T RACK. AS A RESULT THE LOCOMOTIVE MADE CONTACT WITH THE CARS THAT WERE PARKED ON THE SIDING. DAMAGE T O BOTH LOCOMOTIVE AND RAILCAR.",False,True,False,False,True,0.0
222,19,10,HESR,26,AKRON,TUSCOLA,"HESR 805-30 WENT INTO AN UNDESIRED EMERGENCY. THE CONDUCTOR WALKED BACK AND FOUND THE 16TH CAR HAD D ERAILED AND WAS ON ITS SIDE. IT WAS DISCOVERED THAT THE CRDX 8719 (LINE 16 IN TRAIN) STRUCK FURX 826 200 THAT WAS ON SPOT AT CO-OP ELEVATOR WHILE TRAIN WAS TRAVELING PAST AND DERAILED IT. THE FURX 8262 00 WAS ON SPOT AT AKRON CO-OP ELEVATOR AS THE HESR 805-30 WAS TRAVELING WEST ON THE MAIN LINE, THE C RDX WAS ROCKING FAR ENOUGH SIDE TO SIDE IT STRUCK THE FURX DERAILING IT AND DRAGGING IT DOWN THE TRA CK OVER THE PERMANENT DERAIL THROWING IT SIDEWAYS OUT INTO THE PUBLIC ROAD. THE FURX 826200 WAS NO T PART OF THE CONSIST OF THE HESR 805-30.",True,True,False,False,False,0.0
223,19,3,NS,26,DETROIT,WAYNE,"TRAIN 38EB030 CO LEFT EQUIPMENT ON MAIN IN LIVERNOIS YARD, FOULING LEAD INTO #9 TRACK. CO THEN SHOVE D INTO #9 TRACK SIDE SWIPING HIS STANDING CUT OF CARS ON MAIN.",False,False,True,False,False,0.0
224,19,9,UP,29,KANSAS CITY,JACKSON,"THE YKC17R-06 BEGAN A SHOVING MOVE OUT OF BOWL 16 AND INTENDED TO SHOVE INTO ZONE 1. THE SWITCHMAN I N THE DOLLHOUSE FAILED TO LINE THE SOUTH SIDE CROSSOVER INTO ZONE 1. THE CROSSOVER WAS LINED INTO ZO NE 2, WHERE THE YKC37R-06 WAS PULLING INTO TRK 305 IN ZONE 2, RESULTING IN THE UP2030 COLLIDING WITH THE YKC37R'S CUT OF CARS AT 4.4 MPH. SWITCHMAN STOPPED THE MOVEMENT WHEN THE OCU SHOWED A ROLL-BACK ERROR ON THE BOX.",False,False,True,False,False,0.0
225,19,4,NS,29,WENTZVILLE,ST CHARLES,"DW26 SHOVING 21 LOADED AUTO RACKS, DERAILED THE R1, R2, L1 AND L2 WHEELS ON TTGX987940.",False,True,False,False,False,0.0
226,19,8,UP,29,KANSAS CITY,JACKSON,"THE YKC35R-06 WAS HUMPING TRACK 104 UP THE SOUTH LEAD OF THE HUMP, THEY HAD 34 CARS LEFT ON THE CUT WHEN THE TTZX84681 DERAILED AT THE SOUTH ESCAPE FROG. THE MOVEMENT COMMAND SPEED WAS 1.7 AND SPEED W AS 1.6 MPH AT THE TIME OF DERAILMENT. TOTAL DISTANCE MOVED IN COMMAND SPEED OF 1.7 MPH WAS 1284 FT B EFORE POINT OF DERAILMENT AND TOP SPEED DURING MOVE WAS 1.9 MPH. TOTAL DISTANCE TRAVERSED AFTER POD WAS 331 FT CAUSING TRACK DAMAGE. CAUSE WAS DUE TO INTERACTION OF LATERAL AND VERTICAL FORCES.",False,True,False,False,True,0.0
227,19,9,BNSF,29,RUSHVILLE,BUCHANAN,"E-MLMNRM0-02 WAS IMPACTED BY A VEHICLE, NOT AT A ROAD CROSSING, WHILE TRAVERSING MAIN 2 TRACK RESULT ING IN SIGNAL AND RAILCAR DAMAGES. NO HAZARDOUS MATERIALS WERE RELEASED.",False,False,True,False,False,0.0
228,19,6,CSX,26,ROMULUS,WAYNE,"WHEN SPOTTING EQ INDUSTRY, D71607 DERAILED ONE CAR BY SHOVING OFF END OF TRACK AND DAMAGED INDUSTRY BUMPING POST.",False,True,False,False,True,0.0
229,19,3,MQT,26,FILER CITY,MANISTEE,"THE MANISTEE-21 CREW WAS SWITCHING PACKAGING CORPORATION OF AMERICA WITH 16X12 WHEN FOUR LOADED ASPH ALT TANK CARS (SEQUENCE: 13, 14, 15, 16) DERAILED NEAR THE GATE BETWEEN MQT AND TONDU (PACKAGING COR PORATION OF AMERICA). 4 HAZMAT (CLASS 9) CARS DERAILED, UPRIGHT AND NOT LEAKING.",False,True,False,True,False,0.0
230,19,10,CSX,1,MOBILE,MOBILE,Y29111 SWITCHMAN FAILED TO TEST THE HAND BRAKE ON ENGINE CSXT 8214 ALLOWING IT TO ROLL INTO THE FOUL OF THE DIESEL SHOP LEAD TRACK AND WAS STRUCK BY ENGINE CSXT 4324.,True,False,False,False,False,0.0
231,19,2,ATK,18,BROWNSBURG,HENDRICKS,"TRAIN 50 OPERATING WITH LOCOMOTIVE E/40 AND 6 CARS STRUCK AN OCCUPIED VEHICLE AT MP 13.95, HUNTER RD CROSSING. THE OCCUPANT IN THE VEHICLE WAS A FATALITY.",True,False,False,False,False,0.0
232,19,3,LIRC,18,AUSTIN,SCOTT,"Q576.11 WAS TRAVELING NORTH WHEN LEAD ENGINE CSXT 3337 STRUCK VEHICLE AT HWY GRADE CROSSING. THE VEH ICLE TRAVERSED THE CROSSING IN A WEST DIRECTION, STOPPED, AND REMAINED STOPPED FOR ROUGHLY 30 SECOND S WITH THE TRAILER FOULING THE TRACKS BEFORE IT WAS STRUCK BY THE TRAIN. THE DRIVER REPORTED NO INJU RIES AND DENIED MEDICAL TREATMENT. BOTH CREW MEMBERS WERE IN THE LOCOMOTIVE AT THE TIME OF THE INCID ENT. THE CROSSING IS EQUIPPED WITH FLASHING LIGHTS, STOP SIGN AND CROSS BUCKS, BOTH MAST WERE CONFIR MED TO BE FUNCTIONING AS INTENDED. NO SIGHT OBSTRUCTIONS WERE PRESENT AT THE CROSSING ON ANY QUADRAN T APPROACH.",True,False,False,False,False,0.0
233,19,11,BLF,12,NORTH MIAMI BEACH,MIAMI-DADE,"BLF 606 WAS TRAVELING SOUTH BOUND ON THE WEST MAIN TRACK, A VEHICLE WAS STOPPED ON THE CROSSING AT M P 352.06 NE 203RD STREET. RESULTING IN A FATALITY TO THE DRIVER OF THE VEHICLE. FEC DAMAGE TOTAL $960.29",False,False,True,False,True,960.29
234,19,11,FEC,12,MIAMI-DADE,MIAMI-DADE,"TAEX 3279 WAS CUT OFF IN TRACK 5 AND FOULING TRACK 6. CREW ATTEMPTED TO SHOVE INTO TRACK 6 WITH SKS X 101382 AND SIDESWIPED STANDING CAR, TAEX 3279.",False,False,True,False,False,0.0
235,19,11,FEC,12,MIAMI-DADE,MIAMI-DADE,"TAEX 3279 WAS CUT OFF IN TRACK 5 AND WAS FOULING TRACK 6. CREW ATTEMPTED TO SHOVE INTO TRACK 6 WITH SKSX 101382 AND SIDESWIPED STANDING CAR, TAEX 3279.",False,False,True,False,False,0.0
236,19,8,UP,17,NORTHLAKE,COOK,"THE YPR11R-08 KICKED 11 LOADED CARS INTO THE NORTH END OF TRACK 11. TRACK 11 ROLLED OUT AND THE UP97 538 STRUCK THE DTTX469295 OF THE CANADIAN PACIFIC TRAIN CPG41-08, WHICH WAS YARDING INTO TRACK 2. *C P REPORTED $32,944 IN EQUIPMENT DAMAGES.*",True,False,False,False,False,32944.0
237,19,8,UP,17,MELROSE PARK,COOK,THE YPR14R-09 WAS HEADED NORTHBOUND ON THE SOUTH LEAD IN YARD 9. THEY WENT OVER THE 212/213 LEAD SWI TCH AND THE REAR TRUCKS PICKED THE SWITCH BECAUSE IT HAD BEEN RUN-THROUGH BY A PREVIOUS JOB. THE CAN ADIAN PACIFIC G41 JOB HAD USED THE LEAD 15-20 MINUTES PRIOR TO COME SOUTH DOWN THE LEAD AND IT IS BE LIEVED THEY RAN THRU THE SWITCH.,False,False,True,False,False,0.0
238,19,8,UP,17,WEST CHICAGO,DU PAGE,"THE ACNNP-13, WHILE PULLING ONTO THE ST. CHARLES LEAD DERAILED 6 CARS. CAUSING DAMAGE TO THE WESTEND CROSSOVER TO THE MAIN LINE AND ONTO THE ST. CHARLES LEAD.",False,True,False,False,True,0.0
239,19,8,UP,17,CHICAGO,COOK,RAILCAR TILX250286 FOUND DAMAGED. NO DERAILMENT OR TRACK DAMAGE.,False,False,True,False,True,0.0
240,19,8,UP,17,NORTHLAKE,COOK,RAILCAR CEFX76194 FOUND WITH SIDE SILLS BENT. LOCATION AND TIME OF DAMAGE UNKNOWN. NO DERAILMENT OR TRACK DAMAGE.,False,False,True,False,True,0.0
241,19,1,NS,13,MACON,BIBB,"GM02 PULLING OUT OF CT15 WITH 33 CARS WHEN 27TH HEAD CAR NS 469241 A-END, 28TH NS 469392 ALL WHEELS, 29TH NS 469397 ALL WHEELS, AND 30TH HEAD CAR NS 469266 A-END DERAILED ON THE CLASS YARD LEAD.",False,True,False,False,False,0.0
242,19,1,NS,13,TOCCOA,STEPHENS,"CREW ALLOWED CARS TO ROLL FREE BEYOND 8 CAR LENGTHS TO STANDING EQUIPMENT, WHICH VIOLATES TIME TABLE INSTRUCTIONS FOR SWITCHING TOCCOA YARD.",False,False,True,False,False,0.0
243,19,3,TRRA,17,EAST ST LOUIS,ST CLAIR,PLEASE SEE UPRR NARRATIVE FOR DETAILS.,False,False,True,False,False,0.0
244,19,8,ATK,17,CHICAGO,COOK,"OPERATING RULE VIOLATION: ALLEGED PERFORMANCE OF IMPROPER CLASS 2 BRAKE INSPECTION PRIOR TO DEPARTI NG CHICAGO UNION STATION ON STATION TRACK #1 ON AMTRAK TRAIN 343 DESTINED FOR MILWAUKEE, WI. ENGINE AT REAR OF TRAIN CONSIST, AMTK 34, WAS DRAGGED 3.2 MILES TO TOWER A3 WITH SLIDE WHEELS, CREATING CO NDEMNABLE FLAT SPOTS. CAUSE: FAILURE TO PERFORM PROPER BRAKE TEST PRIOR TO DEPARTURE. EVENT WAS DI SCOVERED DURING AN INSPECTION IN MILWAUKEE. CONSIST SPEED IS UNKNOWN.",False,False,True,False,False,0.0
245,19,8,ATK,17,CHICAGO,COOK,TRAIN SEPARATION: TRAIN HAD UNDESIRED TRAIN SEPARATION WHILE SHOVING FROM CUS TO THE YARD VIA NEW T AYLOR LEAD. DAMAGE TO THE 4621. CAUSE: FAULTY COUPLER SYSTEM.,False,False,True,False,True,0.0
246,19,2,NS,17,CHICAGO,COOK,"BC36 WAS PULLING EASTWARD ON TRACK CT30, WHEN THE REAR CAR DTTX 890068 STARTED TRAVERSING DOWN THE A DJACENT TRACK, DERAILING CARS DTTX890068 R5-R8, L5-L8, DTTX 655808 R1,R2,L1,L2 AND DTTX 56007 R1, R4 , L1, L4.",False,True,False,False,False,0.0
247,19,6,IC,1,MOBILE,MOBILE,"CN BELT PACK SIDE SWIPED NS TRAIN A94A4-11 IN YARD LIMITS, NS TRAIN DERAILED 4 LOADED ASPHALT CARS. 3 DERAILED ON THEIR SIDE AND 1 DERAILED UPRIGHT. NO LEAKS, EXPOSURES OR INJURIES REPORTED.",False,True,False,False,False,0.0
248,19,1,NS,1,IRONDALE,JEFFERSON,"AB01 RCO HUMP ASSIGNMENT PULLING SOUTH AFTER SETTING OUT A BAD ORDER TO THE HILL TRACKS, WHEN THE TR AIN EXPERIANCED A BROKEN KNUCKLE AT THE 44TH HEAD CAR AOK 113105. RCO WAS UNAWARE OF THE SEPERATION AND CONTINUED PULLING SOUTH IN THE PULLBACK PROTECCTED TRACK TO A POINT WHERE HE FELT HE SHOULD BE S TOPPING. THE FREE ROLLING CUT OF 44 CARS TRAVELLED 1266' BEFORE IMPACTING THE STANDING CUT OF CARS W ITH LOCOMOTIVES ATTACHED, DERAILING THE R&L-1 WHEELS OF THE 25TH HEAD CAR CAEX 581834, AND COMING TO REST 97' FURTHER SOUTH.",False,True,False,False,False,0.0
249,19,1,NS,1,IRONDALE,JEFFERSON,"LOCOMOTIVE SHOP EMPLOYEE MOVING SOUTH WITH ONE LOCOMOTIVE ON TRACK 2 HOUSE, DERAILED NS 2398 (AXLES 1 AND 2) OVER THE 2 HOUSE DERAIL. NO TRANSPORTATION EMPLOYEES INVOLVED.",False,True,False,False,False,0.0
250,19,1,NS,17,CHICAGO,COOK,BC03 WHILE YARDING TRAIN 23Z.09 DERAILED HIS HEAD TWO CARS TTAX 753110 AND TTAX 554281 JUST WEST OF THE NEW CONNECTION CROSS OVER AT 47TH STREET YARD WHEN A PIECE OF RAIL BROKE UNDER MOVEMENT.,False,True,False,False,False,0.0
251,19,3,NS,17,CHICAGO,COOK,"22KB317 DERAILMENT AT 55 YARD UNKNOWN INTERMODAL OPERATOR STRUCK GTW 676006 AND PUSHED THE NORTH SID E OF THE CAR IN THE GAUGE FORCING THE RAIL TO SPREAD. ONCE THE 22KB317 TIED ONTO TRACK 40 AND BEGAN TO PULL EAST DERAILING THE DTTX 723830, DTTX 7894405, DTTX 656583, DTTX 656728.",True,True,False,False,False,0.0
252,19,2,NS,17,CHICAGO,COOK,BS31 YARDING ROAD TRAIN 233L411 DERAILED THE 10TH-12TH HEAD CARS WHEN PULLING THROUGH TRACK LY11 AS THE WHEELS TRAVERSED OVER A MISMATCHED JOINT IN THE BODY OF TRACK LY11. NO INJURIS.,False,True,False,False,False,0.0
253,19,3,UP,17,HIGHLAND PARK,LAKE,THE CNAWK9-28 DERAILED RAILCAR MILX31195 ON THE B-END DUE TO A HOT JOURNAL.,False,True,False,False,False,0.0
254,19,3,NS,18,LOGANSPORT,CASS,D96D113 DERAILMENT - CREW SHOVING WEST DERAILED 5 CARS.,False,True,False,False,False,0.0
255,19,8,NS,18,NEW HAVEN,ALLEN,"NS TRAIN 12QL325 DERAILED NBTX 780725, SOU 531423, GRW 7059, GRW 7476 WHILE SHOVING WESTBOUND.",False,True,False,False,False,0.0
256,19,2,NS,18,ELKHART,ELKHART,BE14 RCO PULLED WEST OUT OF CT07 RUNNING THRU THE RUNNER/1 LEAD SWITCH AND UPON SHOVING BACK TOWARDS CT07 DERAILED 4 CARS. BE14 FOREMAN WAS IN THE TRACK AND WAS NOT IN A POSITION TO SEE HIS HEAD END. WEST END SWITCH TENDER GAVE THE ROUTE TO BE14 WITHHOUT ENSURING THE HAND THROW SWITCH WAS LINED CORR ECTLY FOR THE INTENDED MOVE.,False,True,False,False,False,0.0
257,19,5,CSX,18,CRAWFORDSVILLE,MONTGOMERY,EMPLOYEE WAS CONDUCTING A HI-RAILING INSPECTION AND FAILED TO STOP WITHIN SHORT OF THE ROAD CROSSING AT NUCOR ROAD. THIS RESULTED IN THE CSX VEHICLE STRIKING A OSP VEHICLE IN THE CROSSING.. AGE UNKNO WN. PROTECTION ALSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS ( STOP LINES) MOW HI-RAIL VE HICLE DAMAGE $15K.,False,False,True,False,True,15000.0
258,19,2,CSX,18,INDIANAPOLIS,MARION,UTLX 664825 STALLED IN GROUP 1 BEFORE THE GROUP RETARDER DUE TO A DEFECTIVE SLACK ADJUSTER AND STOPP ED IN THE FOUL OF GROUP 2. THE UTLX 668885 SIDESWIPED IT GOING INTO GROUP 2.,False,False,True,False,False,0.0
259,19,11,UP,20,KANSAS CITY,WYANDOTTE,"THE YKS11R-23 KICKED A CUT OF FOUR EMPTIES INTO TRACK 12. CREW THEN KICKED TWO CARS INTO A DIFFEREN T TRACK, THEN CAME BACK TO TRACK 12, KICKING 7 MORE LOADS. WHEN THE LOADS IMPACTED THE CUT OF FOUR EMPTIES THAT WERE ALREADY IN TRACK 12, THE IMPACT RESULTED IN THE LEAD AXLE OF THE TTZX861038 AND TH E REAR AXLE OF UP466325, TO DERAIL. THE LEAD CAR, TTZX861038, IN CUT OF FOUR EMPTIES CROSSED DRAWBA RS WITH FIRST CAR IN TRACK, NOKL600111. UPON INVESTIGATION, THE PINS ON ALL OF THE CUTS WERE MADE O N THE KICKING PAD AT SPEED OF APPROXIMATELY 5 MPH.",False,True,False,False,False,0.0
260,19,12,CSX,26,DEARBORN,WAYNE,"Y29028, HEADING EAST AS LIGHT LOCOMOTIVE IN TRACK W02 AT ROUGEMERE YARD, STRUCK CAR IN TRACK R01 THA T WAS LEFT FOULING TRACK W02.",True,False,False,False,False,0.0
261,19,9,BNSF,27,FALCON HEIGHTS,RAMSEY,"Z-CHCSSE9-19 DERAILED 9 RAILCARS IN YARD TRACK 7012. AFTER PULLING THROUGH AN IMPROPERLY LINED SWITC H, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTION. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED I N TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIAL WERE RELEASED.",False,True,False,False,False,0.0
262,19,9,CP,27,NORTHFIELD,RICE,"H38-21 DERAILED AT NORTHFIELD YARD #3 SWITCH SHOVING SOUTH WITH THREE ENGINES, THE REAR 3 TRUCKS ON THE LEAD ENGINE PICKED THE SWITCH AND DERAILED. PROGRESSIVE RAIL IS REPORTING $300 IN TRACK DAMAGE.",False,True,False,False,True,300.0
263,19,9,BNSF,27,FRIDLEY,ANOKA,H-NSINTW1-12 DERAILED 3 RAILCAR WHILE PULLING IN YARD TRACK 3011. NO HAZARDOUS MATERIALS WERE RELEAS ED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
264,19,8,UP,29,STRASBURG,CASS,"AASNP-06 EXPERIENCED A UDE. DURING INSPECTION CREW FOUND ETTX701516 AND BNSF302857 DERAILED. TRAIN W AS CONFIGURED 3X1X0 9,920 FT 9944 TONS. DERAILMENT WAS DUE TO POOR MAKE UP. NO RESTRICTIONS WERE IN PLACE OR VIOLATED. NEW TRAIN MAKE UP RESTRICTIONS HAVE BEEN SET AS A RESULT.",False,True,False,False,False,0.0
265,19,8,UP,29,KANSAS CITY,JACKSON,NORTHBOUND MNLNP-04 DERAILED NEAR MP.289.17 ON THE COFFEYVILLE SUB. TRAIN WAS TRAVELING AT A SPEED O F 25 MPH WITHIN THE LIMITS OF FORM A 147671 (289.0-289.5 25 MPH MT). NO AUTOMATIC BRAKES WERE APPLIE D. CAR ACFX98207 DERAILED THE FIRST AXLE DUE TO DEFECTIVE SNUBBING AND WAS DRAGGED APPROXIMATELY 1/4 MILE BEFORE THE TRAIN WENT INTO EMERGENCY.,False,True,False,False,False,0.0
266,19,8,UP,29,JAMESPORT,LIVINGSTON,MCBKC-13 HAD THE DYNAMIC BRAKING GRIDS ON LEAD UNIT UP8511 CAUGHT ON FIRE. NO DERAILMENT OR TRACK DA MAGE.,False,False,True,False,False,0.0
267,19,8,UP,29,INDEPENDENCE,JACKSON,"AASFX-18, LEAD UNIT UP2658, DERAILED 10 CARS, DUE TO TRAIN MAKE UP, RESULTING IN EXCESSIVE BUFF FORC ES. AT THE TIME OF THE INCIDENT, THERE WERE NO TRAIN MAKE-UP RESTRICTIONS VIOLATED. AS A RESULT OF T HIS INCIDENT, NEW RESTRICTIONS WERE PUT INTO PLACE AND THE CREW WAS NOT HELD RESPONSIBLE. ROCK CREEK JCT CONTROL POINT IS DISPATCHED BY KCT, OWNED BY UP, TRACK MAINTAINED BY UP, SIGNAL MAINTENANCE PER FORMED BY KCT FOR BNSF. *KCT MAINTAINS SIGNAL. KCT SIGNAL COST = $97,587*",False,True,False,False,False,97587.0
268,19,9,MDS,28,MERIDIAN,LAUDERDALE,AN UATTENDED CONSIST WAS SITTING ON TRACK AWAITING NEXT DAY'S MOVEMENT. NEIGHBORING RAILROAD LOST C ONTROL OF A CAR. THE RUNAWAY CAR ENTERED THE YARD AND STRUCK THE TRAILING ENGINE OF THE CONSIST. N ONE OF OUR PERSONNEL WERE PRESENT AT THE TIME. THE TRAILING ENGINE WAS HEAVILY DAMAGED. NO OTHER D AMAGE IS REPORTED.,True,False,False,False,True,0.0
269,19,1,CP,38,KENMARE,WARD,"392-021 (GRAIN TRAIN) EXPERIENCED AN UNDESIRED EMERGENCY BRAKE APPLICATION AT APPROXIMATELY MP. 516. 0 ON PORTAL SUB. INSPECTION OF TRAIN IDENTIFIED THAT LINE 58 THRU 73 DERAILED. PREVIOUSLY CREW STOPP ED AT MP. 520.0 (WEST KENMARE) & RECEIVED AUTHORITY TO PASS SIGNAL DISPLAYING STOP DUE TO A TRACK LI GHT THAT CAME IN BEHIND THE 293-28. AFTER RECEIVING AUTHORITY FROM DISPATCHER, CREW BRIEFED ON THE R EQUIREMENTS OF RESTRICTED SPEED AS WELL AS DISTANCE & LOCATION THE RESTRICTION PERTAINED TO. CREW DE PARTED AT RESTRICTED SPEED FROM MP 520.0 TO MP 516.0 WHERE THEY PASSED A PROCEED INDICATION. THEY TR AVELED APPROXIMATELY 3000 FEET PAST THE SIGNAL AT MP 516.0 BEFORE EXPERIENCING AN UNDESIRED EMERGENC Y BRAKE APPLICATION. CREW STATED THEY DID NOT SEE OR FEEL ANYTHING ABNORMAL WHEN THE TRAIN WENT INTO EMERGENCY, THERE WAS NO SEVERE SLACK ACTION EVENT. A BROKEN RAIL WAS IDENTIFIED AS THE CAUSE - POD APPROXIMATELY 130 FEET WEST OF THE BRIDGE AT MP 516.6 RESULTING IN DERAILMENT.",False,True,False,False,False,0.0
270,19,6,BNSF,38,MANDAN,MORTON,"RCO Y-YMAN3032-06 DERAILED 2 RAILCARS IN YARD TRACK 2139. AFTER PULLING THROUGH AN IMPROPERLY LINED SWITCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED S PEED. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
271,19,6,UP,31,NORTH PLATTE,LINCOLN,"YNP06R-09, WHILE TRIMMING OUT THE MNPCH, FOREMAN WAS STANDING BY THE SWITCH WHEN HE PULLED OUT BOWL 12 TO DOUBLE TO 13 AND DERAILED TTZX864370 AND TTZX866029 DUE TO BY-PASSED DRAWBARS.",False,True,False,False,False,0.0
272,19,6,NCRC,31,MADISON,MADISON,"TRAIN CREW WAS SHOVING NORTH INTO TRACK 713 & MADE JOINT. WHEN CREW WENT TO STRETCH THE JOINT, ENGIN EER COULDN'T MOVE TRAIN. INSPECTION SHOWED 6 CARS WERE DERAILED DUE TO WIDE GAUGE OF TRACKS.",False,True,False,False,False,0.0
273,19,6,UP,31,NORTH PLATTE,LINCOLN,EMPLOYEE WAS WORKING AS THE FOREMAN ON THE YNP02R-16 AND IN CONTROL OF THE PITCH WHILE SHOVING A CUT EAST OUT OF 202 TO THE HILL. MEANWHILE THE FOREMAN OF THE YNP01R-16 WAS RUNNING LIGHT POWER WESTWA RD THROUGH 203. FOREMAN ON THE YNP02R-16 DID NOT CONTROL THE MOVEMENT OF HIS TRAIN AND IMPACTED THE FIRST CAR (CHTT721880) WITH THE LAST LOCOMOTIVE (UP1739) OF THE LIGHT ENGINE CONSIST THAT WAS CLEAR ING UP THE LEAD.,False,False,True,False,False,0.0
274,19,1,UP,35,LA MESA,DONA ANA,"SWITCHING CONTRACTOR ITS, HAD A HOLD OF THE ISALB-19 AND WAS SHOVING EAST INTO TRACK 353. THE SWITC H WAS LINED FOR 352. THE SWITCHMAN ON THE GROUND GAVE THE ENGINEER INSTRUCTIONS TO SHOVE BACK 40 CA RS. THE SWITCHMAN NEVER LINED THE 352 SWITCH FOR MOVEMENT INTO 353, THEREFORE THE TRAIN WENT INTO 3 52 TRACK AT 16 MPH AND COLLIDED WITH A CUT OF CARS. AT THE TIME OF THE INCIDENT THE RAIL EQUIPMENT WAS MOVING ABOVE THE MAXIMUM FOR THE TRACK CLASS REPORTED",False,False,True,False,False,0.0
275,19,9,CSX,36,SELKIRK,ALBANY,Y39127 SHOVED TRACK 035 EAST INTO THE SIDE OF Y39627 PULLING OUT OF THE EAST END OF TRACK 036 IN THE BOWL.,False,False,True,False,False,0.0
276,19,6,NS,39,CAMPBELL,MAHONING,"C43C702 SHOVING SOUTH WITH 2 UNITS, 28 LOADS, 4 EMPTIES, AND 3832 TONS ON NORTH DIVISION LEAD DERAIL ED 7 CARS (NS 202053, RGCX 1188, CRDX 20606, RGCX 1222, CRDX 20050, CEFX 53739, & UTLX 71467).",False,True,False,False,False,0.0
277,19,8,NS,39,COLUMBUS,FRANKLIN,CAR DAMAGED WHEN SWITCHED FREE ROLLING INTO TRACK. CAR STRUCTURE FOUND TO BE WEAKENED DUE TO COMMODI TY (SALT) HAULED IN CAR. DAMAGE OCCURRED DURING NORMAL SWITCHING OPERATIONS.,False,False,True,False,True,0.0
278,19,2,NS,39,LUCASVILLE,SCIOTO,TRAIN 194LB28 WAS NOTIFIED THEY HAD A WHEEL DERAILED AND KICKING UP BALLAST. CREW WAS NOTIFIED BY TH E DISPATCHER TO BRING THEIR TRAIN TO A SAFE STOP. ENGINEER BEGAN TO SET HIS AIR TO BRING TRAIN TO A STOP AT MILEPOST N618.2 AND WENT INTO EMERGENCY.. CREW INSPECTED THEIR TRAIN AND FOUND 16 CARS DERAI LED BEGINNING WITH FMSX 3261 (102ND THROUGH 117TH H/C).,False,True,False,False,False,0.0
279,19,2,NS,39,MIDDLETOWN,BUTLER,L04LC04 WAS PULLING EAST WHEN DERAILMENT OCCURED.,False,True,False,False,False,0.0
280,19,2,NS,39,BELLEVUE,ERIE,"LB24 WAS HUMPING TRACK AA11 WHEN DPRX 258519 STALLED IN THE FOUL AT THE EAST END OF CT34. THE NEXT C AR IN THE HUMP, SHPX 209425, WAS GOING TO TRACK CT33 WHEN IT CORNED THE FIRST CAR CAUSING DAMAGE TO BOTH.",False,False,True,False,True,0.0
281,19,2,NS,39,STRYKER,WILLIAMS,NS TRAIN 206B312 STRUCK A HWY-USER AT A HWY-GRADE CROSSING.,True,False,False,False,False,0.0
282,19,4,UP,41,LA GRANDE,UNION,"MRVNPB-31, TREAD BUILDUP ON THE WCRC7259 PRODUCED ENOUGH WHEEL HOP TO CAUSE THE EMPTY CAR TO DERAIL.",False,True,False,False,False,0.0
283,19,4,UP,41,PORTLAND,MULTNOMAH,YPD10-12 RAN THROUGH THE 40 CROSSOVER SWITCH WHILE MOVING EAST FOLLOWED BY A REVERSE MOVE CAUSING A 3 CAR DERAILMENT.,False,True,False,False,False,0.0
284,19,2,BNSF,41,MADRAS,JEFFERSON,MAINTENANCE OF WAY HY-RAIL STRUCK A BOULDER THAT HAD FELL ONTO THE TRACKS CAUSING DAMAGE TO THE VEHI CLE AND FOR THE HY-RAIL TO DERAIL ON SINGLE MAIN TRACK. NO HAZARDOUS MATERIALS WERE RELEASED.,True,True,False,False,True,0.0
285,19,1,NS,45,COLUMBIA,RICHLAND,"24QP920 SHOVING EAST WITH 0X28, 2016 TONS INTO TRACK EY01 STRUCK STANDING EQUIPMENT",True,False,False,False,False,0.0
286,19,10,CSX,47,NASHVILLE,DAVIDSON,SKATE FAILURE ON B31 ALLOWED TRACK TO ROLL OUT AND STRIKE THE Y29310 WHO WAS PULLING OUT OF B25.,False,False,True,False,False,0.0
287,19,12,XTGS,48,ANAHUAC,CHAMBERS,BALLAST WAS FOULING THE TRACK DURING LOADING AND UNLOADING OPERATIONS,False,False,True,False,False,0.0
288,19,1,UP,48,BEAUMONT,JEFFERSON,"THE YBM05R-07 HAD A HOLD OF 65 CARS IN HUMP OPERATION, THEY HUMPED 8 CARS ALL GOING TO BOWL TRACK #9 , WHEN THEY HUMPED CARS #9 (CAR A) & #10 (CAR B) AS A DOUBLE THEY BOTH BEGAN TO ROLL ACROSS THE HUMP . AS THE CARS BEGAN DOWN THE HILL THEY BOTH BEGAN TO STALL, THEN STOP JUST PAST THE KING SWITCH. W HILE THE CARS WERE SLOWING TO A STOP, OPERATOR B GAVE A STOP COMMAND BUT IT WAS TOO LATE AS OPERATOR A HAD PULLED THE PIN ON CAR#11 (CAR C), RELEASING IT TO ROLL OVER THE HUMP TO TRACK #14 WHEN CAR C WAS NEARING THE KING SWITCH, THE SWITCH LINED TO GO TO THE HIGH SIDE OF BOWL WITHOUT CARS A & B CLEA RING. THIS CAUSED THE A END OF CAR C TO IMPACT WITH THE A END OF CAR B, BYPASSING THE DRAWBARS, WIT HOUT DERAILING.",False,True,False,False,False,0.0
289,19,10,TXOR,48,SWEETWATER,NOLAN,TXOR DERAILED 15 LOADED CARS OUT OF 25 LOADED CARS ON BNSF TRACK 5199. CAUSE IS STILL BEING INVESTI GATED.,False,True,False,False,False,0.0
290,19,10,UP,48,EL PASO,EL PASO,"MHNTU-24 TRAVELING WEST DERAILED THE TRAILING WHEELS OF CAR AZER77034 AT MP 1297.7. SHORT CAR 48 EM PTY AZER77034 AHEAD OF LONG 94 FT LOADED AUTO CAR TO INCLUDE THE NEXT 10 CAR LOADS AND MORE THAN 9,0 00 TRAILING TONS EXPERIENCED A WHEEL LIFT DUE TO TRAIN MAKEUP AND TRAILING WHEELS OF AZER77034 DERAI LING. NOT A RULE VIOLATION. NO DISCIPLINE WAS ASSESSED.",False,True,False,False,False,0.0
291,19,8,UP,48,EL PASO,EL PASO,"MTUEP-11 WAS SHOVING LIGHT POWER WEST IN 835 TRACK AT ALFALFA TO PUT IN 836 TRACK. CONDUCTOR INSTRUC TED ENGINEER TO SHOVE BACK TO CLEAR 836 SWITCH. DURING THIS MOVE, THE CONDUCTOR DID NOT NOTICE LEAD SWITCH WAS LINED AGAINST THE MOVE CAUSING ENGINES TO RUN THROUGH THE SWITCH. THE SECOND AND THIRD UN ITS DERAILED WHILE MAKING A REVERSE MOVE THROUGH THE RUN THROUGH SWITCH.",False,True,False,False,False,0.0
292,19,8,UP,48,DALLAS,DALLAS,"AMQARR-18, LEAD UNIT UP8019, DERAILED 1 CAR ON DALLAS MAIN 2 WHILE TRAVELING WEST. CAUSE WAS A WORN SWITCH POINT.",False,True,False,False,False,0.0
293,19,8,UP,48,HILLSBORO,HILL,THE MFWSA-19 WAS TRAVELING SOUTH ON THE FORTH WORTH SUB AND AT 1520 THE TRAIN WENT INTO EMERGENCY. U PON INSPECTION THE TRAIN DERAILED 32 CARS. THERE WERE NO INJURIES AND NO HAZMAT CARS INVOLVED. THE T RAIN WAS 139 CARS (129 LOADS AND 19 EMPTIES). IT ALSO HAD 22 CUSHION DRAWBARS. THE CREW HANDLED THE TRAIN WITH NO EXCEPTIONS AND THE TRAIN MAKE WAS ALSO PER UP STANDARDS.,False,True,False,False,False,0.0
294,19,8,UP,48,PECOS,REEVES,"LBN44-25, LEAD UNIT UP8468, TRAVELING EAST, STRUCK THE REAR END OF A SEMI TRUCK AT MP 653.59 ON THE TOYAH SUB.",True,False,False,False,False,0.0
295,19,10,BNSF,48,SILSBEE,HARDIN,"Y-SSB1321-30 DERAILED 30 RAILCARS IN YARD TRACK 101. AFTER SHOVING THROUGH AN IMPROPERLY LINED SWITC H, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO CONTROL SHOVE MOVE IN TURN RU NNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
296,19,10,BNSF,48,ORANGE,ORANGE,SEMI TRUCK AND TRAILER WERE STOPPED ON CROSSING AND WERE UNABLE TO MOVE IN TIME DUE TO TRAFFIC AND W AS STRUCK BY H-LALSVL-1-13A TRAIN ON THE CROSSING. NO HAZMAT RELEASED.,True,False,False,False,False,0.0
297,19,10,BNSF,48,FARWELL,PARMER,TRUCK DRIVER FAILED TO YIELD AT THE CROSSING AND WAS STRUCK BY U-AMOSNJ-1-16A TRAIN. NO HAZMAT RELEA SED.,True,False,False,False,False,0.0
298,19,8,UP,48,TAFT,SAN PATRICIO,"THE AWFBVR-29, WITH LEAD LOCOMOTIVE UP4715, STRUCK A VEHICLE THAT HAD STALLED ON TRACKS AT THE CROSS ING. DRIVER HAD MINOR INJURIES TO FOREHEAD.",True,False,False,False,False,0.0
299,19,7,UP,48,HEWITT,MCLENNAN,MSAFW-09 CREW WAS TRAVELING NORTH ON THE WACO SUB WHEN THEY WENT INTO UDE. THE CREW WAS TRAVELING AT 20 MPH WHEN DERAILMENT OCCURRED. IT WAS DETERMINED THAT THE ENGINEER HAD TOO MANY DYNAMIC BRAKES CU T IN ON THE LEAD LOCOMOTIVE OF CONSIST. THE EDBA ON THE CONSIST WAS 48.5 COMPARED TO A MAX ALLOWABLE OF 28. NO TRACK DAMAGE.,False,True,False,False,False,0.0
300,19,7,UP,48,FORT WORTH,TARRANT,THE SIGNAL DEPARTMENT HAD WORKED ON THE 45/48 SWITCH ON THE WEST END OF THE BOWL. THEY TESTED IT AND RETURNED TO SERVICE. THE FIRST 2 CARS OF THE HUMP FROM THE YFW34R-12 WERE DESTINED TO 46 BOWL. WHEN THE CARS WENT THRU THE 45/48 SWITCH THE LEAD SET OF TRUCKS WENT TOWARD TRACK 45 AND THE SECOND SET OF TRUCKS SPLIT THE SWITCH AND WENT TOWARD TRACK 48 DERAILING THE SECOND SET OF TRUCKS AND ALL THE T RUCKS ON THE SECOND CAR. TRACK 48 HAD ROLLED RAIL AND ABOUT 150 FOOT OF BROKEN RAIL. THERE WERE NO I NJURIES AND NO HAZMAT RELEASE.,False,True,False,False,False,0.0
301,19,5,RLAX,48,BAYTOWN,CHAMBERS,CONDUCTOR RELEASED HAND BRAKE ON TRACK 17 SOUTH AND BEGAN SWITCHING CARS FROM TRACK 17 TO THE YARD L EAD. AS CONDUCTOR WAS SHOVING CARS ON YARD LEAD THE REMAINING CARS IN TRACK 17 ROLLED OUT AND INTO T HE SIDE OF THE CARS THAT WERE BEING SHOVED CAUSING ONE CAR TO DERAIL.,False,True,False,False,False,0.0
302,19,7,BNSF,48,FORT WORTH,TARRANT,"Y-NYF1052-02 DERAILED 1 RAILCAR IN YARD TRACK 9112. AFTER PULLING THROUGH AND IMPROPERLY LINED SWITC H, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS, CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
303,19,11,BNSF,48,CLEVELAND,LIBERTY,H-TPLLAL1-07 DERAILED 9 RAILCARS WHILE PULLING OUT OF SIDING TRACK 1081 DUE TO TRACK WIDE GAGE. NO H AZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
304,19,11,BNSF,48,FORT WORTH,TARRANT,"RCO Y-NYF3082-27 DERAILED 1 LOCOMOTIVE IN YARD TRACK 9109. AFTER PULLING THROUGH AN IMPROPERLY LINED SWITCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
305,19,1,UP,48,HOUSTON,HARRIS,"THE MPTHO-05 WAS TRAVELLING ON THE HOUSTON EAST BELT AT MP 8. AFTER STOPPING AT CPEB080 NEAR THE HO USTON BAYOU BRIDGE, THE CREW GOT A SIGNAL TO PROCEED NORTH AND AS THEY STARTED MOVING THE TRAIN WENT INTO EMERGENCY AT CBEB076. THE CONDUCTOR PROCEEDED TO WALK THE TRAIN AND NOTICED A SET OF WHEELS W AS MISSING FROM CAR CCBX58281 AND HAD DERAILED.",False,True,False,False,False,0.0
306,19,2,DGNO,48,DALLAS,DALLAS,SHOVING CARS FROM SOUTH END OF CADIZ WHEN 24TH CAR DRIPPED INSIDE GAGE PRIOR TO SWITCH. RESULTING IN 4 CARS RIDING UP SWITCH POINT & GOING DOWN TK400. LATERAL FORCES BETWEEN TRACKS & CARS PULLED 4 CAR S OFF RAIL & 5TH CAR HAVING ONE SET OF TRUCKS SITTING ON WEB OF ROLLED RAIL. TRAILING MOTOR OF CONSI ST ALSO HAD 2 AXLES DERAILED DUE TO WIDE GAGE.,False,True,False,False,False,0.0
307,19,12,UP,48,GALENA PARK,HARRIS,YGP70-13 WAS DRAGGING OUT OF TRACK 402 AND DERAILED TWO CARS DUE TO WIDE GAUGE CAUSED BY INSUFFICIEN T FASTENERS.,False,True,False,False,False,0.0
308,19,4,UP,49,HELPER,CARBON,"CSKVY-20, LEAD LOCOMOTIVE UP6268, DERAILED 5 CARS. CAUSE OF DERAILMENT WAS BROKEN RAIL. INDUSTRY M AINTAINS TRACK",False,True,False,False,False,0.0
309,19,5,UFRC,49,OREM,UTAH,THE GRADE CROSSING AT 400 S IN OREM WAS ACTIVATED FOR A SB TRAIN. AN EB PASSENGER VEHICLE DID NOT S TOP AT THE PAVEMENT MARKING BEFORE THE HORIZONTAL CROSSING WARNING ARM. THE PASSENGER VEHICLE CAME T O A STOP ON THE RAIL. THE SB TRAIN MADE CONTACT SECONDS AFTER THE PASSENGER VEHICLE CAME TO A STOP C AUSING THE DEATH OF THE SINGLE OCCUPANT IN THE AUTOMOBILE. THERE WERE NO INJURIES ON THE TRAIN.,False,False,True,False,False,0.0
310,19,4,UP,49,OGDEN,WEBER,"CARMAN INSPECTING TRAIN FOUND 3 CARS THAT HAD DERAILED DURING SHOVING OPERATIONS, MWCX500502, MWCX50 0492, AND UTLX631107.",False,True,False,False,False,0.0
311,19,4,UP,49,OGDEN,WEBER,THE YOG31R-14 WAS PULLING A CUT WHEN A PAIR OF TRUCKS CAME OUT FROM UNDER A CAR IN THEIR SWITCH CUT. IT WAS CAUSED BY MECHANICAL FAILURE OF THE CENTER PIN. 1 DRUG POSITIVE - NOT DETERMINED TO BE A C AUSAL FACTOR.,False,False,True,False,False,0.0
312,19,12,CWRY,51,SUFFOLK,SUFFOLK,"CWRY1 CREW SWITCHING SOLENIS CHEMICAL PLANT WHILE MAKING A SHOVING MOVEMENT INSIDE SOLENIS TRACK 1, TWO CARS DERAILED AT THE END OF THE SPILL PAD DUE TO WIDE GUAGE. SUPPLEMENTAL CODE Z: INDUSTRY - OWN ED TRACK. TRACK DAMAGE = $12,000 (SOLENIS CHEMICAL) INDUSTRY-OWNED. UPDATED 2/3/2020 TO CORRECT INDU STRY.",False,True,False,False,True,12000.0
313,19,3,UP,48,HOUSTON,HARRIS,CAR WAS FOUND WITHOUT A MATE IN THE REPAIR TRACK BY THE CAR DEPARTMENT WITH DAMAGE FROM HUMPING. NO DERAILMENT OR TRACK DAMAGE.,False,False,True,False,True,0.0
314,19,3,UP,48,LA PORTE,HARRIS,"A CUT OF TWO CARS WAS HUMPED INTO BOWL 8. THE CUT OF CARS ROLLED INTO BOWL 8 AT A SLOW RATE OF SPEE D, CAUSING A SECOND CUT OF TWO CARS HUMPED TO CATCH UP TO IT AND CORNERING EACH OTHER. TWO TANK CAR S DAMAGED WITH NO DERAILMENT. CORNERING PROTECTION ON THE SIGNAL SOFTWARE IS NOT ADEQUATE TO PREVENT THE INCIDENT.",False,False,True,False,True,0.0
315,19,1,TXR,48,BROWNWOOD,BROWN,"TXR CREW WAS DRAGGING INTO TRACK 113 FROM THE WEST END WHEN THEY DERAILED FIVE CARS DUE TO WIDE GAUG E RAIL. NO HAZARDOUS MATERIALS WERE RELEASED. BNSF IS REPORTING OR REPORTED TRACK DAMAGES OF $8,9 46",False,True,False,False,False,89.0
316,19,12,UP,48,BEAUMONT,JEFFERSON,"MBTEW-11 WAS BEGINNING THEIR DOUBLEOVER ON THE WEST END OF BEAUMONT YARD, FROM TRACK 201 TO TRACK 20 2. THE CONDUCTOR STAYED AT THE 201 SWITCH AND TOLD THE ENGINEER TO PULL FORWARD 100 FEET. THE ENGI NEER STATED THAT HE BEGAN TO PULL, NOTICED HE HAD THE SIGNAL AT CPLF282, AND THEN CHECKED THE POWER DERAIL SWITCH. WHEN THE CREW CLEARED THE TRACK 201 SWITCH, THE CONDUCTOR LINED THE SWITCH, AND GAVE THE ENGINEER THE COMMAND TO SHOVE BACK. THE ENGINEER SHOVED BACK 5 CARS WHEN THE TRAIN WENT INTO E MERGENCY AND STOPPED, FOUND CARS TILX135689 AND NDYX113623 DERAILED. THE HUMP POWER WAS PASSING AND SIDESWIPED THE NDYX113623, THAT WAS FOULING THE HUMP LEAD, DAMAGING UPY358, UPY458, AND UP1730. UP ON ARRIVAL ON SCENE IT WAS NOTICED THAT THE SWITCH HANDLE WAS STILL IN THE POSITION THAT WOULD BE LI NED FOR TRACK 102, AND AFTER LOOKING AT THE OUT FACING VIDEO CAMERA IT WAS CLEAR THAT THE ENGINEER D ID NOT STOP AND LINE THE SWITCH FOR HIS MOVEMENT.",False,True,False,False,False,0.0
317,19,11,UP,48,WEIMAR,COLORADO,"DPU UNIT UP7411 CAUGHT ON FIRE ON TRAIN MWCLI-29, LEAD UNIT UP8843.",False,False,True,False,False,0.0
318,19,1,GVSR,48,GALVESTON,GALVESTON,"WHILE PULLING CUT OF WINDMILL CARS OUT TO SWITCH WITH EMPTIES, CREW SIDESWIPED A CUT OF CARS ON THE ADJACENT TRACK THAT WAS INSIDE THE CLEARANCE POINT. NO CARS WILL BE ALLOWED ON ADJACENT TRACKS GOING FORWARD.",False,False,True,False,False,0.0
319,19,1,BNSF,48,AMARILLO,POTTER,RCO Y-AMA2012-31 DERAILED 4 RAILCARS WHILE PULLING INTO YARD TRACK 125 DUE TO SWITCH NOR LATCHED OR LOCKED. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
320,19,1,BNSF,48,AMARILLO,RANDALL,Y-AMA9031-18 DERAILED 5 RAILCARS WHILE SHOVING YARD TRACK 1322 DUE TO FAILURE TO CONTROL SHOVE IN TU RN RUNNING OVER A DERAIL. NO HAZARDOUS MATERIAL WAS RELEASED.,False,True,False,False,False,0.0
321,19,5,DGNO,48,DALLAS,DALLAS,"CREW WAS SWITCHING CARRY TRANSIT'S WEST FACILITY ON WEST END OF MOCKINGBIRD YARD, THEY HAD AHOLD OF 12 TANK CARS, 10 OF WHICH WERE LOADS WITH HEAD AND REAR CARS BEING EMPTIES. AS CREW MADE A HEAD-END MOVE AROUND CORNER DOWN INTERCON LEAD TRACK, THEY FELT MOVEMENT IN TRAIN AND SHUT DOWN. INVESTIGATON REVEALED REAR MOTOR ALONG WITH HEAD FIVE CARS WERE DERAILED WITH ROLLED RAIL UNDERNEATH THEM.",False,True,False,False,False,0.0
322,19,4,UP,48,CLINT,EL PASO,"WEST BOUND AMT-105, LEAD UNIT AMTK78, COLLIDED WITH AN AUTOMOBILE RUNNING AROUND XING GATES IN THE L OWERED POSITION. AMTK EQUIPMENT DAMAGE =$15,033",False,False,True,False,True,15033.0
323,19,1,XTGS,48,ANAHUAC,CHAMBERS,RAIL ROLLED OVER AND LOST GAUGE UNDER WEIGHT OF LOADED CARS.,False,False,True,False,False,0.0
324,19,1,KCS,48,NEDERLAND,JEFFERSON,SHOVING OALBM-11 AT PHILLIPS 66 LEAD AND DERAILED 5 CARS (FLOATING BETWEEN RAIL AND TIES; BROKEN SWI TCH POINT PROTECTOR). MP 775.1 BEAUMONT SUBDIVION,False,True,False,False,False,0.0
325,19,2,BNSF,48,SAGINAW,TARRANT,Y-SAG1061-01 DERAILED 3 RAILCARS WHILE PULLING OUT OF YARD TRACK 8203. THE DERAILED RAILCARS IMPACT ED A LOCOMOTIVE STANDING IN ADJACENT TRACK. THE CAUSE WAS TRACK BROKEN RAIL. NO HAZARDOUS MATERIAL S WERE RELEASED.,False,True,False,False,False,0.0
326,19,2,UP,48,LONGVIEW,GREGG,"BNSF TRAIN, QLWBRJ-09 DERAILED THE LEADING WHEELS OF BNSF728580 AFTER TRAVELING ACROSS DISTURBED TRA CK AT MP 88.39 ON THE LITTLE ROCK SUB. THE CAUSE WAS DETERMINED TO BE SUBGRADE CONDITIONS/WATER POC KET UNDER TRACK, EXACERBATED BY RECENT RAINFALL CAUSING WARPED CONDITIONS. THE CAR RERAILED ITSELF AFTER TRAVELING APPROXIMATELY 580FT AND STRIKING THE CROSSING PLATES OF THE LAUNCH PAD AT MP 88.28. BNSF EQUIPMENT DAMAGE = $3,943",False,True,False,False,True,3943.0
327,19,2,BNSF,48,LONGVIEW,GREGG,H-SSBMEM1-08 DERAILED 1 RAILCAR WHILE TRAVERSING FOREIGN MAIN 2 TRACK DUE TO TRACK ROADBED DEFECTS. SUBGRADE CONDITIONS AND WATER POCKET UNDER TRACK. RESULTED IN SIGNIFICANT TRACK DAMAGE. NO HAZARD OUS MATERIALS WERE RELEASED.,False,True,False,False,True,0.0
328,19,2,BNSF,48,SANGER,DENTON,"TRACTOR & TRAILER HEADED WESTBOUND ACROSS CROSSING, HAD ITS TRAILER STANDS GET HUNG UP ON THE APPROA CH TO THE CROSSING, CAUSING BOTH TO BECOME HUNG UP ON THE RAIL AND WAS STRUCK BY TRAIN. RESULTING I N EQUIPMENT AND SIGNAL DAMAGES.
",True,False,False,False,False,0.0
329,19,2,BNSF,48,JOSHUA,JOHNSON,H-TULTPL1-25 DERAILED 1 RAILCAR WHILE TRAVERSING SINGLE MAIN TRACK DUE TO SUPERELEVATION EXCESSIVE. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
330,19,1,BNSF,48,DAYTON,LIBERTY,RCO Y-DYT2512-02 DERAILED 2 RAILCARS WHILE SHOVING YARD TRACK 635 DUE TO FAILURE TO CONTROL SHOVE MO VE. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
331,19,1,BNSF,48,BROWNWOOD,BROWN,FOREIGN TRAIN F-TXR1251-04 DERAILED 5 RAILCARS WHILE PULLING INTO YARD TRACK 113 DUE TO TRACK WIDE G AGE. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
332,19,1,BNSF,48,FORT WORTH,TARRANT,Y-NYF2021-05 EXPERIENCED DAMAGE TO 2 RAILCARS IN YARD TRACK 9113 DURING SWITCHING OPERATIONS DUE TO INADEQUATE PRECAUTIONS WHILE KICKING RAILCARS. NO HAZARDOUS MATERIALS WERE RELEASED.,False,False,True,False,True,0.0
333,19,6,WATX,48,HOUSTON,HARRIS,"WDRL GREENS PORT RAIL - HOUSTON, TEXAS - REPORTABLE DERAILMENT - NO INJURIES - NO ENVIRONMENTAL RELE ASE
DESCRIPTION AT APPROXIMATELY 00:35 ON 6/21/19, GPIP RAIL CREW 107 EXPERIENCED A TWO CAR DERAIL MENT WHILE PERFORMING SWITCHING OPERATIONS IN GREENS PORT INDUSTRIAL PARK. THE CREW WAS HOLDING TO 6 LOADED GASOLINE CARS PULLED FROM THE WEST YARD, AND WERE IN THE PROCESS OF DOUBLING OVER TO CARS ON TRACK 201. THE BRAKEMAN LINED THE TRAIN INTO 201 AND INITIATED THE SHOVE MOVEMENT BEFORE TRANSFERRI NG CONTROL OF THE TRAIN TO THE CREW LEADER. THE BRAKEMAN FAILED TO LINE THE CBRB SWITCH FOR HIS MOVE MENT. THE TRAIN STARTED DOWN CBRB TRACK INSTEAD OF 201 AND RAN OVER THE DERAIL PROTECTING THE CBR RA CK. THE LEAD CAR OF THE SHOVE DERAILED AND LAID OVER ON ITS SIDE. THE A END TRUCKS OF THE SECOND CAR DERAILED, BUT THE CAR REMAINED UPRIGHT. THERE WERE NO INJURIES FROM THE DERAILMENT. THERE HAS BEEN NO ENVIRONMENTAL RELEASE, AND CLEARING IS ONGOING.",False,True,False,False,False,0.0
334,19,6,BNSF,48,MORGAN,BOSQUE,G-CCDEAP9-13 DERAILED 1 RAILCAR WHILE TRAVERSING SINGLE MAIN TRACK DUE TO A BROKEN DRAFT SILL ON RAI LCAR. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
335,19,6,BNSF,48,DAYTON,LIBERTY,"Y-DYT2311-18 DERAILED 6 RAILCARS ON UPRR MAIN 1 TRACK. AFTER PULLING THROUGH AN IMPROPERLY LINED SWI TCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEE D. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
336,19,5,BNSF,48,HEREFORD,DEAF SMITH,TRUCK DRIVER WENT AROUND THE GATES AT A CROSSING AND WAS STRUCK BY WESTBOUND TRAIN.,True,False,False,False,False,0.0
337,19,10,UP,48,BEAUMONT,JEFFERSON,"BNSF TRAIN QDYBTJ-26, WHILE PULLING NORTH ON THE NORTHWEST CONNECTION ON THE SABINE INDUSTRIAL LEAD, DERAILED ONE RAILCAR. THE CAR WAS DRAGGED ONTO UPRR PROPERTY. BNSF EQUIPMENT DAMAGE = $80,176. B NST TRACK DAMAGE = $15,000",False,True,False,False,True,95176.0
338,19,10,BNSF,48,CORSICANA,NAVARRO,MAINTENANCE OF WAY TAMPER MACHINE STRUCK A MAINTENANCE OF WAY REGULATOR MACHINE WHILE TRAVERSING MAI N 1 TRACK DUE TO ON-TRACK EQUIPMENT FAILURE TO COMPLY WITH RULES. RESULTED IN DAMAGES TO BOTH MACHIN ES. NO HAZARDOUS MATERIALS WERE RELEASED.,True,False,False,False,False,0.0
339,19,10,UP,48,HOUSTON,HARRIS,"YEW71-04, WHILE SHOVING INTO BOWL 19, RAILCAR PPGX12236 DERAILED ON THE #20 SWITCH, DUE TO A GAPPED SWITCH POINT.",False,True,False,False,False,0.0
340,19,11,BNSF,48,AMARILLO,POTTER,"RCO Y-AMA3022-01 DERAILED 3 RAILCARS WHILE SHOVING YARD TRACK 117 DUE TO FAILURE TO STRETCH RAILCARS BEFORE SHOVING, THE CUT OF RAILCARS HAD PASSED COUPLERS. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
341,19,12,FWWR,48,FORT WORTH,TARRANT,"PROPERLY SECURED AND TESTED SINGLE CAR ROLLED AWAY ON THE MAIN LINE DUE TO A BAD ORDER SLACK ADJUSTE R.
CAR MADE IMPACT WITH CUSTOMER CAR ON CUSTOMER TRACK 605 ON THE FORT WORTH SUB DIVISION.
EQUIP MENT DAMAGE IS AN ESTIMATE BASED ON DEPRICIATED VALUE OF THE CAR THAT ROLLED AWAY, AMCX 108358. $41, 733
CUSTOMER CAR JBRX 318 ON CUSTOMER TRACK WAS IMPACTED AND DAMAGED - $7,969 DEPRECIATED VALUE
DISCUSSED NEED FOR ADDITIONAL 8150.54 REPORT WITH MICHAEL WISSMAN AND MICHELLE WILK 02/10/2020 - D UE TO THE COLLISION INVOLVING CUSTOMER EQUIPMENT ON A CUSTOMER TRACK, NO ADDITIONAL .54 FORM IS REQU IRED. TOTAL DAMAGE IS CAPTURED HERE IN THE NARRATIVE SECTION.",False,False,True,False,True,8010.0
342,19,10,UP,48,HOUSTON,HARRIS,YEW31R-20 WAS PULLING BACK TRACK 302 FROM THE NORTH SIDE. CONDUCTOR NOTICED DUST FLYING TOWARDS BOT TOM OF HILL WHEN HE THEN PLACED THE TRAIN IN STOP. THIS RESULTED IN 5 CARS DERAILING.,False,True,False,False,False,0.0
343,19,6,UP,48,MINEOLA,REEVES,"TRAVELING EASTBOUND THE ILXDI-13, LEAD UNIT UP8657, STRUCK A SEMI TRUCK AND TRAILER AT MP 656.94.",True,False,False,False,False,0.0
344,19,6,UP,48,STANTON,MARTIN,THE ILXNSX-13 STRUCK A VEHICLE THAT WAS STOPPED ON THE CROSSING AT MP 534.99.,True,False,False,False,False,0.0
345,19,7,BNSF,48,JUSTIN,DENTON,V-CDTALT1-27 DERAILED 1 LOCOMOTIVE WHILE OPERATING LIGHT POWER IN YARD TRACK 7303 DUE TO IMPROPER RA DIO COMMUNICATIONS BETWEEN THE CREW AND THE MACHINIST. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
346,19,9,CCPN,48,CORPUS CHRISTI,NUECES,"CREW WAS PULLING INTO YARD TO DELIVER TRACK 15, TRACK 12 WAS FOUND TO HAVE A VERY SMALL GAP IN IT. ENGINEER SAID HE FELT SOMETHING AWKWARD AND REALIZED HE WAS ON THE GROUND. THE OTHER 35 CARS WERE STILL ON THE LEAD HEADING DOWN TRACK 15. UP REPORTING $28,208 IN TRACK DAMAGE. CCPN AND UP HAVE COMM UNICATED BUT DISAGREE ON THE CAUSE OF THE ACCIDENT.",False,False,True,False,True,28208.0
347,19,8,CCPN,48,CORPUS CHRISTI,NUECES,"BN WAS SHOVING INTO THE YARD TO DELIVER SOME CARS, MADE A CUT, PULLED ABOUT 4 CARS AHEAD, DERAILED A T VULCAN CROSSING. BNSF HUMAN FACTOR. F54 REPORT CREATED UPON RECEIPT OF BNSF REPORT. BNSF EQUIPMENT DAMAGES = $181,899.00",False,True,False,False,False,181899.0
348,19,11,DGNO,48,GREENVILLE,HUNT,"S-711 JOB WAS HANDLING A 75-CAR LOADED ROCK TRAIN ON GARLAND SUB WHEN LINES 68-74 DERAILED DUE TO BR OKEN RAIL HEAD NEAR MP 713.8. OF SEVEN CARS DERAILED, THREE ARE ON THEIR SIDE, TWO ARE LEANING, AND TWO ARE UPRIGHT.",False,True,False,False,False,0.0
349,19,3,UP,48,ARLINGTON,TARRANT,"AARARR-15 DERAILED 3 CARS WHILE SETTING OUT AT THE GSWN. CREW HAD ORIGINALLY WENT INTO TRACK 2 AND PULLED AHEAD TO DOUBLE OVER 8 RAIL. WHILE SHOVING INTO 8 RAIL, CONDUCTOR SAW A LIGHT POLE FALL AND STOPPED MOVEMENT, HE WALKED TOWARDS THE HEAD END AND DISCOVERED THAT 3 CARS HAD DERAILED, KNOCKING O VER THE POLE, CAUSE WAS DUE TO EXCESSIVE LATERAL DRAWBAR FORCE ON CURVE.",False,True,False,False,False,0.0
350,19,3,UP,48,FORT WORTH,TARRANT,"THE YFW31-15 WAS SHOVING OFF THE MIDDLE LEAD TO TRACK 304 USING THE #7/8 CROSSOVER. THEY SIDESWIPED THE YFW36-15 LITE POWER SITTING ON THE #6 TRIM SWITCH. THIS WAS AFTER THE TC LINED THE SWITCH THAT SHOWED THE 36 IN THE CLEAR WHEN HE WAS ACTUALLY FOULING THE ADJACENT TRACK, WAITING FOR THE BLUE FLA G THAT WOULD ALLOW THEM TO BACK THE POWER ON THE OUTBOUND TRAIN. WITH THE YFW31 SHOVING, THE ENGINE ER ON THE 36 SAID `STOP` OVER THE RADIO, AND EXITED OUT THE BACK DOOR OF THE LOCOMOTIVE. NO INJURIE S AND NO DERAILMENT.",False,False,True,False,False,0.0
351,19,3,UP,48,BIG SPRING,HOWARD,"WHILE WORKING ON EAST LEAD, THE MMHFWX-21 DERAILED 5 CARS. NO RELEASES. NO INJURIES. CAUSE WAS DUE TO IRREGULAR TRACK ALIGNMENT.",False,True,False,False,False,0.0
352,19,3,UP,48,ROUND ROCK,WILLIAMSON,"WHILE MACHINE CAT1406 (CAT) WAS MOVING NORTH BEHIND BRP1203, CAT MACHINE 1406 CAME AROUND THE CURVE HEADING NORTH, CAT1406 OPERATOR WAS UNABLE TO STOP IN HALF THE DISTANCE TO BE SEEN CLEAR. CAT1406 C AME INTO CONTACT WITH BRP1203. A TOTAL OF FOUR EMPLOYEES WERE INVOLVED IN THIS INCIDENT. ALL FOUR EMPLOYEES REMOVED THEMSELVES FROM THE EQUIPMENT AND THREE OF THE EMPLOYEES REQUESTED TO BE TRANSPORT ED BY EMS TO LOCAL HOSPITAL.",False,False,True,False,False,0.0
353,19,3,UP,48,HOUSTON,HARRIS,"YEW31R-01 WAS HUMPING CARS INTO TRACK 53, WHEN A SINGLE CAR, UTLX670807 WAS CAUGHT IN THE MASTER RET ARDER, WHEN CAR GATX88631 IMPACTED THE UTLX CAR CAUSING THE WEST TRUCKS TO COME OUT OF THE BOWL AND ROLL UNDER THE CAR. NO DERAILMENT OCCURRED.",False,False,True,False,False,0.0
354,19,4,BNSF,48,JUSTIN,DENTON,RCO Y-ALT2012-15 DERAILED 3 RAILCARS WHILE PULLING OUT OF YARD TRACK 7133. NO MATERIALS WERE RELEASE D. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
355,19,3,CGIV,48,CHANNELVIEW,HARRIS,"PTRA TEAM WAS SPOTTING RAIL CARS IN CARGILL YARD. AFTER SPOTTING TWO STRING OF CARS ON TRACKS 5 & 6 RESPECTIVELY, CREW PROCEEDED TO SPOT RAIL CARS ON TRACK #3 TO JUST BEFORE CAR PROGRESSOR. THE PTRA C ONDUCTOR (RIDING THE LEAD CAR) NOTED THAT THE STRING OF CARS WAS NOT MOVING AS NORMAL. CONDUCTOR COM MUNICATED WITH THE ENGINEER TO STOP MOVEMENT. PTRA CONDUCTOR AND CARGILL EMPLOYEE WALKED BACK TO THE MAIN ENTRANCE POINT TO CARGILL YARD AND DISCOVERED THERE WERE 8 DERAILED CARS BETWEEN TRACKS 2 & 3 AND THRU THE CROSSING.",False,True,False,False,False,0.0
356,19,8,BNSF,48,CORPUS CHRISTI,NUECES,CREW ON H-GATLAR1-29A RAN THROUGH PORT LEAD SWITCH AND DERAILED WHEN THEY WENT THE OTHER DIRECTION. THE CONDUCTOR STOPPED MOVEMENT AND INCORRECTLY LINED THE SWITCH AGAINST THE TRAIN AND THEN SHOVED TH ROUGH IT.,False,True,False,False,False,0.0
357,19,8,BNSF,48,EL PASO,EL PASO,"UPON DEPARTING EL PASO, TRACK FLAGMAN HAD NOTICED THAT A SET OF TRUCKS/WHEELS WERE OFF OF THE RAIL. HE THEN PROCEEDED TO REQUEST THAT THE TRAIN COME TO A STOP. UPON INITIAL INSPECTION, IT APPEARED THA T THE CONTRIBUTING FACTOR WAS DUE TO THE BRAKE RIGGING DRAGGING.",False,False,True,False,False,0.0
358,19,8,UP,48,WOODLAWN,HARRISON,"MTXSH-09 WAS TRAVELING SOUTH ON THE LITTLE ROCK SUB WHEN THE TRAIN WENT INTO EMERGENCY NEAR MP 63. T HE CONDUCTOR WALKED BACK TOWARD THE REAR OF THE TRAIN AND FOUND 7 CARS DERAILED. THE DERAILMENT ACTU ALLY OCCURRED AT MP 59.5, NEAR THE SOUTH END OF WOODLANE SIDING BEFORE THEY WENT INTO EMERGENCY, CAU SING EXTENSIVE TRACK DAMAGE. CAUSE IS IRREGULAR CROSS LEVEL OF TRACK, COUPLED WITH TOO RAPID ADJUSTM ENT OF DYNAMIC BRAKES.",False,True,False,False,True,0.0
359,19,4,BNSF,48,WEATHERFORD,PARKER,H-SAGSLA1-02 DERAILED 27 RAILCARS WHILE TRAVERSING SINGLE MAIN TRACK EXCESSIVE DYNAMIC BRAKING CAUSE D BUFF FORCES. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
360,19,8,UP,48,LIBERTY,LIBERTY,"AMT2-28 HIT 18 WHEELER AT CROSSING. LEAD SET OF TRUCKS ON LEAD ENGINE DERAILED. ATK EQUIPMENT DAMA GE = $103,926",False,True,False,False,False,103926.0
361,19,8,UP,48,HARLINGEN,CAMERON,"THE LHL41-29 WAS AT HARLINGEN YARD ATTEMPTING TO BRING A YARD CUT TO OLMITO YARD. THE PLAN WAS TO D OUBLE 51 CARS OUT OF TRACK 30 AND PICK UP 45 CARS OUT OF TRACK 28. THE ENGINEER STARTED PULLING ON TRACK 30 BUT NOTICED THE CUT OF CARS GOT EXTREMELY HARD TO PULL AFTER MOVING ABOUT 1100'. THE ENGIN EER BROUGHT THE TRAIN TO A STOP, THE CONDUCTOR/BRAKEMAN WALKED BACK TO FIND 5 CARS DERAILED JUST PAS T THE CROSSOVER SWITCH. DERAILMENT WAS DRAGGED ONTO UPRR MAINTAINED TRACK. RVSC MAINTAINS TRACK. RVSC TRACK DAMAGE = $5,999",False,True,False,False,True,5999.0
362,19,3,UP,48,MARSHALL,HARRISON,THE MRENL-20 DERAILED THREE LOADED AUTO RACKS AT MP 351.06 ON THE REISOR SUB. THERE ARE NO INJURIES OR HAZMAT RELEASES ASSOCIATED WITH THIS DERAILMENT. 1 DRUG POSITIVE - NOT DETERMINED TO BE A CAUSA L FACTOR.,False,True,False,True,False,0.0
363,19,3,UP,48,BIG SANDY,UPSHUR,"TRAIN MAVFW-19, LEAD LOCOMOTIVE NS8318, DERAILED 17 CARS ON THE PINE BLUFF SUB DUE TO A MECHANICAL I SSUE ON RAILCAR ECUX844612.",False,True,False,False,False,0.0
364,19,3,UP,48,LONGVIEW,GREGG,"THE YLT25-31 WAS SWITCHING OUT OF 2 RAIL AND AS THE FOREMAN BEGAN RELEASING BRAKES AND BLEEDING AIR ON 2 RAIL IN ORDER TO PULL THE TRACK OUT, THE FOREMAN NOTICED THE CUT BEGINS TO ROLL WEST. THE CUT ROLLS OUT THE WEST END OF TRACK 2 AND COLLIDED WITH YLT67 JOB THAT IS SWITCHING ON THE WEST LEAD. T HIS RESULTED IN 10 CARS TOTAL DERAILING ON THEIR SIDES.",False,True,False,False,False,0.0
365,19,9,UP,48,VON ORMY,BEXAR,"CONTRACTOR JOB03-09, BUILT IN TRACK 801 ISAMNX-09 OCCUPYING THE 800 LEAD SWITCH WHEN DOING SO, SWITC H 800/400 WAS RAN THROUGH DUE TO CONTRACT TRAINCREW PRS/TSS EMPLOYEE NOT PROPERLY PROTECTING SHOVE E NSURING ROUTE WAS ADEQUATELY LINED. CAMERAS WERE REVIEWING SHOWING TRAIN CREW WALKED UP TO A SWITCH (412 SWITCH) SHORT OF THE 800/400 SWITCH, NEVER INSPECTING THE SWITCH FOR THE INTENDED ROUTE. UP CRE W CALLED FOR TRAIN ATTEMPTING TO DEPART CAUSING THE LAST CAR THAT RAN THROUGH THE SWITCH TO DERAIL D TTX785473 UPRIGHT. INDUSTRY MAINTAINS TRACK.",False,True,False,False,False,0.0
366,19,9,UP,48,GEORGE WEST,LIVE OAK,"LHD67-16, LEAD UNIT UP1793, STRUCK AN 18 WHEELER AT MP 82.46 OF THE CORPUS CHRISTI SUBDIVISION.",True,False,False,False,False,0.0
367,19,9,UP,48,EAGLE PASS,MAVERICK,"UP TRAIN 2MEGSA-15, LEAD UNIT UP4986, APPROACHED A BRIDGE AND SAW IT WAS ON FIRE. CREW WAS NOT ABLE TO STOP SHORT OF THE BRIDGE. ONCE STOPPED, THE CREW SAFETLY CUT THE LEAD UNIT AWAY AND CROSSED THE B RIDGE. THE WOODEN BRIDGE BECAME FULLY ENGULFED IN FLAMES, AS DID ONE LOCOMOTIVE AND TWO RAIL CARS TH AT WERE ON THE BRIDGE. PROBABLE CAUSE OF THE FIRE WAS SPARKS FROM A WHEEL ON CAR BNSF482761 FROM A B NSF TRAIN THAT HAD TRAVERSED THE TRACKS EARLIER.",False,False,True,False,False,0.0
368,19,9,UP,48,THOMASTON,DE WITT,"THE WLDEWZ-18 WAS TRAVELING SOUTH ON THE CUERO SUB WHEN THE TRAIN STRUCK A SEMI TRACTOR TRAILER LOAD ED WITH ASPHALT, WHICH WAS TRAVELING WEST.",True,False,False,False,False,0.0
369,19,3,UP,48,ARLINGTON,TARRANT,AARARR-25 DERAILED 7 CARS WHEN SHOVING INTO THE GSWN YARD. CREW WAS GOING TO MAKE THEIR SET OUT IN 2 RAIL WHEN THE ENGINEER NOTIFIED THE CONDUCTOR AND UTILITY MAN THAT THE TRAIN WENT INTO EMERGENCY. UPON FURTHER INVESTIGATION IT WAS CONFIRMED THAT 7 CARS WERE ON THE GROUND.,False,True,False,False,False,0.0
370,19,3,PTRA,48,HOUSTON,HARRIS,"SWITCHMAN KICKED CAR INTO TRACK AND COUPLING DID NOT MAKE, THE CAR ROLLED BACK INTO THE FOUL OF THE LEAD AND DAMAGED SEVERAL CARS THAT THE CREW WAS PULLING FROM AN ADJACENT TRACK.",False,False,True,False,True,0.0
371,19,4,UP,48,FORT WORTH,TARRANT,"UEBLTG-20 WAS TRAVELLING SOUTH WHEN THE TRAIN REACHED ECHO LAKE PARK BRIDGE, THE CREW NOTICED WATER RUSHING UP AGAINST THE MAINLINE ON THE SOUTH SIDE OF THE TRACKS. AS THE TRAIN ROUNDED THE CORNER PA ST THE FIRST SIGNAL, THE TRAIN WENT INTO EMERGENCY. THE TRAIN DERAILED 27 CARS DUE TO A WASHOUT AND CAUGHT ON FIRE. CAR# UTLX 209403 ETHANOL, 27,379 GALLONS. CAR#: TCBX 194145 ETHANOL, 28,779 GALLO NS. CAR#: UTLX 209301 ETHANOL, 18,270 GALLONS.",False,True,False,False,False,0.0
372,19,9,XTGS,48,ANAHUAC,CHAMBERS,"CONDUCTOR FAILED TO PROVIDE POINT PROTECTION DURING SHOVING MOVE AND RAN OVER DERAIL. CONTINUED TO S WITCH, CAUSING FURTHER DAMAGE TO TRACK AND EQUIPMENT.",False,True,False,False,True,0.0
373,19,5,LBWR,48,LUBBOCK,LUBBOCK,"AT 0255 ON 5-14-19 THE 201 CREW WERE PULLING A 92 CAR TRAIN OF LOADED HAZMAT STORAGE TANK CARS INTO DOUD. THEY STOPPED THE TRAIN TO MAKE A CUT AT UPLAND AVE.(DOT# 017591G) AND AS THE CONDUCTOR WAS TYI NG HANDBRAKES, HE HEARD A LOUD CRASH. UPON INVESTIGATION, HE FOUND A VEHICLE HAD COLLIDED WITH THE T RAIN AT THE UPLAND AVE. CROSSING. LPD IS ISSUING A CITATION FOR FAILURE TO YIELD RIGHT OF WAY. THE D RIVER DID HAVE INSURANCE. ALL CARS WERE LOADED HAZMAT BUT NO LEAKS. NO INJURIES TO THE CREW.911 WAS CALLED IMMEDIATELY AND THE DRIVER WAS TAKEN TO THE HOSPITAL. THE TRAIN WAS SECURED AGAINST UNDESIRED MOVEMENT AND THE INVESTIGATION BEGAN.THE TRAIN WAS SECURED SO THAT THERE WOULD BE NO MOVEMENT DURIN G THE REMOVAL OF THE VEHICLE OR DURING THE INVESTIGATION.",False,False,True,False,False,0.0
374,19,1,UP,48,PLEASANTON,ATASCOSA,THE LSAFT-16 WAS TRAVELING SOUTH ON THE CORPUS CHRISTI SUB AT MP 31.52 WHEN A SEMI TRUCK LOADED WITH MOLASSES PULLED OUT IN FRONT OF THEM AND THEY STRUCK IT BETWEEN THE TRUCK AND TRAILER.,True,False,False,False,False,0.0
375,19,4,UP,48,ODESSA,ECTOR,YOD52-23 DERAILED 4 SAND CARS ON THE UNIVAR LEAD DUE TO A BROKEN RAIL.,False,True,False,False,False,0.0
376,19,4,UP,48,HOLLAND,BELL,"AMTK22-25 WAS TRAVELING NORTH BOUND WHEN A VEHICLE CROSSED FROM WEST TO EAST AT THE MILLS RD CROSSIN G. THE VEHICLE DID NOT STOP OR YIELD AT THE CROSSING BUT KEPT ON GOING THROUGH. THE TRAIN STRUCK T HE VEHICLE, FATALLY INJURING THE DRIVER OF THE VEHICLE. AMTRAK'S ESTIMATED EQUIPMENT DAMAGE = $16,1 97",True,False,False,False,True,161.0
377,19,8,DGNO,48,GREENVILLE,HUNT,B703 DERAILED SEVEN CARS BETWEEN MOCKINGBIRD AND SHERMAN WITH 3 LOCOMOTIVES. 47 LOADS AND 1 EMPTY. L INES 31-37 ARE DERAILED. LINES 34-36 ARE ON THEIR SIDE.,False,True,False,False,False,0.0
378,19,7,UP,48,LONGVIEW,HARRISON,"THE ALDASB-09 DERAILED ON MAIN 1 ON THE LITTLE ROCK SUB WHEN A DRAWBAR CAME OUT OF THE HOUSING AND S TRUCK A TIE, LIFTING THE CAR AND SHIFTING IT TO THE NORTH SIDE OF THE TRACK.",False,True,False,False,False,0.0
379,19,7,UP,48,HOUSTON,HARRIS,ILBEW-19 WITH LEAD UNIT UP7181 WAS TRAVELING EAST ON NUMBER 2 MAIN WHEN THEY STRCUK A VEHICLE FOULIN G THE CROSSING AT FONDREN ROAD. DRIVER WAS ISSUED A CITATION.,False,False,True,False,False,0.0
380,19,7,BNSF,48,AMARILLO,POTTER,RCO Y-AMA3032-29 IMPACTED THE Y-AMA3011-29 WHILE SHOVING YARD TRACK 603 DUE TO FAILURE TO CONTROL SH OVE MOVE AND AN IMPROPERLY LINED SWITCH. RESULTED IN 3 RAILCARS DERAILED. NO HAZARDOUS MATERIALS WER E RELEASED.,False,True,False,False,False,0.0
381,19,4,UP,48,SAN ANTONIO,BEXAR,YSA21R-23 DERAILED 4 CARS DURING SWITCHING OPERATIONS AFTER EXPERIENCING A BROKEN KNUCKLE DURING A P ULLOUT MOVE.,False,True,False,False,False,0.0
382,19,4,UP,48,WEATHERFORD,PARKER,"BNSF TRAIN QT5TFJ-02 DERAILED 15 CARS. BNSF ESTIMATED EQUIPMENT DAMAGE = $1,380,000",False,True,False,False,True,1380000.0
383,19,4,UP,48,MESQUITE,DALLAS,"MDANL-11 AS COMING DOWN THE HILL AT MP 204 WHEN THEY LOST THEIR DYNAMIC BRAKE CAPABILITIES. SMOKE S TARTED TO ENTER THE CAB AND THE CREW COULD SEE FLAMES COMING OUT OF THE LOCOMOTIVE WHERE THE ENGINE IS LOCATED. CREW STOPPED THE TRAIN, NOTIFIED THE DISPATCHER AND SECURED THE CARS. NO DERAILMENT OR TRACK DAMAGE.",False,False,True,False,True,0.0
384,19,7,UP,48,CHANNELVIEW,HARRIS,"WHEN PULLING OUT OF TRACK 823 FROM CUSTOMER LYONDELL, 2 SETS OF TRUCKS FELL OFF THE RAIL INTO THE CU RVE DUE TO CROSS LEVEL, WARP IN THE TRACK, AND MUD SPOTS ALLOWING PUMPING. *INDUSTRY MAINTAINS TRACK",False,False,True,False,False,0.0
385,19,2,RLAX,48,BAYTOWN,CHAMBERS,CONDUCTOR ON SWITCHER 3 MADE A SHOVING MOVE INTO TRACK 551 WITHOUT ENSURING THAT THE SWITCH WAS LINE D FOR THE INTENDED ROUTE (TRACK 550). THE EQUIPMENT COUPLED AND SHOVED THE REAR CAR OFF OF THE END O F THE STORAGE TRACK-DERAILING SET OF TRUCKS.,False,True,False,False,False,0.0
386,19,9,DGNO,48,SHERMAN,GRAYSON,"WHEN MAKING REVERSE MOVE OF LOADED ROCK TRAIN, BROKEN RAIL UNDERNEATH FIRST CAR BEHIND MOTORS CAUSED ONE CAR AND ONE MOTOR TO DERAIL.
12-03-19 REVISED BLOCK #37/TRACK
",False,True,False,False,False,0.0
387,19,7,BNSF,48,JUSTIN,DENTON,Y-NYF1101-27 DERAILED 9 RAILCARS WHILE PULLING INTO YARD TRACK 7108 CARS STARTED DERAILING AFTER 120 0 FEET INTO THE TRACK. NO HAZARDOUS MATERIALS WERE RELEASED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
388,19,3,UP,48,SAN ANTONIO,BEXAR,THE MLDSA-15 WAS SHOVING WHEN THEY DERAILED 2 CARS (NOKL560999 AND COER173407) DUE TO A BROKEN RAIL.,False,True,False,False,False,0.0
389,19,3,UP,48,SAN ANTONIO,BEXAR,"IMXDT-18 WAS TRAVELING EAST ON THE DEL RIO SUB ON MAIN TRACK 2, APPROACHING S SAN MARCOS STREET, WHE N THEY NOTICED A VEHICLE GO AROUND ANOTHER VEHICLE TO CROSS MAIN TRACK 1 AHEAD OF A WEST BOUND TRAIN (MEWWC-17). THE VEHICLE WAS STRUCK BY THE EAST BOUND TRAIN AND PUSHED EAST OF THE CROSSING, DESTRO YING THE CROSSING SIGNAL AND GATES.",True,False,False,False,False,0.0
390,19,3,UP,48,ARLINGTON,TARRANT,"THE LBH03R-04 DERAILED 3 CARS IN TRACK 810 DUE TO TRACK GEOMETRY, DEVIATION FROM UNIFORM TOP OF RAIL PROFILE.",False,True,False,False,False,0.0
391,19,4,UP,48,GALENA PARK,HARRIS,GEHPHP-22 WAS SHOVING A LOADED GRAIN TRAIN INTO TRACK 4 ON THE LOW SIDE AT THE GRAIN FACILITY AT GAL ENA PARK. WHEN THEY DERAILED 4 CARS DUE TO TRACK ISSUE. INDUSTRY MAINTAINS TRACK,False,True,False,False,False,0.0
392,19,8,BNSF,48,SAGINAW,TARRANT,Y-ALT2041-04 DERAILED 6 RAILCARS AND IMPACTED A SINGLE RAILCAR IN ADJACENT TRACK WHILE SHOVING YARD TRACK 8202 DUE BUFFING ACTION BECAUSE OF TRAIN MAKEUP SHORT AND LONG CAR COMBINATION. NO HAZARDOUS M ATERIALS WERE RELEASED.,False,True,False,False,False,0.0
393,19,6,KCS,48,BEAUMONT,JEFFERSON,CREW SHOVED REAR OF TRAIN THRU SWITCH AND THEN PULLED FOWARD CAUSING FOUR CARS TO DERAIL. MP 768 BEA UMONT SUBDIVISION.,False,True,False,False,False,0.0
394,19,6,UP,48,ARTESIA WELLS,LA SALLE,"IMXDT-24, STRUCK A GTI ENERGY SERVICES TRUCK RIG THAT WAS HAULING A LOADED FLATBED WITH MOTOR GRADER , TRAVLING EAST THAT MADE A STOP AT CROSSING, AND THEN PROCEEDED OVER CROSSING.",True,False,False,False,False,0.0
395,19,4,BNSF,48,AMARILLO,POTTER,L-KAN0381-05 DERAILED 4 RAILCAR WHILE PULLING INTO YARD TRACK 103 DUE TO A DEFECTIVE SWITCH ROD. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
396,19,4,BNSF,48,AMARILLO,POTTER,Y-AMA2061-09 HAD 4 RAILCARS PUSHED OUT OF YARD TRACK 7105 AND DERAILED DURING SWITCHING OPERATIONS D UE TO INADEQUATE PRECAUTIONS WHILE KICKING RAILCARS. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
397,19,4,UP,48,HOUSTON,HARRIS,"THE TSE (RERRN-27) WAS DOUBLING OVER THE MASEW-25 FROM TRACK 217 TO TRACK 216. THEY HAD 25 CARS WHE N THEY SHOVED IN AND MADE A JOINT IN TRACK 216 AGAINST 30 CARS TIED DOWN FROM THE MYCEW-25. INSTEAD OF WALKING BACK 30 CARS TO WATCH THE SHOVE, THE CONDUCTOR PULLED THE TRAIN AHEAD 30 CARS UNTIL THE REAR OF THE TRAIN REACHED HIM. AS THE CREW IS SHOVING BACK THE CAR DERAILS AT THE FROG. DERAILED C AR WAS FUTURE BAD ORDERED UPON ARRIVAL INTO ENGLEWOOD FOR TREAD. THE WHEEL THAT DERAILED FIRST ON T HIS CAR IS THE SAME WHEEL THAT WAS FURTHER BAD ORDERED.",False,True,False,False,False,0.0
398,19,5,UP,48,DAYTON,CHAMBERS,"AEX13751 ARRIVED MONT BELVIEU YARD ON THE LHH35 ALREADY DAMAGED. DAMAGES APPEAR TO BE A RESULT OF A N IMPACT. AFTER FURTHER REVIEW/INVESTIGATION OF CAR MOVEMENT, WEIGH BILLS, NUMBER OF EVENTS, RUST A GE, AND NATUE OF DEFECT, MECHANICAL FORCES WERE NOT ABLE TO ASCERTAIN OCCURRENCE OF DAMAGE.",False,False,True,False,True,0.0
399,19,5,UP,48,GALENA PARK,HARRIS,"THE YGP55-28 WAS SHOVING 22 CARS TOWARDS LDC TRACK #6 TO SPOT 16 CARS WHEN CAR UP92688 DERAILED LEAD ING WHEEL OF REAR TRUCK ON THE #3 SWITCH, RESULTING IN A TOTAL OF 4 CARS DERAILING. CAUSE WAS DUE T O A GAPPED SWITCH POINT. INDUSTRY MAINTAINS TRACK",False,True,False,False,False,0.0
400,19,4,KCS,48,SAN DIEGO,JIM WELLS,CREW WAS SHOVING CARS. VEHICLE DROVE AROUND GATES & TRAIN STRUCK VEHICLE. ONE CAR DERAILED. RESUL TED IN A FATALITY. DATE OF DEATH 4/4/19. MP 109.54 LAREDO SUBDIVISION,True,True,False,False,False,0.0
401,19,4,KCS,48,BEAUMONT,ORANGE,TRUCK PULLING TRAILER STUCK ON TRACK. GATES WENT DOWN. TRAIN STRUCK TRAILER. MP 762.89 BEAUMONT SUBDIVISION,True,False,False,False,False,0.0
402,19,8,UP,48,FORT WORTH,TARRANT,"OVERSPEED CARS DAKX252137 AND DAKX395745 HUMPED BY YFW10R-16 WENT THROUGH 34 BOWL AND MADE CONTACT W ITH YFW35-15 CARS NATX 250961, TILX 251307, AND TILX 253942 ON THE 32 LEAD. ALL CARS DERAILED AND BO TH DAKX CARS WERE ON THEIR SIDES LEAKING PLASTIC PELLETS. NO INJURIES. CAUSE WAS FAILURE TO PLACE TH E HUMP COMPUTER IN THE PROPER MODE.",False,True,False,False,False,0.0
403,19,7,UP,48,PECOS,REEVES,"ZLAIC-20, LEAD UNIT UP3851, STRUCK A TRUCK/TRAILER AT A CROSSING.",True,False,False,False,False,0.0
404,19,8,UP,48,MARION,GUADALUPE,"AMTRAK'S AMT2-31, LEAD UNIT AMTK175, COLLIDED WITH A VEHICLE AT A PRIVATE CROSSING ON THE GLIDDEN SU B. *AMTRAK'S EQUIPMENT DAMAGE = $36,177*",False,False,True,False,True,36177.0
405,19,8,UP,48,SAN ANTONIO,BEXAR,"YEY26-16 WAS SHOVING 22 CARS INTO TRACK 3 FROM THE WEST END OF EAST YARD. WHEN SHOVING INTO TRACK 3, RAILCARS DERAILED DUE TO EXCESSIVE HORSEPOWER.",False,True,False,False,False,0.0
406,19,8,UP,48,SAN ANTONIO,BEXAR,"MSAFW-20 WAS HEADING NORTH AFTER DEPARTING SOSAN YARD ALONG THE LAREDO #1 MAIN, WHEN THE TRACTION MO TOR ON THE SECOND LOCOMOTIVE LOCKED UP, AND CAUSED THE TRAIN TO DERAIL 4 LOCOMOTIVES AND 11 CARS.",False,True,False,False,False,0.0
407,19,2,UP,48,EL PASO,EL PASO,"YLP15R-09, RAILCAR TILX3205 HAD PART OF DRAWBAR FALL OUT OF THE CAR WHEN SWITCH CREW UNCOUPLED AND P ULLED AWAY. NO DERAILMENT OR TRACK DAMAGE.",False,False,True,False,True,0.0
408,19,4,BNSF,48,DAYTON,LIBERTY,Y-DYT2111-22 HAD RAILCARS IMPACT EACH OTHER IN RESULTING IN EQUIPMENT DAMAGES DURING SWITCHING OPERA TIONS IN YARD TRACK 615 DUE TO INADEQUATE PRECAUTIONS WHILE KICKING RAILCARS. NO HAZARDOUS MATERIALS WERE RELEASED.,False,False,True,False,False,0.0
409,19,4,BNSF,48,SILSBEE,HARDIN,THE HYDRAULIC MOTOR AND ITS HOUSING BROKE FROM THE CAR BODY AND DERAILED THE TWO CARS BEHIND IT. NO HAZARDOUS MATERIALS RELEASED.,False,True,False,False,False,0.0
410,19,4,UP,48,CORPUS CHRISTI,NUECES,"YCC52-19 HAD A HOLD OF 10 CARS SHOVING BACK INTO TRACK 5, PICKING UP 5 CARS. THE CONDUCTOR DID NOT CHECK THE 5 CARS FOR HANDBRAKES AND THE CARS DID NOT HAVE ANY BRAKES APPLIED. WHEN SHOVING BACK INT O THE 5 CARS, THERE WAS A BAD CAR COUNT AND WHEN THE CARS MADE CONTACT, THEY DID NOT COUPLE AND THE REAR CAR WENT PAST THE BUMPER AND DERAILED. INDUSTRY MAINTAINS TRACK",False,True,False,False,False,0.0
411,19,4,BNSF,48,AMARILLO,POTTER,H-SLADEN1-21 DERAILED 2 RAILCARS AND 2 LOCOMOTIVES WHILE SHOVING YARD TRACK 7107 DUE TO FAILURE TO C ONTROL SHOVE MOVE IN TURN RUNNING THROUGH AND IMPROPERLY LINED SWITCH POINT DERAIL. NO HAZARDOUS MAT ERIALS WERE RELEASED.,False,True,False,False,False,0.0
412,19,9,KCS,48,LAREDO,WEBB,CREW WAS TRAVELING ON TRACK 106 AND 8 RAIL CARS DERAILED. CAR UTLX 209475 - ULTRA LOW SULPHUR DIESE L RELEASED APPROX 50 GALLONS. MP 9 LAREDO SUBDIVISION,False,True,False,False,False,0.0
413,19,9,PTRA,48,PASADENA,HARRIS,"JOB 332 SWITCHING ON THE SOUTH END LEAD OF PASADENA YARD. THE CREW PULLED A CUT OF CARS OUT OF TRACK 10, THEY KICKED THE 3 NORTH CARS BACK IN 10. AFTER KICKING THE THREE CARS THE ENGINEER NOTED THAT T HE MOVE CAME TO A STOP BY ITSELF. INSPECTION OF THE CUT FOUND THAT SIX CARS HAD DERAILED ON THE LEAD .",False,True,False,False,False,0.0
414,19,2,BNSF,48,AMARILLO,POTTER,RCO Y-AMA2062-10 DERAILED 1 RAILCAR WHILE SHOVING YARD TRACK 7108 DUE TO FAILURE TO CONTROL SHOVE MO VE IN TURN SHOVING OFF THE END OF THE TRACK. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
415,19,5,UP,48,JEWETT,LEON,CREW ON THE ALDASB-30 WITH LEAD UNIT UP6633 HIT A TREE RESULTING IN INJURY.,False,False,True,False,False,0.0
416,19,5,UP,48,ELKHART,ANDERSON,TRAIN MAGNL-18 WITH LEAD LOCOMOTIVE UP4642 WAS TRAVELING NORTH ON THE PALESTINE SUB AND DERAILED DUE TO WASHOUT AT MP 93.75.,False,True,False,False,False,0.0
417,19,5,BNSF,48,HOUSTON,HARRIS,Y-HOU2121-19 DERAILED 2 RAILCARS WHILE SHOVING YARD TRACK 1504 DUE TO AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
418,19,5,BNSF,48,SAGINAW,TARRANT,Y-SAG3211-21 DERAILED 7 RAILCARS WHILE SHOVING YARD TRACK 8201 DUE TO SWITCH NOT LATCHED OR LOCKED. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
419,19,5,BNSF,48,SAGINAW,TARRANT,Y-SAG1311-24 DERAILED 1 RAILCAR WHILE SWITCHING IN YARD TRACK 8259 DUE TO AN IMPROPERLY LINED SWITCH . NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
420,19,6,UP,48,EL PASO,EL PASO,YLP67R-26 WAS MAKING A FORWARD MOVE (EAST) WITH 5 CARS AND 3 LOCOMOTIVES WHEN TRAIN CAME TO AN IMMED IATE STOP. NO SWITCHES OR DERAILS INVOLVED. WIDE GAUGE IS THE CAUSE OF DERAILMENT. INDUSTRY MAINT AINS TRACK,False,True,False,False,False,0.0
421,19,6,UP,48,TAYLOR,WILLIAMSON,"MFWSA-05, WHILE TRAVELING SOUTH GOING FROM THE WACO SUB TO THE AUSTIN SUB THROUGH THE NORTH LEG OF T HE WYE INTO TRACK 1 OF TAYLOR YARD, DERAILED MULTIPLE CUSHIONED DRAWBAR PLACEMENTS IN TRAIN WITHOUT PLACEMENT ERRORS CAUSED BUFF FORCES IN SPIRAL OF TURNOUT THAT CAUSED DERAILMENT.",False,True,False,False,False,0.0
422,19,4,BNSF,48,EL PASO,EL PASO,"H-BELELP1-17 IMPACTED THE Y-ELP9011-17 IN STORAGE TRACK 421 DUE TO MAIN LINE SWITCH BEING LEFT IN TH E REVERSE POSITION, IMPROPERLY LINED SWITCH. THE IMPACT RESULTED IN 4 LOCOMOTIVES AND 5 RAILCARS DER AILED. NO HAZARDOUS MATERIALS WERE RELEASED.",False,False,True,False,False,0.0
423,19,11,BNSF,48,TEAGUE,FREESTONE,"R-RDV8241-31 DERAILED 5 RAILCARS ON SINGLE MAIN TRACK. THE DERAILED RAILCARS IN TURN IMPACTED AND DE RAILED A LOCOMOTIVE ON ADJACENT TRACK. AFTER PULLING THROUGH AND IMPROPERLY LINED SWITCH, SUBSEQUENT LY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED, IN TURN RUNN ING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
424,19,10,BNSF,48,SWEETWATER,NOLAN,FOREIGN TRAIN T-SWRTXO1-21 DERAILED 15 RAILCARS WHILE PULLING INTO YARD TRACK 5199. NO HAZARDOUS MAT ERIALS WERE RELEASED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
425,19,10,UP,48,ORANGE,ORANGE,"WESTBOUND QIJBTJ-4, LEAD LOCOMOTIVE BNSF5020, WITH A BNSF CREW, COLLIDED WITH A TRACTOR-TRAILER LOAD ED WITH LUMBER THAT WAS STOPPED ON A CROSSING AT MILE POST 254.7 OF THE LAFAYETTE SUBDIVISION IN ORA NGE, TX. THERE WERE NO DERAILMENTS, AND NO RELEASES DUE TO THE INCIDENT. THE DRIVER WAS OUTSIDE OF THE VEHICLE AT THE TIME OF THE COLLISION AND SUSTAINED NO INJURIES. BNSF EQUIPMENT DAMAGE = $10,15 0",False,True,False,False,True,1015.0
426,19,5,UP,48,HARWOOD,GONZALES,"THE MEWWC-16 DERAILED RAILCAR MP260411 AFTER TRAIN WENT INTO EMERGENCY STOP ONCE THE TRAIN SEPARATED . UPON INVESTIGATION, IT WAS FOUND THAT AN AIRHOSE CAME APART AND CAUSED A DRAWBAR TO PULL APART DU E TO WEAK LUGS. THIS DRAWBAR CAUSED THE CAR TO LIFT AND DERAIL 1 SET OF TRUCKS.",False,True,False,False,False,0.0
427,19,5,UP,48,SAN ANTONIO,BEXAR,"TRAIN YSA34-17, LEAD LOCOMOTIVE UP5203, WAS SHOVING NORTHBOUND AT THE SOUTH END OF THE RIP TRACKS NE AR MP265 OF THE LAREDO SUB. UPON INVESTIGATION, IT WAS FOUND THAT 6 CARS HAD DERAILED DURING THE SH OVE MOVEMENT.",False,True,False,False,False,0.0
428,19,5,UP,48,SAN ANTONIO,BEXAR,"THE YSA11-19 WAS SHOVING 89 CARS NORTH INTO 911 TRACK TO SET ON TRAIN MSAMX-19. WHILE SHOVING NORTH WITH THE CUT, 43 CARS SUCCESSFULLY WENT INTO TRACK 911, THEN LINES 45, 46, AND 47 DERAILED. CAUSE IS DUE TO INTERACTION OF LATERAL AND VERTICAL FORCES.",False,True,False,False,False,0.0
429,19,5,UP,48,PYOTE,WARD,"THE THIRD LOCOMOTIVE, UP6272, OF THE MFWWCB-30, CAUGHT ON FIRE. NO INJURIES.",False,False,True,False,False,0.0
430,19,9,UP,48,SAN ANTONIO,BEXAR,"YSA20-22, WHILE SWITCHING ON THE NORTH END OF SOSAN, KICKED A TOTAL OF 18 CARS DOWN A CLEAR TRACK IN ERROR DUE TO AN IMPROPERLY LINED SWITCH, RESULTING IN THE CARS STRICKING A TRIM CUT ON THE SOUTH LE AD AND DERAILING 4 RAILCARS.",False,True,False,False,False,0.0
431,19,9,UP,48,DIME BOX,LEE,"BNSF TRAIN, CJSCWK-21 DERAILED AT DIME BOX, TX. CAUSE WAS DUE TO IRREGULAR TRACK ALIGNMENT. BNSF EQU IPMENT DAMAGE = $61,424",False,True,False,False,True,61424.0
432,19,9,UP,48,HOLLAND,BELL,"MFWSA-12 EXPERIENCED A UDE AIR HOSE SEPARATION BETWEEN CARS SP654797 AND MP269796, CAUSING 13 CARS T O DERAIL. THE REAR END SLACK RAN OUT WHICH CAUSED A WHEEL LIFT ON AN EMPTY BOX CAR, ABOX 52033, 16 C ARS FROM THE REAR DPUS AND SUBSEQUENTLY DERAILMENT. AS THE REAR END EMERGENCY BRAKE APPLICATION SET UP, IT PULLED BACK AWAY FROM THE HEAD END WHICH ALSO CAUSED A KNUCKLE ON A EMPTY FRAME FLAT FTTX9617 38. THE TRAIN WAS OPERATING IN A 4 (3 ONLINE) X2 CONFIGURATION IN ASYNCHRONOUS MODE ON UNDULATING TE RRITORY.",False,True,False,False,False,0.0
433,19,1,UP,48,MONAHANS,WARD,"THE LBN48-31 WAS PULLING A CUT OF CARS FROM TRACK 612, AND STRUCK THE UP8368, CAUSING THE CARS TO DE RAIL.",True,False,False,False,False,0.0
434,19,5,CGIV,48,CHANNELVIEW,HARRIS,"PTRA TEAM WAS SPOTTING RAIL CARS ON CARGILL YARD. PTRA CONDUCTOR WAS STATIONED ON THE SOUTH END OF YARD TO PROTECT THE POINT WHILE THE STRING OF 114 CARS WERE BEING SHOVED TO THE UNLOAD AREA. PTRA C ONDUCTOR NOTICED THAT SOME CARS STARTED TO DERAIL AS THEY WERE GOING THROUGH A CROSSOVER SWITCH. TH E LEAD CAR MADE IT THROUGH THE CROSSOVER SWITCH, HOWEVER CARS 2-6 CAME OFF TRACK AND RESTED ON THEIR SIDE.",False,True,False,False,False,0.0
435,19,5,PTRA,48,CHANNELVIEW,HARRIS,"PTRA JOB 170 WAS SHOVING AT 6 MPH WITH 114X0 GRAIN HOPPERS IN CARGILL YARD TRACK 02 WHEN THE SECOND THROUGH SIXTH CARS IN THE SHOVE DERAILED AND TURNED OVER DUE TO WIDE GAUGE FROM DETERIORATED TIE CON DITIONS. ESTIMATE $50,000 IN EQUIPMENT DAMGES AND $100,000 IN TRACK DAMAGES.",False,True,False,False,False,150000.0
436,19,6,WTJR,48,WICHITA FALLS,WICHITA,"DERAILMENT OCCURRED ON AND WAS CAUSED BY INDUSTRY TRACKAGE. ON 6/06/19 ENGINEER ENTERED VITRO'S PLA NT TRACK WITH 25 LOADED CARS. CONDUCTOR HAD DRIVEN TO THE JOINT OF 11 EMPTY CARS ON THE LEAD OF VIR TO'S PLANT TRACK. THEY MADE THE COUPLING AND HEADED OUT TO SET THE EMPTIES ON THE MAIN BEFORE SPOTT ING THE LOADS. ENGINEER TOLD CONDUCTOR THAT THE TRAIN FELT HEAVY AND STOPPED. CONDUCTOR DROVE BACK IN TO CHECK FOR HANDBRAKES AND ENGINEER BEGAN TO WALK TRAIN. ENGINEER HAD TRAVELED ABOUT 5 CAR LEN GTHS FROM COUPLING UP TO EMPTIES. THE WEST RAIL HAD ROLLED AND THE WHEELS WERE UP ON THE INSIDE OF THE RAIL. THE WHEELS ON THE EAST SIDE HAD DROPPED INSIDE OF THE RAIL; HOWEVER, THE TRUCK FRAME WAS SLIDING ON TOP OF THE RAIL. CARS 19 THROUGH 23 HAD DERAILED. IT WAS DETERMINED THAT A CRANE SHOULD BE CALLED TO GET THE CARS RERAILED.",False,True,False,False,False,0.0
437,19,8,UP,48,EL PASO,EL PASO,"IDILB-11, LEAD UNIT UP7447, STRUCK A SEMI TRAILER WITH A VEHICLE LOADED ON THE TRAILER, CAUSING DAMA GE TO THE SEMI TRAILER AND VEHICLE. SEMI TRAILER WAS ON THE CROSSING WHEN TRAIN STRUCK IT.",True,False,False,False,False,0.0
438,19,9,TXGN,48,HARWOOD,GONZALES,"THE T101 JOB WERE ASSIGNED TO CLASSIFY INBOUND STORAGE CARS FROM THE UPPER YARD TO THE LOWER YARD PR IOR TO SPOTTING GONZA CUSTOMERS. THE CREW SWITCHED OUT THE THREE LOADS FOR GONZA CUSTOMERS AND HOOKE D UP TO 44 EMPTIES. THE CREW THEN COMPLETED THE SHOVE FROM THE LOOP ONTO THE LOWER GONZA LEAD. ONCE THE ENGINEER CLEARED THE GONZA LEAD SWITCH THE TRAIN WENT INTO EMERGENCY, UPON CHECKING THE TRAIN TH E CREW DISCOVERED CAR, WHICH WAS NUMBER 30 IN CONSIST, HAD DERAILED.",False,True,False,False,False,0.0
439,19,8,UP,48,DALLAS,DALLAS,"THE YMY36R-01 WAS SWITCHING CARS ON THE SOUTH LEAD AT MILLER YARD. UPON PULLING DOWN THE LEAD AND CL EARING THE FIVE SWITCH, THEN LINING THE FIVE SWITCH TO SHOVE NORTH, THE CREW NOTICED THEY HAD THREE CARS ON THE GROUND DUE TO WORN SWITCH POINTS.",False,False,True,False,False,0.0
440,19,8,UP,48,GRAND SALINE,VAN ZANDT,"MAVFW-07 SECOND UNIT, UP6416 STARTED ON FIRE. SHUT DOWN LOCOMOTIVE AND EXTINGUISHED THE FLAMES. NO D ERAILMENT.",False,False,True,False,False,0.0
441,19,3,DCTA,48,LAKE DALLAS,DENTON,"MOTORIST WAS TRAVELING WESTBOUND ON KELTON AVE, DROVE THROUGH CROSSING GATES IN DOWN POSITION AND WA S STRUCK BY TRAIN.",True,False,False,False,False,0.0
442,19,2,UP,48,KNIPPA,UVALDE,"BRANDT TRUCK 84672, WHILE MAKING A SHOVE MOVE, RAN THROUGH POWER SWITCH AT CPSA289, CAUSING EXTENSIV E DAMAGE. NO DERAILMENT OR EQUIPMENT DAMAGE.",False,False,True,False,True,0.0
443,19,2,UP,48,BAYTOWN,HARRIS,"LHH30-01 CREW WAS SHOVING TRACK 48 WHEN THE BRAKEMAN LINED SWITCH UNDER CARS, DERAILING 4 CARS.",False,True,False,False,False,0.0
444,19,2,UP,48,GOODRICH,POLK,FIRST KNOWLEDGE OF CAR WITH IMPACT DAMAGE ON A-END OF CAR (BUCKLED SIDE SILLS) ON 2/14/19. CAR WAS DELIVERED TO INDUSTRY ON 2/4/19. INDUSTRY CLAIMS 10 DAYS LATER THAT DAMAGE OCCURRED PRIOR TO DELIVE RY INTO THEIR PLANT. NO KNOWN INCIDENT PRIOR TO DELIVERY. NO DERAILMENT OR TRACK DAMAGE.,False,False,True,False,True,0.0
445,19,2,UP,48,HOUSTON,HARRIS,"THE YHO31R-23 PULLED SOUTH OUT OF SETTEGAST YARD TO DRAG A CUT OF CARS SOUTH TOWARDS THE NORTHEAST W YE CONNECTION TRACK. THE CONNECTION TRACK FROM THE HOUSTON EAST BELT TO THE HOUSTON SUBDIVISION IN IN A CURVE. ONCE THE RCO MOVEMENT TRAVERSED ONTO THE HOUSTON SUB, THEIR LEAD RCL UNIT WENT INTO SUP PRESSION, CAUSING THEIIR TRAIN TO STOP ABRUPTLY. THIS STOP WAS CAUSED BY THE RCL SYSTEM RECEIVING A `NO TAG` FAULT. OPERATOR A USED THE OVERRIDE BUTTON TO CONTINUE THE MOVE SOUTH TO FINISH MAKING TH E TRIM MOVE OUT OF THE YARD. OPERATOR A THEN PITCHED THE CONTROL BACK TO OPERATOR B TO PROCEED SHOV ING BACK INTO THE YARD WITH THE CUT OF CARS. ONCE THE JOB BEGAN TO SHOVE BACK INTO SETTEGAST YARD, THE ENGINE WENT INTO SUPPRESSION AGAIN, CAUSING ADDITIONAL FORCES IN TRAIN TO TAKE PLACE. THESE ERR ATIC STOPS PULLING OUT AND SHOVING BACK INTO THE YARD CAUSED ADDITIONAL LATERAL & VERTICAL FORCES WI THIN THE CURVE OF THE CONNECTION TRACK, ULTIMATELY CAUSING THE WHEELS TO DERAIL. UPON INSPECTION, T HE CREW FOUND 7 CARS DERAILED. CAUSE OF THE DERAILMENT DETERMINED TO BE THE FORCES PLACED ON THE EM PTY CARS WITHIN THE CURVE OF THE CONNECTING TRACK (LATERAL & VERTICAL), WITH THE ADDITION OF THE RCL UNIT GOING INTO THE SUPPRESSION FROM RECEIVING A NO TAG FAULT.",False,True,False,False,False,0.0
446,19,6,UP,48,FORT WORTH,TARRANT,"MFWWCB-01, UP8380 HAD A TURBO FIRE. NO DERAILMENT OR TRACK DAMAGE.",False,False,True,False,True,0.0
447,19,1,KCS,48,VICTORIA,VICTORIA,STRUCK A TRUCK FOULING THE TRACK. MP 977.43. ROSENBERG SUBDIVISION,True,False,False,False,False,0.0
448,19,12,ATK,48,DAYTON,LIBERTY,"TRAIN 2 OPERATING WITH LOCOMOTIVES E/173-E/153 AND 7 CARS STRUCK A CEMENT-MIXING TRUCK AT MP 404.65, COUNTY RD 621 CROSSING. HIGHWAY USER AGE AND GENDER IS UNKNOWN.",True,False,False,False,False,0.0
449,19,12,FWWR,48,FORT WORTH,TARRANT,TRAIN SHOVING EAST ON MAIN LINE WHEN TRUCK AND TRAILER STOPPED ON CROSSING. THE GATES OF THE CROSSI NG CAME DOWN ON THE TRUCK. TRAIN WAS PLACED INTO EMERGENCY BUT MADE IMPACT. DRIVER OF THE TRUCK WA S CITED FOR FAILURE TO YEILD TO TRAIN.,False,False,True,False,False,0.0
450,19,10,UP,48,SMITHVILLE,BASTROP,"MFWSA-08 DERAILED 11 CARS WHILE APPROACHING SMITHVILLE, TX. FIRST INVOLVED CAR CLIMBED THE HIGH SID E OF A FIVE DEGREE CURVE. EVENT RECORDER REVIEW FOUND NO EXCEPTIONS TO TRAIN HANDLING. TRACK MEASU RES SHOW IT TO BE TO STANDARD. TRAIN WAS IN COMPLIANCE WITH UP BUILD STANDARDS. EXCESSIVE IN-TRAIN FORCES CAUSED CAR TO BE PUSHED OFF THE HIGH SIDE OF THE CURVE.",False,True,False,False,False,0.0
451,19,10,UP,48,SAN MARCOS,HAYS,"ROGHL-09 TRAVELING NORTHWARD ON AUSTIN SUB, STRUCK AN 18-WHEELER THAT WAS STALLED ON THE TRACKS. 18 -WHEELER WAS STRUCK IN THE MIDDLE OF THE EMPTY TRAILER.",True,False,False,False,False,0.0
452,19,10,UP,48,OLDEN,EASTLAND,"IDILB-17, LEAD LOCOMOTIVE UP6700 CAUGHT FIRE WHILE PULLING THE GRADE AT MP 347. THE FIRE DEPARTMENT CAME OUT AND EXTINGUISHED THE FIRE AND SAID THERE WERE RAGS SOAKED WITH DIESEL ON TOP OF THE ENGINE THAT STARTED THE FIRE. NO INJURIES TO THE CREW MEMBERS OR THE FIRE DEPT. NO DERAILMENT OR TRACK D AMAGE.",False,False,True,False,False,0.0
453,19,6,UP,48,STANTON,MARTIN,"MODFW-10, LOCOMOTIVE UP5325 CAUGHT FIRE. NO DERAILMENT.",False,False,True,False,False,0.0
454,19,3,BNSF,47,MEMPHIS,SHELBY,RCO Y-MEM2222-14 HAD RAILCARS UNCOUPLE WHILE SHOVING YARD TRACK 102 AND IMPACT THE H-MEMBIR1-14 THAT WAS STANDING WAITING TO DEPART. RESULTED IN A TOTAL OF 11 RAILCARS DERAILED. NO HAZARDOUS MATERIALS WERE RELEASED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
455,19,11,CSX,47,NASHVILLE,DAVIDSON,NKCR 7296 ROLLED IN B-34 AND KICKED THE SKATES OFF AND ROLLED INTO B-36 THAT WAS BEING PULLED OUT BY Y29108 WHILE BUILDING Q53308.,False,False,True,False,False,0.0
456,19,10,IC,47,MEMPHIS,SHELBY,"CREW REPORTED TRACK MO20 ROLLED OUT OF THE SOUTH END TRACK CAUSING GPLX78230 TO BE SIDE SWIPED BY 3 CARS BEING PULLED OUT OF TRACK MO15. IT WAS LEARNED THE PROPERLY FUNCTIONING RETARDERS WERE OVERWHEL MED BY THE CUMALATIVE WEIGHT OF DOUBLE CUT EXTRA HEAVEY CARS BEYOND THE RETARDER'S BREAKING CAPABILI TY. GOING FORWARD CAPITAL INVESTMENT IS INSTALLING ADDITIONAL INERT RETARDING DEVICES AT THE END OF BOWL TRACKS. IN ADDITION, THERE WILL BE A REDUCTION OF TWO CAR CUTS OF EXTRA HEAVY TO ONLY SINGLE CA RS.",False,False,True,False,False,0.0
457,19,8,CSX,47,NASHVILLE,DAVIDSON,DURING NORMAL HUMPING OPERATIONS SKATES FAILED TO HOLD BRIX97471 IN B31 AND THIS CAR SIDE SWIPED TIL X 290885 AND AOK 27653.,False,False,True,False,False,0.0
458,19,4,UP,48,BRYAN,BRAZOS,MFWHO-24 DERAILED 8 CARS AND 3 LOCOMOTIVES DUE TO WEAKENED STRUCTURE CAUSED BY WASHOUT.,False,True,False,False,False,0.0
459,19,9,CSX,45,CAMERON,CALHOUN,F71706 STRUCK A LOADED TRACTOR AND TRAILER AT A ROAD CROSSING AT GRADE WHICH RESULTED IN DERAILING 2 LOCOMOTIVES AND THE HEAD 2 CARS. ENGINEER AND CONDUCTOR BOTH INJURED. AGE UNKNOWN. PROTECTION ALSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS (STOP LINES & RR XING SYMBOLS).,True,True,False,False,False,0.0
460,19,7,LC,45,RICHBURG,CHESTER,TRAIN 14 OPERATING 8MPH ON 1.2% DECENDING GRADE W/ 10LBS OF BRAKING AEX 8160 DERAILED CAUSING 7 BEHI ND TO DO SAME. BENT CENTER PIN - CENTER PINE HALE DISTORTED AND L1 + R2 BRAINS SEIZED,False,True,False,False,False,0.0
461,19,2,BNSF,46,MILBANK,GRANT,VEHICLE WITH TRAILER WAS STUCK ON CROSSING DUE TO SNOW AND ICE. TRAIN COLLIDED WITH TRAILER CAUSING DERAILMENT OF 23 CARS. DERAILMENT THEN COLLIDED WITH COAL TRAIN IN THE SIDING.,False,True,False,False,False,0.0
462,19,3,BNSF,46,LYONS,MINNEHAHA,X-INBLYS9-01 DERAILED 6 RAILCARS WHILE PULLING OUT OF INDUSTRY TRACK 4101 DUE TO TRACK BROKEN RAIL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
463,19,5,CSX,45,FLORENCE,FLORENCE,"Q49211 DERAILED WHILE DEPARTING FLORENCE YARD. TRAIN CONTINUED ON THE SOUTH END SUBDIVISION FOR APP ROXIMATELY 13 MILES CAUSING DAMAGE TO MULTIPLE MAIN LINE POWER SWITCHES. RAIL CAR TEXX 900 SHOULD H AVE BEEN PLACED ON THE REAR OF Q492-11, HOWEVER THERE WE NO RESTRICTIONS IN THE YES SYSTEM, THE CSX OPERATING RULES MANUAL DOES NOT LIST THIS CAR AS A REAR RIDER AND NOTHING FLAGGED ON THE WORK ORDER TO ALERT THE CREW OF ANY RESTRICITONS ON THIS CAR.",False,True,False,False,True,0.0
464,19,9,CSX,45,ORA,LAURENS,F79119 STRUCK A DUMP TRUCK THAT FAILED TO ADHERE TO ROAD CROSSING WARNING DEVICES..,True,False,False,False,False,0.0
465,19,3,CSX,45,HOLLY HILL,ORANGEBURG,F75528 WHILE SHOVING ONTO THE FENCE TRACK THE RAIL BROKE UNDER THE TRAIN DERAILING 5 CARS.,False,True,False,False,False,0.0
466,19,3,CSX,45,NORTH CHARLESTON,CHARLESTON,Y29013 KICKED CAR TO TRACK 007 WHERE IT STAYED IN FOUL. SECOND CAR WAS KICKED TO TRACK 11. THE CARS SIDESWIPED DUE TO CAR WASN?T CLEAR OF THE LEAD AT THE 007 SWITCH.,False,False,True,False,False,0.0
467,19,1,ATK,42,PHILADELPHIA,PHILADELPHIA,"WHILE ENGINE 661 WAS SHOVING 5 CARS INTO 28 TRACK PCY, THE R-3 WHEEL CAME OFF OF RAIL AND FELL INTO GAUGE CAUSING DERAILMENT. THERE WERE NO INJURIES TO REPORT.",False,True,False,False,False,0.0
468,19,1,CRSH,42,BRISTOL,BUCKS,FP12 WAS SERVICING DOW WHEN CARS DERAILED DUE TO BROKEN JOINT BAR.,False,True,False,False,False,0.0
469,19,1,NS,42,YORK,YORK,"H96H225 WITH 3 UNITS, 48 LOADS, AND 6140 TONS OPERATING EAST ON YORK SWITCHING LEAD DERAILED 7 LOADE D CARS.",False,True,False,False,False,0.0
470,19,5,CSX,45,ABBEVILLE,ABBEVILLE,N31927 TRAVELING NORTHBOUND AT 19 MPH DERAILED HEAD 14 CARS AT MP SG 443.8.,False,True,False,False,False,0.0
471,19,2,CSX,45,CLARKS HILL,MCCORMICK,Q69227 HAD A CENTER SILL BREAK IN CAR KCS 161040 CAUSING CAR FSRR 107391 TO DERAIL.,False,True,False,False,False,0.0
472,19,2,CSX,45,FLORENCE,FLORENCE,Y19024 DERAILED DUE TO RAIL CAR WHERE COUPLER WAS LOWER THAN SET STANDARDS. ALSO ANOTHER CAR DERAILE D DUE TO COUPLER WAS HIGHER THAN SET STANDARDS AND WAS ALSO DEFECTIVE DUE TO THE EXTREME WARP IN THE MIDDLE OF THE CAR.,False,True,False,False,False,0.0
473,19,11,NS,42,GEORGES STATION,WESTMORELAND,"WESTBOUND Z7XC107 OPERATING ON MAIN 2 FAILED TO STOP SHORT OF THE REAR END OF TRAIN 21VC108 WHICH WA S STOPPED AHEAD, DERAILING BOTH LOCOMOTIVES ON Z7XC107 AND THE REAR 3 CARS ON TRAIN 21VC108. 20QC107 OPERATING EASTBOUND ON MAIN 1 WAS STRUCK BY Z7XC1107 LOCOMOTIVES WHEN THEY DERAILED AFTER STRIKING 21VC108, THIS CAUSED LINES 48 THROUGH 55 TO DERAIL ON 20QC107.",True,True,False,False,False,0.0
474,19,11,NS,42,CONWAY,BEAVER,"CW24 SHOVING EAST ON TRACK WF903 DERAILED CAR HLSC 3059 AND CARS ON ADJACENT TRACK WF902, NS 170334, NS 170387 AND NS 170278.",False,True,False,False,False,0.0
475,19,2,BNSF,41,PORTLAND,MULTNOMAH,Y-ESJ2291-13 DERAILED 2 RAILCARS WHILE SHOVING YARD TRACK 2277 DUE TO FAILURE TO CONTROL SHOVE MOVE IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
476,19,9,NS,39,BELLEVUE,HURON,LB29 WAS TRAVERSING THE 41 CROSSOVER SWITCH ON NUMBER 2 PULLBACK WHEN THE SWITCH POINT OPENED UP UND ER MOVEMENT RESULTING IN A DERAILMENT.,False,True,False,False,False,0.0
477,19,10,NS,39,HUDSON,SUMMIT,"C97 PULLING WITH 2 UNITS AND ONE LOAD, DERAILED CAR TILX 621296 R1, R2, R3, R4, L3, & L4.",False,True,False,False,False,0.0
478,19,9,NS,39,EVENDALE,HAMILTON,"NS TRAIN LC29, A RCO INDUSTRY ASSIGNMENT WORKING IN RULE 261 TERRITORY, SHOVING EAST STRUCK STANDING TRAIN M23L026 AT MPCF17.9 AT A SPEED OF 16MPH. SUBSEQUNELTY DERAILING SHPX432618 L1 AND R1 WHEELS W HICH WAS PART OF LC29 TRAIN AND DAMAGING A CAR FROOM M23L026 TRAIN DJTX 30763.",True,True,False,False,False,0.0
479,19,10,NS,39,MAPLE HEIGHTS,CUYAHOGA,NS TRAIN 21VC303 WHILE SHOVING EAST ON TRACK 3 WEST AT MAPLE HEIGHTS SHOVED OVER THE DERAIL AT THE E AST END OF TRACK 3 WEST DERAILING DTTX 728415.,False,True,False,False,False,0.0
480,19,12,NS,39,SALEM,COLUMBIANA,C45C608 CONDUCTOR PLACED DERAIL IN THE DERAILING POSITION AS LOCOMOTIVE WAS TRAVERSING OVER THE DERA IL AT SIMMONS FEED PC69.6.,False,True,False,False,False,0.0
481,19,12,NS,39,CHATFIELD,CRAWFORD,TRAIN 178L828 TRAVELING WEST TOWARDS BELLEVUE WAS STOPPED AT CHATTFIELD MP S 73.7 DUE TO EXCESSIVE W IND ADVISORY. WHILE STOPPED THE REAR CAR OF THE CONSIST A CP546106 (EMPTY AUTORACK) WAS BLOWN ONTO I TS SIDE.,False,False,True,False,False,0.0
482,19,12,CSX,39,OREGON,LUCAS,Y10917 SHOVING INTO L09 TRACK DERAILING 10 CARS .,False,True,False,False,False,0.0
483,19,8,CSX,39,CINCINNATI,HAMILTON,"TILX 31178 STALLED ON HUMP, CARS HUMPED INTO IT & BUCKLED SKIN/SIDE SILL.",False,False,True,False,False,0.0
484,19,1,CSX,39,SHILOH,RICHLAND,Q25419 COLLIDED WITH A CITY SNOW PLOW THAT WAS STUCK ON THE CROSSING. THE OPERATOR OF THE SNOW PLOW WAS ABLE TO JUMP OFF BEFORE IMPACT AND RAN TO A NEARBY CONVENIENCE STORE.. AGE UNKNOWN. PROTECTION ALSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS (STOP LINES & RR XING SYMBOLS).,False,False,True,False,False,0.0
485,19,1,CSX,39,CHILLICOTHE,PIKE,T61221 STRUCK TREES FROM LAND SLIDE.,True,False,False,False,False,0.0
486,19,2,CSX,39,WILLARD,HURON,Y39614 WAS PULLING WEST OUT OF W16 WHEN THE RAIL BROKE UNDER THE 16TH CAR DERAILING 6 CARS. THE 3RD AND 4TH DERAILED CARS WERE LEANING TOWARD 1 MAIN SIDESWIPING THE REAR 10 CARS OF K13814 THAT WAS PUL LING EAST INTO THE BLOCKSWAP.,False,True,False,False,False,0.0
487,19,1,CSX,39,ASHTABULA,ASHTABULA,THE C51916 FAILED TO REESTABLISH THE ZONE AFTER LUNCH RESULTING IN SIDESWIPE OF CAR GACX 54009 ON TH E Q56015.,False,False,True,False,False,0.0
488,19,9,CSX,39,COLUMBUS,FRANKLIN,"WHILE SHOVING TRACK P19, Y39101 DERAILED LEADING TWO CARS. UPON INVESTIGATION THERE WERE SEVERAL LO W JOINTS ON THE NORTH RAIL. THE JOINT THAT CAUSED THE DERAILMENT DID NOT MEET CLASS ONE STANDARDS. T HE JOINT CAUSING THE DERAILMENT MEASURED 3 ? INCHES LOW UNDER LOAD, WHICH CAUSED THE DERAILMENT. WHI LE THEY WERE SHOVING LOW JOINTS CAUSED A ROCKING EFFECT, UPON PASSING THE 3 ? LOW JOINT THE CAR TIPP ED OVER ON ITS SIDE.",False,True,False,False,False,0.0
489,19,12,CSX,39,WALBRIDGE,WOOD,Y19714 SHOVING INTO E01 TRACK IN THE NORTHWARD DIRECTION DERAILING 3 CARS.,False,True,False,False,False,0.0
490,19,12,NS,39,BELLEVUE,SANDUSKY,NS MOW VEHICLE WAS STRUCK BY A HWY-USER AT A HWY-GRADE CROSSING. DRIVER'S AGE NOT VERIFIED.,True,False,False,False,False,0.0
491,19,12,ATK,36,RENSSELAER,RENSSELAER,"RULE VIOLATION: A SIDE SWIPE AND DERAILMENT OF 2 SETS OF TRAIN EQUIPMENT WAS REPORTED ON THE NORTH END OF THE RENSSELAER MECHANICAL FACILITY, NORTH OF THE ALBANY TRAIN STATION. THE TRAIN SETS INVOLV ED WERE: TRAIN 232 ON #9 TRACK WITH E/711 AND 6 CARS. TRAIN 234 ON #14 TRACK WITH E/705 AND 6 CARS . THE DIRECTION OF MOVEMENT FOR BOTH TRAIN SETS WAS NORTHWARD.",False,True,False,False,False,0.0
492,19,12,NS,36,BUFFALO,ERIE,C88C911 PULLING WEST THROUGH THE BSOR CONNECTION TRACK DERAILED FIVE CARS.,False,True,False,False,False,0.0
493,19,8,CSX,39,CAREY,WYANDOT,H70211 COLLIDED WITH W31411. SEVERAL CARS DERAILED. IT IS UNKNOWN WHETHER A POSITIVE DRUG TEST RESUL T WERE THE CAUSE OF THIS DERAILMENT BUT IT IS A CONTRIBUTING FACTOR.,False,True,False,False,False,0.0
494,19,8,CSX,39,CINCINNATI,HAMILTON,"EMPLOYEE CLEARED STALL PROTECTION WHILE WORKING AS HUMP YARDMASTER WITHOUT VERIFYING CARS WERE IN TH E CLEAR IN B20. EMPLOYEE HUMPED INTO ADJACENT TRACK B21, STRIKING FOULED CARS IN B20 CAUSING DAMAGE TO EQUIPMENT.",False,False,True,False,True,0.0
495,19,12,ATK,36,NEW YORK NEW YORK,NEW YORK,"RULE VIOLATION: AMTRAK RELAY CREW YNP06A WAS SHOVING NJT 7817 EQUIPMENT ONTO NO.4 TRACK. THE CONDU CTOR WAS ON THE LEADING END OF THE MOVE WITH E/4640 AND ALLEGED HE WAS USING THE COMMUNICATING SIGN AL APPLIANCE `BUZZER` TO GIVE THE CAR COUNT DUE TO RADIO CHATTER. ENGINEER OPERATING FROM THE REAR E/7031 WAS SIGNALED TO STOP. AS THE ENGINEER WAS COMING TO A STOP, MOTOR 4640 STRUCK THE BUMPING BL OCK ON NO.4 TRACK. DAMAGE TO NJT EQUIPMENT IS $73,946.",True,False,False,False,True,73946.0
496,19,12,ATK,36,LONG ISLAND CITY,QUEENS,RULE VIOLATION: SUNNYSIDE YARD CREW WAS ASSIGNED TO MOVE TRAIN 79S EQUIPMENT OFF 7 TRACK TO THE STA TION. IT WAS ALLEGED THAT THE CREW PASSED THE 34RA SIGNAL AT `Q` TOWER IN STOP POSITION AND RUNNING THROUGH THE 39 SWITCH NORMAL WHICH WAS LINED AGAINST THEIR MOVE.,False,False,True,False,False,0.0
497,19,3,UP,35,LOGAN,QUAY,"TRAIN IG4TU-12 DERAILMENT CAUSED BY HIGH WIND GUST CONDITIONS. AS TRAIN WAS CROSSING BRIDGE WESTWAR D, HIGH WINDS BLEW OVER REAR 25 CARS OF TRAIN DOWN EMBANKMENT.",False,True,False,False,False,0.0
498,19,8,UP,35,LORDSBURG,HIDALGO,"LKH10-05, WHILE MAKING A SHOVING MOVE WITH LIGHT POWER, SHOVED THROUGH A BAD SWITCH, THEN REVERSED D IRECTION AND DERAILED BOTH LOCOMOTIVES.",False,True,False,False,False,0.0
499,19,8,UP,35,SANTA ROSA,GUADALUPE,THE GBLB6P-01 WAS TRAVELING WEST AT 37MPH IN A TEMPORARY SPEED RESTRICTION OF 45MPH. 16 RAILCARS DER AILED DUE TO DISTURBED TRACK.,False,False,True,False,False,0.0
500,19,8,BNSF,35,GALLUP,MCKINLEY,"ENGINEER RAN THROUGH A SWITCH, CHANGED DIRECTIONS AND DERAILED 4 CARS.",False,True,False,False,False,0.0
501,19,11,BNSF,35,GALLUP,MCKINLEY,G-LRLFRS9-26 DERAILED 2 LOCOMOTIVES WHILE PULLING INTO YARD TRACK 1626 DUE TO TRACK BROKEN RAIL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
502,19,11,BNSF,35,FORT SUMNER,DE BACA,Z-STOCHI6-28 DERAILED 9 RAILCARS WHILE TRAVERSING MAIN 1 TRACK DUE TO TRACK BROKEN RAIL. NO HAZARDOU S MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
503,19,9,ATK,35,LAGUNA,CIBOLA,BOULDER/ROCK STRIKE: TRAIN 3 WAS DELAYED AFTER STRIKING A BOULDER ON THE TRACKS AT MP66.7. ALL CAR S REMAINED ON THE TRACKS BUT DAMAGE WAS REPORTED TO THE PLOW AND ON THE ENGINEERS SIDE OF LEAD LOCOM OTIVE E/164.,False,False,True,False,True,0.0
504,19,7,BNSF,35,CLOVIS,CURRY,"Y-CLO3021-24 DERAILED 6 RAILCARS IN YARD TRACK 104. AFTER PULLING THROUGH AND IMPROPERLY LINED SWITC H, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIAL WAS RELEASED.",False,True,False,False,False,0.0
505,19,2,UP,35,LORDSBURG,HIDALGO,"THE MFWWC-01 HAD A SINGLE CAR DERAILMENT DUE TO BREAK-IN-TWO FROM A WRONG-END DRAWBAR, RESULTING IN APPROXIMATELY 1000 FEET OF TRACK DAMAGE.",False,True,False,False,True,0.0
506,19,10,BNSF,35,CLAYTON,UNION,E-SLPBTM8-77 DERAILED 8 RAILCARS WHILE SHOVING OUT OF SIDING TRACK 6698 DUE TO EXCESSIVE SLACK ACTIO N. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
507,19,8,BNSF,35,PORTALES,ROOSEVELT,"TRACTOR & TRAILER WAS TRAVELING WEST BOUND AND CROSSED IN FRONT OF THE TRAIN, THE TRAIN IMPACTED THE PASSENGER SIDE OF THE TRUCK RESULTING IN DISLODGING THE TRAILER FROM THE TRUCK, THREE LOCOMOTIVES A ND EIGHT CARS DERAILING.",False,True,False,False,False,0.0
508,19,8,SW,35,DEMING,LUNA,EQUIPMENT DAMAGE - $3211.45 + TRACK DAMAGE - $7860.00 = TOTAL $11071.46,False,False,True,False,True,11071.46
509,19,4,UP,35,LORDSBURG,HIDALGO,MWCEW-10 WAS TIED DOWN IN THE SIDING AT GARY. THE OUTBOUND CREW GOT ON THE TRAIN AND AFTER UNTYING IT THEY PROCEEDED ON SIGNAL INDICATION EASTWARD. THEY RAN OVER THE LAST DERAIL THAT WAS IN THE DERA ILING POSITION PUTTING THE LEAD 3 AXLES OF THE UP8083 ON THE GROUND.,False,True,False,False,False,0.0
510,19,9,BNSF,35,GRANTS,CIBOLA,H-BARGAL1-20 DERAILED 1 RAILCAR WHILE TRAVERSING MAIN 1 TRACK RESULTING IN TRACK DAMAGE. NO HAZARDOU S MATERIALS WERE RELEASED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,True,0.0
511,19,9,BNSF,35,LAGUNA,CIBOLA,AMTRAK HIT A BOULDER ON BNSF MAIN TRACK CAUSING DAMAGE TO AMTRAK LEAD LOCOMOTIVE. NO HAZMAT RELEASED .,False,False,True,False,True,0.0
512,19,4,UP,31,NORTH PLATTE,LINCOLN,"THE YNP12R-03, WHILE SHOVING, DERAILED 2 CARS ON THE 9/10 - 11/13 FROG DUE TO TRACK GEOMETRY.",False,True,False,False,False,0.0
513,19,7,UP,31,NORTH PLATTE,LINCOLN,THE HELPER ON THE YNP44R-22 WAS TRIMMING THE MNPAH DOWN EAST DEPARTURE 5 TRACK. THE HELPER FAILED TO STOP HIS TRAIN IN THE CLEAR AND COLLIDED WITH THE MNPAL-22 THAT WAS DOUBLED UP ON THE DEPARTURE YAR D LEAD.,False,False,True,False,False,0.0
514,19,7,UP,31,NORTH PLATTE,LINCOLN,"WHILE SHOVING WEST INTO FORWARDER 10, THE YNP31R-23 DERAILED 6 CARS ON THE 8-13 LEAD.",False,True,False,False,False,0.0
515,19,6,UP,31,NORTH PLATTE,LINCOLN,"WHILE SHOVING 7 CARS, UNP46-26 DERAILED 3 CARS ON THE TEEN LEAD AT THE CAB ALLEY SWITCH. EMPLOYEE S TATED THEY WERE RIDING ON A RAIL CAR HOLDING ONTO THE LADDER WITH THEIR RIGHT HAND AND WAS REACHING UP WITH THEIR LEFT ARM TO USE THE RADIO WHEN THE CAR CAME TO A SUDDEN STOP THROWING THEM INTO THE LA DDER. HE REPORTED HIS LEFT SHOULDER ON THE BAR. INVESTIGATION FOUND THAT THE BRAKE RIGGING HAD BE EN DAMAGED DUE TO BOWL DAMAGE. CAR HAD BEEN HUMPED MULTIPLE TIMES AND NOT BEEN INSPECTED PRIOR TO T HE INCIDENT.",False,True,False,False,True,0.0
516,19,6,UP,31,NORTH PLATTE,LINCOLN,CAR SDPX96231 DERAILMENT DUE TO SHOE WITHIN GROUP 4 FINALS RETARDER FAILING AND DROPPING DOWNWARD CA USING CAR TO CLIMB THE RETARDER DERAILING AT THE EAST END OF THE FINAL. 1 SET OF TRUCKS IN THE DIRT .,False,True,False,False,False,0.0
517,19,2,UP,31,AMES,DODGE,"THE CNAWF9-05 DERAILED THE DP LOCOMOTIVE UP8521 AND ONE LOADED COAD CAR NORX2550. THE DPU AT THE RE AR OF TRAIN WAS DRAGGED 2.4 MILES, CAUSING BROKEN TIES, BUSTED OFF CLIPS AND TORE UP POWER SWITCHES AT CONTROL POINT. ALSO HAD TO REPLACE RAIL.",False,True,False,False,False,0.0
518,19,2,UP,31,OMAHA,DOUGLAS,"THE LNA01-13, WHILE ON YARD 2 TRACK 822, DERAILED THE MTNR175157 ON THE YARD 2 TRACK 820 SWITCH. TH E DERAILED CAR CAUSED AN ADDITIONAL 2 CARS TO DERAIL AS WELL.",False,True,False,False,False,0.0
519,19,2,UP,31,NORTH PLATTE,LINCOLN,YNP28R-12 BYPASSED COUPLERS IN WEST BOWL 52 BETWEEN CARS BNSF561471 AND TBOX667631. BOTH CARS DERAI LED.,False,False,True,False,False,0.0
520,19,6,BNSF,35,ALBUQUERQUE,BERNALILLO,Y-ABQ2011-25 DERAILED 2 RAILCARS WHILE SHOVING INDUSTRY TRACK 761 DUE TO FAILURE TO COMPLY WITH RADI O COMMUNICATION IN TURN SHOVING OFF THE END OF THE TRACK. NO HAZARDOUS MATERIALS RELEASED.,False,True,False,False,False,0.0
521,19,10,BNSF,35,RADIUM SPRINGS,DONA ANA,G-KMLELP9-28 DERAILED 23 RAILCARS AND 1 LOCOMOTIVE WHILE TRAVERSING SINGLE MAIN TRACK DUE TO TRACK B ROKEN RAIL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
522,19,4,BNSF,35,BELEN,VALENCIA,RCO Y-BEL1022-13 DERAILED 4 RAILCARS WHILE SHOVING YARD TRACK 7105 DUE TO EXCESSIVE SLACK ACTION. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
523,19,6,BNSF,38,BEULAH,MERCER,R-TWI7172-21 DERAILED 4 RAILCARS WHILE PULLING INTO INDUSTRY TRACK 3804 DUE TO TRACK ROADBED SETTLED OR SOFT. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
524,19,5,BNSF,38,GRAND FORKS,GRAND FORKS,U-GFDPLU0-19 OPERATING LIGHT LOCOMOTIVES IMPACTED THE H-GFDSUP1-20 IN YARD TRACK 112 DUE TO FAILURE TO COMPLY WITH RESTRICTED SPEED. RESULTED IN EQUIPMENT DAMAGES. NO HAZARDOUS MATERIALS WERE RELEASED .,False,False,True,False,False,0.0
525,19,3,BNSF,30,EDGAR,CARBON,H-LAUDEN1-17 IMPACTED A DRAWBAR THAT HAD FELL FROM ANOTHER TRAIN AND WAS FOULING SINGLE MAIN TRACK. THE IMPACT PUNCTURED THE FUEL TANK OF A LOCOMOTIVE RESULTING IN APPROXIMATELY 500 GALLONS OF DIESEL FUEL RELEASED.,False,False,True,False,False,0.0
526,19,2,UP,31,FREMONT,DODGE,"MALNPX-03, LEAD LOCOMOTIVE UP8056, DERAILED 12 CARS AT APPROXIMATELY MP 366.11.",False,True,False,False,False,0.0
527,19,8,ATK,29,MINERAL POINT,WASHINGTON,"TRAIN 22(18) WITH E/58 AND 8 CARS STRUCK A DUMP TRUCK AT A PRIVATE CROSSING. THE TRUCK WAS STOPPED ON THE CROSSING, THEN ATTEMPTED TO BACK OUT OF THE CROSSING WEN IT WAS STRUCK BY THE TRAIN. THE TRA IN WAS ABLE TO PROCEED WEST.",True,False,False,False,False,0.0
528,19,7,UP,29,KANSAS CITY,JACKSON,"THE YKC09R-25 HAD A TOTAL OF 112 CARS COMING TO THE HILL AT NEFF. TRAIN SHOVED UP TO THE HUMP AND BE GAN HUMPING OPERATIONS AND ONCE THEY WERE DOWN TO 27 CARS LEFT TO HUMP, CARS WERE DERAILED ON THE SO UTH AND NORTH LEAD OF THE HUMP AT NEFF. IT WAS LATER DETERMINED THE CARS ORIGINALLY DERAILED AT THE WEST END OF 206 NEAR A FROG AND GUARDRAIL DUE TO DEVIATION FROM UNIFORM TOP OF RAIL PROFILE.",False,True,False,False,False,0.0
529,19,7,UP,29,MERCER,MERCER,"THE MBUFW-23 TRAVELING SOUTH ON THE TRENTON SUB AT 50MPH, DERAILED 69 LOADED SAND CARS AT MP 381. CA USE WAS DUE TO SOFT ROADBED.",False,True,False,False,False,0.0
530,19,7,MNA,29,INDEPENDENCE,JACKSON,"RECEIVED NOTIFICATION BY PASSING UP CREW COMING OUT OF KC THAT MNA 4081 WAS SMOKING BADLY AND FLAMES WERE SEEN. CREW STOPPED TRAIN AND EXTINGUISHED FIRE. CONTACTED MNA OPERATIONS & MECHANICAL THEN CON TINUED ON PLEASANT HILL UP INTERCHANGE TO MNA. UP TRACK DAMAGE: $165
10-08-19 REVISED BLOCK #S: 22, 23
01-06-2020 REVISED BLOCK #S: 16, 22, 26, 37, 50, 51
01-07-2020 REVISED BLOCK #S: 7, 12",False,False,True,False,True,165.0
531,19,7,NS,29,WENTZVILLE,ST CHARLES,NS TRAIN 285D704 PULLING DERAILED AXLES OF A CAR.,False,True,False,False,False,0.0
532,19,9,MNA,29,NEVADA,VERNON,"WHILE SHOVING A CUT OF CARS INTO TRACK 002 IN NEVADA YARD, REAR CAR PICKED SWITCH. TWO CARS DERAILED AND CLIPPED A CAR ON TRACK 001",False,True,False,False,False,0.0
533,19,9,MNA,29,NEVADA,VERNON,"WHILE SHOVING A CUT OF CARS INTO TRACK 002 IN NEVADA, REAR CAR PICKED SWITCH. TWO CARS DERAILED AND CLIPPED A CAR ON TRACK 001.",False,True,False,False,False,0.0
534,19,9,UP,29,KANSAS CITY,JACKSON,"THE YKC27R-13 HAD DOUBLED TRACK 102 TO 203 AND WAS SHOVING ON THE LEAD THROUGH 203 TO THE HILL TO HU MP. CREW HAD PROCESSED 10 CARS OVER THE HILL WHEN THEY REALIZED A DERAILMENT HAD OCCURRED. THE UP905 80 WAS THE FIRST CAR TO DERAIL, WHICH JUMPED THE 102 GUARD RAIL, CAUSING THE SIX CARS IN THE CUT TO ACCORDION, AND CAUSE SUBSTANTIAL TRACK DAMAGE. THERE WAS TWO CARS DAMAGED IN ADJACENT TRACK 101 AND ALSO TO 4 RAILCARS THAT WERE IN TRACK 114 AT THE TIME.",False,True,False,False,True,0.0
535,19,7,BNSF,29,ST LOUIS,ST LOUIS CITY,RCO Y-STL2232-20 DERAILED 3 RAILCARS WHILE SHOVING YARD TRACK 910 DUE TO DRAGGING RAILCAR RIGGING GE TTING CAUGHT UP IN THE SWITCH POINT. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
536,19,3,UP,29,JAMESPORT,LIVINGSTON,"MAINTENANCE OF WAY WAS INSTRUCTED TO DUMP THE AIR ON DUMP ROCK CARS AT COBURN SO THEY COULD BE SCRAP ED. DUE TO FROZEN MATERIAL IN THE CAR CAUSED BY WINTER WEATHER, INSTEAD OF THE MATERIAL DUMPING FRO M THE CAR, IT TIPPED THE ENTIRE CAR OVER AND OFF THE RAIL. NO TRACK DAMAGE.",False,False,True,False,False,0.0
537,19,3,UP,29,KANSAS CITY,JACKSON,THE MKCEW-17 WAS PULLING EAST OUT OF NEFF YARD WHEN THE LEADING WHEEL OF CAR TTGX993516 DROPPED INSI DE THE NORTH RAIL IN TRACK 305 AND WAS DRAGGED AN ADDITIONAL 768 FEET. THIS CAUSED THE NORTH RAIL T O ROLL AND THE FOLLOWING 11 CARS TO RIDE INSIDE THE WEB OF THE RAIL. NO INJURIES AND NO HAZMAT RELE ASED.,False,False,True,False,False,0.0
538,19,2,UP,29,INDEPENDENCE,JACKSON,"CNAIM9-20, SECOND LOCOMOTIVE UP7283 WAS ON FIRE NEAR MP 273 ON THE RIVER SUB IN INDEPENDENCE, MO. N O DERAILMENT OR TRACK DAMAGE.",False,True,False,False,True,0.0
539,19,5,BNSF,38,WHITE EARTH,MOUNTRAIL,"M MINMIN1-03 WAS TRAVELING WESTWARD ON MT1, GLASGOW SUB, HIT TRACTOR-TRAILER AT GRADE CROSSING LOCAT ED AT MP 68.1. IMPACT WAS TO TRAILER WHICH WAS HAULING WATER. IMPACT TO LOADED TRAILER CAUSED DERAIL MENT TO LEAD 3 LOCOMOTIVES AND 16 CARS.",False,True,False,False,False,0.0
540,19,5,BNSF,38,STEELE,KIDDER,C-SCMSUD0-76 DERAILED 1 RAILCAR WHILE TRAVERSING SINGLE MAIN TRACK DUE TO A DEFECTIVE DRAFT GEAR ON A RAILCAR. NO HAZARDOUS MATERIALS WERE RELEASED. 7/11/19 NUMBER OF CARS 241 WAS VERIFIED BY THE RAI LROAD.,False,True,False,False,False,0.0
541,19,9,BNSF,27,KEEWATIN,ITASCA,U-KEESUP4-15 DERAILED 1 LOCOMOTIVE AND THREE RAILCARS ON BNSF MAINTAINED INDUSTRY TRACK DUE TO MISSI NG TIES. NO HAZMAT RELEASED.,False,True,False,False,False,0.0
542,19,3,CP,27,CARLOS,DOUGLAS,680-332 WAS TRAVELING EASTWARD ON THE DETROIT LAKES SUBDIVISION WHEN THE 20TH CAR TRAVERSED A BROKEN BOLT HOLE CAUSING 32 CARS TO DERAIL. TRAIN WAS TRAVELING IN 8 THROTTLE AT 32.9MPH AT THE TIME OF TH E DERAILMENT. LINE 25 (UCRY 5498) TO LINE 56 (PLCX 19124) DERAILED. TRAIN WAS OPERATING WITH DISTRIB UTIVE POWER WITH THE REMOTE LOCOMOTIVE ON THE REAR OF THE TRAIN. THERE WERE NO TRAIN HANDLING EXCEPT IONS NOTED. THE MAXIMUM SPEED AT THIS LOCATION IS 40MPH.,False,True,False,False,False,0.0
543,19,6,UP,27,MINNEAPOLIS,HENNEPIN,"CREW ON THE YSPBN-06, LITE ENGINE CONSIST, MOVING WESTWARD, FAILED TO STOP AT SIGNAL DISPLAYING STOP INDICATION - MP 9.7 - HARRISON STREET, RESULTING IN OCCUPYING MAIN TRACK WITHOUT AUTHORITY AND RUNN ING THRU DUAL CONTROL POWER SWITCH CAUSING DAMAGE TO SWITCH. NO DERAILMENT OR EQUIPMENT DAMAGE. BN SF REPORTED $21,700 IN TRACK DAMAGES.",False,False,True,False,True,21700.0
544,19,4,BNSF,27,FRIDLEY,ANOKA,RCO Y-NTW9002-15 DERAILED 8 RAILCARS DURING HUMP OPERATIONS IN YARD TRACK 1002 DUE TO TRACK BROKEN R AIL DETAIL FRACTURE. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
545,19,10,BNSF,27,DILWORTH,CLAY,"Y-DIL7512-09 DERAILED 1 LOCOMOTIVE WHILE OPERATING LIGHT POWER IN YARD TRACK 301. AFTER PULLING THRO UGH AN IMPROPERLY LINED SWITCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERI AL WAS RELEASED.",False,True,False,False,False,0.0
546,19,10,BNSF,27,ROSEVILLE,RAMSEY,Q-CHCSTP1-11 DERAILED 5 RAILCARS WHILE PULLING INTO YARD TRACK 7001 DUE TO A PREVIOUSLY RUN THROUGH SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
547,19,10,UP,27,ST PAUL,DAKOTA,LTB46-30 WAS SHOVING CARS INTO ORIGINATION AND DERAILED DUE TO WIDE GAUGE FROM BAD TIE CONDITIONS. THREE CARS DERAILED. INDUSTRY MAINTAINS TRACK,False,True,False,False,False,0.0
548,19,10,BNSF,27,FRIDLEY,ANOKA,RCO Y-NTW1002-25 DERAILED 1 RAILCAR DURING HUMP OPERATIONS IN YARD TRACK 2024 DUE TO PASSED COUPLERS AUTOMATED CLASSIFICATION YARD. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
549,19,1,ATK,26,THREE OAKS,BERRIEN,"TRAIN350 OPERATING WITH LOCOMOTIVES E/126-E/35 AND 5 CARS STRUCK A SEMI-TRACTOR TRAILER AT MP 211.88 , S. ELM STREET CROSSING. THE TRUCK WAS CAUGHT BETWEEN THE CROSSING GATES.",True,False,False,False,False,0.0
550,19,9,CRSH,26,RIVER ROUGE,WAYNE,FL97 WITH 2 UNITS AND 16 CARS SIDESWIPED CR 631490.,False,False,True,False,False,0.0
551,19,3,AA,26,MILAN,MONROE,"ANN ARBOR RAILROAD, HFI, DERAILMENT , ON 03/15/2019 AT APPROXIMATELY 0315 THE RS102 CREW: ENGINEER BEN COX (3YRS) AND CONDUCTOR RICKY DAVIS (1.5YRS) WITH THE WAMX 2373 AND WAMX 1337 WERE SETTING OUT 34 CARS IN MILAN YARD. AFTER CUTTING AWAY AND PULLING NORTH THE CONDUCTOR NOTICED SPARKS UNDER THE RAILCARS AND STOPPED THE MOVEMENT AND DISCOVERED THAT 3 LOADED TANK CARS (CRUDE OIL) HAD DERAILED A T THE CROSSOVER SWITCH. AT THIS POINT IT APPEARS THAT THE SOUTH SWITCH OF THE CROSSOVER WAS RUN THR U DURING THE SET OUT WHICH RESULTED IN THE DERAILMENT WHEN THE CARS WERE PULLED BACK NORTH. FURTHER INVESTIGATION REVEALED THAT THE CONDUCTOR DID NOT PROPERLY LINE THE SOUTH SWITCH OF THE CROSSOVER W HEN SHOVING CARS FROM THE MAINLINE INTO MILAN YARD #4 TRACK. THE SWITCH IN QUESTION WAS FOUND TO BE LINED AND LOCKED FOR OTHER THAN CROSSOVER MOVEMENT WITH A DERAILED RAILCAR ON THE GROUND AND WITHIN THE GAUGE OF THE SWITCH.",False,True,False,False,False,0.0
552,19,1,CRSH,26,RIVER ROUGE,WAYNE,FL42 DERAILED CARS DUE TO WIDE GAUGE.,False,True,False,False,False,0.0
553,19,1,NS,26,DETROIT,WAYNE,"BD60 OPERATING WITH REMOTE UNIT 5212 PULLING EAST OUT OF CLASS TRACK 1 ONTO THE 3RD RAIL WITH 41 EMP TY MULTILEVELS WHEN THE TRAIL TRUCK OF THE 8TH CAR CTTX 694514 FROM REAR OF 41 EMPTY MULTILEVELS ROL LED OUT LOW RAIL IN A 9DEGREE RETURN CURVE, ACCOUNNT POSSIBLE CENTERBOWL RIM CONTACT AND OTHER TRUCK TURNING RESISTANCES FORCING WHEELS AGAINST THE SOUTH/LOW RAIL WHERE TRACK PROFILE REDUCED VERTICAL WHEEL LOADS AND TIE STRENGTH WAS POOR RESULTING IN DERAILING THE REAR EIGHT CARS.",False,True,False,False,False,0.0
554,19,5,HESR,26,DURAND,SHIAWASSEE,HESR 767-29 SWITCHING AT THE WEST END OF THE WEST YARD SHOVING 21 CARS INTO WEST 5 DERAILED 9 CARS B Y THE SHORTBELT.,False,True,False,False,False,0.0
555,19,3,UP,17,MELROSE PARK,COOK,"FOUR CARS IN TRACK 18 ROLLED OUT, THE LUHX1096, UTCX48872, ACFX40511, AND UTCX50399, ALL POLICIES AN D PROCEDURES WERE FOLLOWED, POST CARS FAILED TO HOLD THE TRACK. TWO CARS IN ADJACENT TRACK 17 HAD P REVIOUSLY ROLLED OUT, THE MBLX53245 AND ECUX882134 AND WERE STRUCK BY THE CARS FROM TRACK 18.",True,False,False,False,False,0.0
556,19,3,UP,17,BELVIDERE,BOONE,CREW ON THE YBE52X-11 WAS HEADING BACK OVER TO CHRYSLER WITH 51 EMPTIES BECAUSE THEY HAD JUST PULLED LOADS FOR OUTBOUND TRAIN ABEHI. THEY WERE SHOVING AROUND CURVE GOING INTO CHRYSLER AND WERE LINED FOR TRACK 765. CONDUCTOR WAS SHOVING AND NOTICED THE DERAIL APPROXIMATELY 5-6 CARS DEEP IN THE TRAC K HAD SOMEHOW BEEN PLACED IN DERAILING POSITION. CONDUCTOR IMMEDIATELY TOLD ENGINEER TO STOP. THEY THEN WENT TO CUT AWAY AND MOVED ABOUT 2 AUTO RACKS WHEN THE ENGINEER SAID HE WAS HAVING ISSUES PULL ING. THEY STOPPED THE MOVEMENT AND THE CONDUCTOR WALKED UP TO FIND THEY WERE ON THE GROUND.,False,True,False,False,False,0.0
557,19,3,UP,17,WEST CHICAGO,DU PAGE,LPJ02-12 WAS IN THE PROCESS OF BULIDING THEIR TRAIN ON TRACK 414. CONDUCTOR FOUND 7 CARS DERAILED I N TRACK 414. CAUSE OF DERAILMENT WAS BROKEN RAIL FOUND BETWEEN THE 6TH AND 7TH CAR.,False,True,False,False,False,0.0
558,19,3,UP,17,BERKELEY,COOK,YG206-14 RAN THRU 6 MAIN CROSSOVER SWITCH AND DERAILED UP6637 DURING A BACKUP MOVEMENT.,False,True,False,False,False,0.0
559,19,8,NS,18,NEW HAVEN,ALLEN,"NS TRAIN L90L626 HEADING WEST THROUGH WEST END NEW CROSSOVER SWITCH AND DERAILED LEAD UNIT NS 3235, DUE TO WORN SWITCH POINT.",False,True,False,False,False,0.0
560,19,7,NS,18,ELKHART,ELKHART,DEBRIS IN THE FLANGEWAY FROM THE BRAKE RIGGING ON NDYX 849070 CAUSED THE RAILCAR TO DERAIL.,False,True,False,False,False,0.0
561,19,6,NS,18,ODELL,FOUNTAIN,"34ZD1.22 STRUCK LARGE TREE MP D270. ENGINE NS 7664 DAMAGE TO HEADLIGHTS, DITCH LIGHT AND HORN.",True,False,False,False,True,0.0
562,19,10,CSX,18,RENSSELAER,JASPER,J77325 STRUCK AN OCCUPIED SEMI-TRUCK AT CROSSING. PROTECTION ALSO AT CROSSING: ADVANCE WARNING.,True,False,False,False,False,0.0
563,19,11,CSX,18,MCCORDSVILLE,HANCOCK,SEMI TRUCK WAS STUCK ON THE TRACKS PRIOR TO GATES COMING DOWN AND WAS STRUCK BY Q21702. AGE UNKNOWN. PROTECTION ALSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS (STOP LINES & RR XING SYMBOLS).,True,False,False,False,False,0.0
564,19,2,CSX,18,BROWNSBURG,HENDRICKS,P05023 COLLIDED WITH PICKUP THAT WENT AROUND GATE ARMS. AMTRAK REPORTS $45K IN DAMAGES. PROTECTION A LSO AT CROSSING: ADVANCE WARNING AND PAVEMENT MARKINGS (STOP LINES & RR XING SYMBOLS).,False,False,True,False,False,45000.0
565,19,2,CSX,18,INDIANAPOLIS,MARION,UNKNOWN HUMP LOCOMOTIVE PULLED INTO 48 AND 49 CLASS TRACK CARS AND SHOVED INTO 50 CLASS AND COUPLED. THE LOCOMOTIVE MADE FOUR FORWARD AND BACKWARDS MOVEMENTS. AT THE END OF THE LAST MOVEMENT A CAR DER AILED. THEN AS THE LOCOMOTIVE PULLED WEST ANOTHER CAR DERAILED.,False,True,False,False,False,0.0
566,19,4,WC,17,CHICAGO HTS,COOK,"AT APPROXIMATELY 2023 CDT ON APRIL 2ND TRAIN A40891-02 (69L, 45E, 9R, 10398T, 7505F) WENT INTO EMERG ENCY ON MAIN ONE AT MILE 25.2 ON THE MATTESON SUBDIVISION (CHICAGO HEIGHTS). AT 2123 CDT TRAIN A4919 1-02 (64L, 120E, 9R, 11537T, 9396F) REPORTED THAT THE TAIL END CAR FROM A408, LOADED SHEET METAL CAR CN 187092, HAD ROLLED INTO THEIR LEAD MOTOR (UP 4646). ENGINEER AND CONDUCTOR WERE TRANSPORTED BY A MBULANCE TO ST MARY HOSPITAL WITH MINOR INJURIES. NO DERAILMENT AND NO DANGEROUS GOODS INVOLVED. CAU SE IS UNDER INVESTIGATION.",False,False,True,False,False,0.0
567,19,2,IR,17,OREGON,OGLE,99 CARS SECURED ON THE MT MORRIS BRANCH ROLLED DOWN HILL DERAILING WHEN THEY HIT A DERAIL IN PLACE F OR PROTECTION. CARS WERE ESTIMATED TO BE MOVING AT 15MPH AT THE TIME OF DERAILING. CAUSE WAS DETURMI NED TO BE UNINTENDED MOVEMENT DUE TO TRESPASSER VANDALISM.,False,True,False,False,False,0.0
568,19,5,TRRA,17,EAST ST LOUIS,ST CLAIR,THE EXTREME CURVATURE OF THE DIAMOND COMBINED WITH DIFFERENTIAL DEFLECTION OF THE MORE FLEXIBLE RAIL JOINT IN CLOSE PROXIMITY TO THE OPPOSITE PART OF THE WHEEL AXLE LOADING THE MUCH STIFFER FROG PORTI ON OF THE DIAMOND IN POOR DRAINAGE AND MUDDY CONDITIONS LIKELY WAS THE PRIMARY CONTRIBUTING CAUSE TO THE WHEEL LIFT OF THE EMPTY CAR.,False,False,True,False,False,0.0
569,19,6,BRC,17,BEDFORD PARK,COOK,AT 06:23 ON 6/15/19 THE OUTBOUND NS 34G-15 DERAILED ON TRACK 34 EAST DEPT. THE CREW WAS IN THE PROCE SS OF PULLING OUT OF 34 EAST DEPT. WHEN THE CONDUCTOR NOTICED THE CARS ROCKING FROM SIDE TO SIDE AND CALLED OUT EMERGENCY TO THE ENGINEER ON THE ASSIGNMENT. BY THE TIME THE ENGINEER WAS ABLE TO STOP T HE TRAIN THE # 61 CAR IN THE TRAIN GFSX 510010 AND THE # 62 CAR IN THE TRAIN ECNX 165222 HAD DERAILE D. BOTH CARS WERE EMPTY HOPPERS. MTO BILLINGSLY WAS IMMEDIATELY NOTIFIED. CAR FOREMAN SIPPLE AND M O F WAY FOREMAN BALICH WERE ON LOCATION TO ACCESS THE DAMAGE TO CARS AND RAIL. IT WAS DETERMINED THAT THE NDYX 829007 IN THE THE # 59 POSITION IN THE TRAIN HAD LOST THE FRONT HOPPER DOOR RELEASE RATCHET ROD FROM THE CAR. THIS PIECE OF HARDWARE IS APPROX. 40 INCHES IN LENGTH AND HANGS UNDER THE HOPPER DOOR AND PROVIDES MOVEMENT TO OPEN THE LOWER COMPARTMENT. IT HAS A VERY STURDY CONSTRUCTION MADE OF SOLID STEEL. THIS PIECE FELL OFF THE NDYX 829007 AND FELL IN THE OPEN SIDE OF THE 34 EAST DEPT. SWIT CH CAUSING THE INITIAL POINT OF DERAILMENT.,False,True,False,False,True,0.0
570,19,4,ALS,17,EAST ST LOUIS,ST CLAIR,MYCAS-29 WAS PULLING INTO RECEIVING YARD AND DERAILED IN THE INBOUND POCKET,False,True,False,False,False,0.0
571,19,6,BRC,17,BEDFORD PARK,COOK,"AT 1240 ON JUNE 9TH 2019 THE 0759 EH WAS SHOVING WEST UP 3 EAST APPROACH AND COLLIDED AT THE TOP OF THE HUMP WITH THE 0630 EAST HUMP ASSIGNMENT WHO WAS IN THE PROCESS OF HUMPING WESTWARD OFF OF 01EAPR . NO ONE WAS INJURED FROM THIS INCIDENT HOWEVER THERE WAS A TOTAL OF FOURTEEN CARS DAMAGED OF WHICH 10 OF THE CARS WERE DERAILED OF THE DERAILED CARS SIX OF THEM WERE ON THEIR SIDE JUST TO THE NORTH O F THE EAST HUMP LEADS AT THE TOP OF THE HUMP. MOST OF THE DAMAGED EQUIPMENT WERE TANK CARS IN WHICH TWO OF THEM CLASS 9 HAZARDOUS HOWEVER THERE WAS NO PRODUCT THAT WAS EXPOSED FROM THE DAMAGE. ALL EMP LOYEES WERE CLEARED OF THE AREA AND THE HAZARDOUS MATERIAL TEAM WERE CALLED OUT AS A PRECAUTIONARY, AND A THOROUGH INSPECTION OF THE DAMAGED EQUIPMENT WAS PERFORMED. HULCHER WAS CALLED OUT TOCLEAN UP AND RERAIL DAMAGED CARS.",False,True,False,True,True,0.0
572,19,5,IR,17,OTTAWA,LA SALLE,SEMI TRUCK AND TRAILER TRAVELING NORTH ON BOYCE MEMORIAL DRIVE FAILED TO YIELD TO ONCOMING LOCOMOTIV ES TRAVELING WESTBOUND ON US SILICA LEAD TRACK. CROSSING LIGHTS AND BELL WERE ACTIVATED AND WORKING. ENGINEER WAS SOUNDING HORN AND BELL RINGING ON LOCOMOTIVE. DRIVE OF SEMI TRUCK WAS CITED BY POLICE FOR FAILURE TO YIELD.,False,False,True,False,False,0.0
573,19,4,BNSF,17,ELWOOD,WILL,RCO Y-LPC1052-17 DERAILED 2 RAILCARS WHILE SHOVING YARD TRACK 4345 DUE TO BUFFING ACTION BECAUSE OF TRAIN MAKEUP - LOADS AND EMPTIES CONFIGURATIONS. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
574,19,7,CSX,18,INDIANAPOLIS,MARION,Y29410 WAS SHOVING OFF A CUT INTO D06 IN A WEST DIRECTION WHEN THE Y29310 CAME OUT OF D02 IN AN EAST DIRECTION AND STRUCK THE Y29410 SIDE-SWIPING A CAR AND THE WEST ENGINE OUT OF AN EAST/WEST CONSIST.,True,False,False,False,False,0.0
575,19,6,CSX,18,INDIANAPOLIS,MARION,"WHILE Y392-08 WAS PULLING OUT OF 004 CLASS, 003 CLASS ROLLED OUT AND SIDESWIPED 004 CLASS AFTER JUMP ING AND KNOCKING THE SKATES OFF OF 003 CLASS.",False,False,True,False,False,0.0
576,19,6,UP,19,STANWOOD,CEDAR,"CBTOK-03 WAS OPERATING ON CLEAR WAYSIDE SIGNALS WHEN IT ENCOUNTERED AN IMPROPERLY LINED SWITCH WHICH WAS LINED BY ENGINEERING EMPLOYEE, CAUSING TO DERAIL 2 LOCOMOTIVES AND 35 LOADED COAL CARS.",False,True,False,False,False,0.0
577,19,4,CSX,18,INDIANAPOLIS,MARION,Y29311 PULLER JOB COUPLING 21 CARS IN BOWL TRACK 004. NORMAL HUMP OPERATIONS CONTINUED WITH 3 2-CAR CUTS INTO BOWL 003 TRACK. 003 BOWL TRACK ROLLED EAST 63 FT. AFTER FIRST 2-CAR CUT COUPLED INTO TRACK 003. INVESTIGATION REVEALED THE NORTHSIDE TRACK SKATE FELL OFF NORTHSIDE RAIL DUE TO DEFECTIVE INSI DE RAIL GUIDE BROKEN ON WESTERN CULLEN HAYES FRICTION RAILSKATE. INVESTIGATION ALSO DISCOVERED SKID MARKS ON TOP OF THE RAIL UP TO LOCATION THE SKATE FELL OFF RAIL. BOWL TRACK 003 MOVED ADDITIONAL 10 FT. AFTER SECOND 2-CAR CUT AND ANOTHER 10 FT. AFTER THE LAST 2-CAR CUT WAS HUMPED. INVESTIGATION DET ERMINED THAT THE CARS WERE NOW IN THE FOUL. Y29311 PULLS EAST WHILE OPERATING IN ACTIVE REMOTE CONTR OL ZONE CONTROLLED BY Y29311 FOREMAN SIDE SWIPING AND DERAILING GATX 213599 EAST CAR IN BOWL TRACK 0 3,False,True,False,False,False,0.0
578,19,1,ATK,18,GARY,LAKE,"TRAIN 365 OPERATING WITH LOCOMOTIVE E/29, 6 CARS AND LOCOMOTIVE E/28 TRAILING STRUCK AN OCCUPIED TRA CTOR-TRAILER TRUCK AT NORTH CLARK RD CROSSING.",True,False,False,False,False,0.0
579,19,12,FCR,13,ATLANTA,FULTON,WHILE SHOVING SOUTH THE 13TH CAR (ARMN 170112) DERAILED. WHEN WHEEL FOLLOWED THE DIVERGING TRACK OF A TURNOUT IT DERAILED THE 12TH AND 14TH CAR. THE DERAILMENT WAS CAUSED BY SEVERE TREAD DAMAGE ON THE L1 WHEEL.,False,True,False,False,True,0.0
580,19,12,NS,13,MILLEN,JENKINS,"NS TRAIN 192G5219 WAS PULLING NORTH ON THE WEST LEAD WYE, WHEN THEY DERAILED 7 CARS AS A RESULT OF T HE ENGINEER NOT CONTROLLING THE MOVEMENT.",False,True,False,False,False,0.0
581,19,12,TSWS,5,MARION,CRITTENDEN,"THE EAST END CREW J1, WERE PULLING THE ZLAME 13 OUT OF 701 TO SHOVE 408. THEY HAD 20 CARS AND 4 LOCO S IN THE CONSIST. WHILE WALKER WILLIAMS WAS CLEARING THE EAST 700 HE NOTICED THE CARS WERE COMING OF F OF THE RAIL AND IMMEDIATELY TOLD MATTHEW WOLF,THE ENGINEER TO PUT IT IN EMERGENCY. WHEN THE MOVEM ENT STOPPED IS WHEN THE YARDMASTER COULD SEE WE HAD THREE CARS ON THE GROUND. AFTER FURTHER INSPECTI ON THE CAUSE OF THE DERAILMENT WAS DUE TO A WIDE GAUGE EAST OF THE EAST 700 SWITCH.",False,True,False,False,False,0.0
582,19,3,HESR,26,AKRON,TUSCOLA,CREW WAS SPOTTING 28 EMPTIES TO AKRON CO-OP WHEN THEY DERAILED 4 CARS IN THEIR TRAIN ON THE EAST END DERAIL THAT WAS FAILED TO BE REMOVED BEFORE TRAVERSING THE TRACK.,False,True,False,False,False,0.0
583,19,7,KRR,5,HOPE,HEMPSTEAD,L-AS101 WAS PULLING 22 LOADS TOWARDS HOPE WHEN ENGINEER FELT TUG AND TRAIN WENT INTO EMERGENCY. AFTE R INSPECTION TRAIN CREW FOUND FOUR CARS DERAILED WITH THREE CARS LAYING ON THEIR SIDE.,False,True,False,False,False,0.0
584,19,10,KRR,5,ASHDOWN,LITTLE RIVER,JOB 101 WAS PULLING THROUGH GREENWOOD YARD EASTBOUND WITH 84 CARS. THE 33RD AND 34TH RAILCARS (EMPT Y COVERED HOPPERS) DERAILED.,False,True,False,False,False,0.0
585,19,4,BNSF,5,JONESBORO,CRAIGHEAD,C-EBMMHS0-51 DERAILED 1 RAILCAR AND CAUSED SIGNIFICANT TRACK DAMAGES WHILE TRAVERSING SINGLE MAIN TR ACK DUE TO A BROKEN RIM ON A RAILCAR. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
586,19,5,UP,5,NORTH LITTLE ROCK,PULASKI,"CAR DEPARTMENT FOUND DAMAGE ON 2 CARS IN OUTBOUND TRACK 306. UPON INVESTIGATION IT WAS DISCOVERED T HESE CARS CAME OUT OF BOWL 29 AND HAD BEEN INVOLVED IN A HIGHER SPEED COUPLING ACCOUNT OF HEAVY WHEE L CONTAMINATION ON ALL THE WHEELS. CARS CAME OUT OF RICELAND FLOODS AT STUTTGART, AR AND WERE CONTA MINATED PREVIOUSLY BEFORE GOING OVER THE AUTOMATED HUMP FACILITY ALLOWING A HIGHER SPEED COUPLING. NO DERAILMENT OCCURRED.",False,False,True,False,True,0.0
587,19,5,UP,5,PINE BLUFF,JEFFERSON,"TRAIN YPB35R-11 UNKNOWINGLY RAN THROUGH 3 RAIL POCKET SWITCH SHOVING 39 CARS INTO 202. AS THE TRAIN WAS COMING BACK NORTH WITH LIGHT POWER, IT DERAILED ON THE SWITCH.",False,True,False,False,False,0.0
588,19,2,UP,5,NORTH LITTLE ROCK,PULASKI,THE YNL39R-24 RAN THROUGH A SWITCH AND DERAILED 2 ENGINES JUST SOUTH OF CP342 ON THE SOUTH END OF TH E YARD.,False,True,False,False,False,0.0
589,19,1,UP,5,MCGEHEE,DESHA,PLOW OPERATOR THOUGHT THAT HIS WING WAS LIFTED ALL THE WAY UP. WING CLIPPED THE DUAL OPERATING SIGN AL BOX ON THE GROUND.,False,False,True,False,False,0.0
590,19,1,UP,5,NORTH LITTLE ROCK,PULASKI,"DURING HUMPING OPERATIONS, 2 CARS DERAILED JUST NORTH OF THE GROUP 6 RETARDER. IT WAS DISCOVERED TH AT THE TCMX450618 WAS HUMPED AND ROUTED TO BOWL 24 AND RIGHT BEHIND IT CARS UP94745 AND SSW91087. T HE TCMX450618 CLEARED INTO BOWL 24 AND THE UP94745/SSW91087 WAS HEADING FOR BOWL 18 RIGHT AFTER IT. THE NORTH TRUCKS OF THE UP94745 WENT DOWN TRACK 24 AND THE SWITCH LINED UNDERNEATH IT, SENDING THE SOUTH TRUCKS OF THE UP94745 AND NORTH TRUCKS OF THE SSW91087, CAUSING THE SOUTH TRUCKS OF THE UP9474 5 AND THE NORTH TRUCKS OF THE SSW91087 TO DERAIL.",False,True,False,False,False,0.0
591,19,3,ATK,6,CARPINTERIA,SANTA BARBARA,"TRAIN 759 WITH ENGINE UNIT C2114, STRUCK A TREE AT MP 373.9 NORTH OF CARPINTERIA.",True,False,False,False,False,0.0
592,19,3,ATK,6,OAKLAND,ALAMEDA,"TRAIN 535, IN DEADHEAD MOVE, OPERATING WITH CAMERA-EQUIPPED CAB CAR 6962 IN THE LEAD, 4 CARS AND LOC OMOTIVE E/2104 IN PUSH MODE, STRUCK AN OCCUPIED PICK-UP TRUCK THAT WAS TRAPPED ON THE CROSSING BY TR AFFIC AT MP 9.5, 29TH AVENUE CROSSING.",True,False,False,False,False,0.0
593,19,9,CSX,1,BIRMINGHAM,JEFFERSON,"Y29703 BEGAN TO SWITCH A 50 CAR CUT AT THE NORTH END OF THE RECEIVING YARD. THE JOB SHOVED TOWARD R0 8 WITH THE CUT OF 50 CARS. 29 CARS WERE SHOVED OVER THE SWITCH BEFORE DERAILING LINES 30,31,32, AND 33. AFTER INVESTIGATION IT WAS DETERMINED THAT THE R04 POWER SWITCH GAPPED CAUSING THE CARS TO DERAI L.",False,True,False,False,False,0.0
594,19,7,NS,1,IRONDALE,JEFFERSON,SHOP WAS MAKING A SHOVE MOVE OUT OF SHOP TRAK #5 IN ORDER TO MOVE THE NS 8122 TO ANOTHER TRACK. SHOP CREW FAILED TO CHECK THERE ROUTE AND RAN OVER THE DERAIL IN SHOP TRACK #5 CAUSING THREE WHEELS OF T HE CAB TO COME OFF.,False,True,False,False,False,0.0
595,19,4,NS,1,IRONDALE,JEFFERSON,"AB41 WAS SHOVING WITH 14 CARS, 1200 TONS THROUGH WEST PULLBACK TO DERAILED CAR NS 300381 NEAR THE 5 CROSSOVER.",False,True,False,False,False,0.0
596,19,9,TASD,1,MOBILE,MOBILE,AGR YARD JOB TRAVELING SOUTH THROUGH TASD INTERCHANGE T27 WHEN LEAD ENGINE(BNFX-603) ALONG WITH 2 TR AILING (BNFX-4574 & AGR-3360) ENGINES DERAILED AT THE NORTH END OF T27 IN THE FROG OF THE TRACK.,False,True,False,False,False,0.0
597,19,7,CSX,1,BRUNDIDGE,PIKE,A72312 STRUCK A TRUCK THAT FAILED TO STOP AT CROSSING THERE WERE NO INJURIES. MOTORIST AGE UNKNOWN .,True,False,False,False,False,0.0
598,19,6,NS,1,MOBILE,MOBILE,"**** CANADIAN NATIONAL TRAIN **** A94A411 GIVEN PERMISSION TO ENTER REMOTE ZONE. CN RCL 95871 FAILED TO COVER CAR PULLED BACK AFTER PERMISSION GRANTED, TRIED TO STOP MOVE. RESULTED IN CN RUNNING INTO THE SIDE OF A94 DERAILING FOUR CARS GATX 89756,CTCX 727206, GATX 89588, TIIX 251699 (B END).",False,True,False,False,False,0.0
599,19,8,BNSF,1,DORA,WALKER,S-ATGSOC1-11 STRUCK A LOW HANGING TELEPHONE WIRE THAT OBSTRUCTED PATH OF TRAVEL WHILE TRAVERSING SIN GLE MAIN TRACK. RESULTED IN DAMAGES TO A SIGNAL MAST AT A HIGHWAY GRADE CROSSING. NO HAZARDOUS MATER IALS WERE RELEASED.,True,False,False,False,False,0.0
600,19,5,CSX,1,BIRMINGHAM,JEFFERSON,"N24025 DERAILED 7 CARS AT MILE POST 000393.7. TRAIN N24025 WAS PULLING SOUTHBOUND INTO ALICE YARD T RACK 1 TO STAGE FOR A LATER DEPARTURE. AS N240 WAS PULLING THRU YARD ABOUT 60 TO 70 CAR LENGTHS INT O MOVE THE TRAIN STOPPED ABRUPTLY. CONDUCTOR WALKED AND FOUND CAR 45 -51DERAILED OF 103 CARS. CARS DERAILED `CSXT 377703, CSXT 377818, CSXT 400154, CSXT 376531, CSXT 399930, CSXT 377712, & CSXT 3776 96. N240 HAD 2 LOCOMOTIVES, 13,802 TONS. MAIN #1 BLOCKED ALL TRAFFIC HAD TO ROUTE ON MAIN #2. NS DIAMOND WAS BLOCKED ABOUT 2 HOURS. 96 CARS OF THE 103 CARS WHERE COUPLED TOGETHER AND DEPARTED AS N23925 AROUND 0100.",False,True,False,False,False,0.0
601,19,5,NS,1,WOODVILLE,JACKSON,736AA05 WAS PULLING NORTH THE MAINLINE. CARS BEGAN TO DERAIL DUE TO BROKEN RAIL.,False,True,False,False,False,0.0
602,19,9,NS,1,KIMBROUGH,WILCOX,NS TRAIN A14A403 WAS SHOVING ON ALABAMA & GULF COAST RAILWAY TRACK AND DERAILED 6 CARS AND WENT INTO EMERGENCY.,False,True,False,False,False,0.0
603,19,7,NS,1,IRONDALE,JEFFERSON,"AB01 HUMPING IN AUTOMATIC MODE FROM RT06 WHEN LINE 95 TEIX 25114, STALLED IN THE G ROUP RETARDER, RE SULTING IN FOLLOWING CAR, LINE 94 TEIX 25101, CATCHING UP AND COUPLING TO TEIX 25114 IN THE RETARDER WHILE STILL FOULING THE F GROUP LEAD. THE LAST CAAR CUT, LINE 93 UTLX 640613 DESTINED FOR CT 12, MI SROUTED TOWARD THE F GROUP, RESULTING IN A CORNERING WITH TEIX 25101 DERAILING THE A END OF BOTH CAR S.",False,True,False,False,False,0.0
604,19,7,AGR,1,FOUNTAIN,MONROE,"AGR 31 WAS SWITCHING OUTBOUND TRAIN IN #2 TRACK IN GP MILL YARD. CREW PULLED 31 CARS DOWN TO CUT AND CUT REAR CAR OFF. CREW WENT AHEAD TO CLEAR LEAD SWITCH. TRAIN WENT INTO EMERGENCY. UPON INVESTIGATI NG, FOUND DERAILED CAR ABOUT 1500 FT FROM WHERE PREVIOUS CUT WAS MADE",False,True,False,False,False,0.0
605,19,5,TASD,1,MOBILE,MOBILE,"TASD 2 SHOVING CARS TO SPOT FOR CUSTOMER AT ZENITH. ENGINEER FAILED TO OPERATE AT RESTRICTED SPEED AND SHOVED THROUGH END BLOCK AFTER FAILING TO HEAR CONDUCTOR'S INSTRUCTIONS TO STOP. ENGINEER SHOVED FURTHER THAN HALF THE DISTANCE OF THE LAST COMMUNICATED CLEARANCE DISTANCE FROM CONDUCTOR, WHICH RE SULTED IN DERAILMENT OF PROX 76954 INTO WOODED AREA PASS THE END OF TRACK.",False,True,False,False,False,0.0
606,19,5,TASD,1,MOBILE,MOBILE,"TASD-MCD CREW WHILE IN THE PROCESS OF DUMPING APPROX. 35TH IN TRAIN, ENGINEER STOPPED SHOVING ANDASK ED CONDUCTOR TO CHECK END OF TRAIN FOR POSSIBLE DERAILMENT. CONDUCTOR DISCOVERED THAT DP ENGINE WAS ON THE GROUND /ALL WHEELS.",False,True,False,False,False,0.0
607,19,2,UP,4,TUCSON,PIMA,"YTU22R-06 WAS PULLING EAST OUT OF 22 TRACK WHEN THE HEAD AND WEB OF THE RAIL SEPARATED ON THE TURNOU T SIDE OF THE TRACK, CAUSING A 3 CAR DERAILMENT.",False,True,False,False,False,0.0
608,19,4,UP,4,TUCSON,PIMA,"YTU24R-29, IN AN ATTEMPT TO COUPLE THE UP4590 AND UP4509, THE DRAWBARS CROSSED CAUSING DAMAGE TO THE UP4590. NO DERAILMENT AND NO DAMAGE TO THE UP4509.",False,False,True,False,True,0.0
609,19,6,UP,4,TUCSON,PIMA,"WSBAZZ-14 WAS DEPARTING OUT OF CONTROLLED SIDING 1 HEADING WEST, 8 CARS IN THE CONSIST DERAILED DUE TO WIDE GAGE.",False,True,False,False,False,0.0
610,19,6,UP,4,TUCSON,PIMA,"WHILE THE CONDUCTOR WAS PROTECTING THE POINT OF THE LKP36-17, SHOVING INTO YARD 1, TRACK 802 AT SP30 6, THE AOK5297 WAS SHOVED OFF THE END OF THE TRACK.",False,False,True,False,False,0.0
611,19,10,BNSF,4,FLAGSTAFF,COCONINO,"TRAIN H TULBAR-1-11A DERAILING 14 CARS ON MAIN TRACK 01 AT MP 323.2 IN WINONA, AZ. CARS ARE FOULING MAIN TRACK 02 WITH NO ROUTE AROUND. 07 OF THE DERAILED CARS CONTAIN HAZMAT. NO HAZMAT RELEASED.",False,True,False,False,False,0.0
612,19,10,UP,4,TUCSON,PIMA,"MFWWCB-19 WAS SHOVING TOWARDS TRACK 52 WHEN THE TRAIN DERAILED SEVEN CARS AT THE HEAD END AND TWO LO COMOTIVES, AND IMPACTED A LOCOMOTIVE ON ADJACENT TRACK.",False,True,False,False,False,0.0
613,19,12,TPW,17,BARTONVILLE,PEORIA,"AFTER GETTING A TRACK WARRANT TO DEPART THE TZPR AND ENTER THE UP MAINLINE, THE TRAIN TRAVELED APPRO XIMATELY 85 CAR LENGTHS AND HAD GONE INTO EMERGENCY. UPON INSPECTION, THE REAR 2 LOCOMOTIVES HAD DE RAILED IN THE VICINITY OF MP 0.50 ON THE TZPR MAINLINE CAUSING THE LAST 2 COAL CARS OF THE TRAIN TO BREAK THE COUPLING AND SEPARATE FROM THE REST OF THE TRAIN. NO INJURIES WERE SUSTAINED.",False,False,True,False,False,0.0
614,19,9,TZPR,17,CREVE COEUR,TAZEWELL,"UNION PACIFIC WAS TRAVERSING A LOADED COAL TRAIN (133 X 0) WITH DP POWER CONFIGURATION ON THE TZPR I N AN EASTBOUND DIRECTION ON THE SOUTHERN DIVISION MAIN TRACK NEAR WESLEY JUNCTION WHEN THEIR TRAIN W ENT INTO EMERGENCY. THE UP CONDUCTOR WALKED THE TRAIN AND DISCOVERED A BROKEN KNUCKLE, REPLACED THE KNUCKLE, CHARGED THE TRAIN WITH AIR, AND ATTEMPTED TO MOVE THE TRAIN WITH NO SUCCESS. THE CONDUCTOR THEN WALKED THE REMAINDER OF THE TRAIN AND DISCOVERED CARS 120 THROUGH 123 WERE DERAILED, WITH CARS 121 AND 122 POSITIONED ON THEIR SIDE. THE DERAILMENT LOCATION WAS LOCATED AT THE DUAL CONTROL SWITC H FOR THE EAST LEAD ON THE TZPR, JUST EAST OF THE RIVER BRIDGE. DETAILED EQUIPMENT INSPECTION FOUND UNUSUAL WEAR PATTERNS ON THE CTRN 601091 R3 AND L4 WHEEL, AND UNUSUAL WEAR ON THE CONSTANT CONTACT T RUCK AND BODY SIDE BEARINGS. WEAR FOUND WAS NOT CONDEMNABLE, BUT BELIEVED TO HAVE LED TO INCIDENT.",False,True,False,False,False,0.0
615,19,12,TZPR,17,BARTONVILLE,PEORIA,"AFTER TPW CREW RECEIVED A TRACK WARRANT TO DEPART THE TZPR AND ENTER THE UP MAINLINE, THE TRAIN TRAV ELED APPROXIMATELY 85 CARS LENGTHS AND HAD GONE INTO EMERGENCY. UPON INSPECTION, THE REAR 2 LOCOMOT IVES HAD DERAILED IN THE VICINITY OF MP 0.50 ON THE TZPR MAINLINE CAUSING THE LAST 2 COAL CARS OF TH E TRAIN TO BREAK THE COUPLING AND SEPARATE FROM THE REST OF THE TRAIN.",False,True,False,False,False,0.0
616,19,1,CSX,18,CAYUGA,VERMILLION,1025/04 T08003 AFTER ARRIVING AT THE CAYUGA POWER PLANT WAS INSTRUCTED TO PLACE THEIR TRAIN IN TRACK 4. THE CONDUCTOR FAILED TO LINE THE SOUTH SWITCH OF THE SOUTH CROSSOVER BETWEEN TRACKS 4 AND 2. T HE INDUSTRY HAD LINED THE OPPOSITE SWITCH FOR STRAIGHT AWAY MOVEMENT AND LEFT A CUT OF CARS COVERING THE SWITCH. THE CONDUCTOR WAS THEN TRANSPORTED TO THE NORTH END OF TRACK 4 TO WAIT ON THE TRAIN TO ARRIVE IN ORDER TO CUT ENGINES AWAY. WHEN THE ENGINEER ARRIVED AT THE SOUTH END OF THE SOUTH CROSS OVER HE FAILED TO TAKE ANY ACTION TO STOP THE TRAIN AND TRAVELED AN ADDITIONAL 450 FEET STRIKING THE CUT OF CARS THAT WERE LEFT IN TRACK 2 CAUSING DERAILMENT OF CARS. IT IS UNKNOWN WHETHER THE POSITIV E DRUG RESULTS CAUSED THIS INCIDENT.,False,True,False,False,False,0.0
617,19,1,NS,18,ELKHART,ELKHART,"BE21 SHOVING WEST OFF OF RT07 AND OPERATING IN HUMP FAST 1.6 MPH DERAILED CARS OTTX97371 L1, L2, R1, R2, ITTX 970715 ALL WHEELS, ITTX 970672 ALL WEELS, SOU 160001 L1, L2, L3, L4. R3, R4, NS 171237 ALL WHEELS AND ITTX 942627 L1, L2, R1, R ACCOUNT OF BBUFF FORCES DURING NORMAL HUMPING OPERATIONS.",False,True,False,False,False,0.0
618,19,9,PGR,27,NORTHFIELD,RICE,"CP'S H38-21 DERAILED AT PGR'S NORTHFIELD YARD #3 SWITCH SHOVING SOUTH WITH THREE ENGINES, THE REAR 3 TRUCKS ON THE LEAD ENGINE PICKED THE SWITCH AND DERAILED. CP IS REPORTING $31,543.58 IN EQUIPMENT DAMAGE.",False,True,False,False,True,31543.58
619,19,3,BNSF,27,FRIDLEY,ANOKA,H-GFDNTW2-08 DERAILED 5 RAILCARS WHILE PULLING INTO YARD TRACK 1007 TO YARD THEIR TRAIN. NO HAZARDOU S MATERIALS WERE RELEASED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
620,19,3,CP,38,CARRINGTON,FOSTER,"498-27 WAS TRAVELING EASTWARD ON THE CARRINGTON SUBDIVISION WHEN THE 96TH CAR TRAVERSED A BROKEN BOL T HOLE CAUSING 35 CARS TO DERAIL. TRAIN WAS TRAVELING IN IDLE AT 49MPH AT THE TIME OF THE DERAILMENT . LINE 96 (CRYX 7084) TO LINE 130 (CGTX 64480) DERAILED. TRAIN WAS OPERATING WITH DISTRIBUTIVE POWER WITH THE REMOTE LOCOMOTIVE PLACED IN THE 56TH POSITION OF THE TRAIN. THERE WERE NO TRAIN HANDLING E XCEPTIONS NOTED. THE MAXIMUM SPEED OF THIS LOCATION IS 49MPH. DERAILMENT ALSO RESULTED IN 3 HAZARDOU S CARS RELEASING PRODUCT - PROX 93752 STCC 4905421, PROX 105499 STCC 4920359 & PROX 105275 STCC 4920 359. HAZMAT RELEASE NOT MEASURABLE. PRODUCT WAS FLARED. VAPOR LOSS ONLY.",False,True,False,True,False,0.0
621,19,8,BNSF,38,PISEK,WALSH,TWO REAR DP UNITS ON G-PKVKAL909H DERAILED AS THE TRAIN TRAVERSED OVER THE HANNAH SUBDIVISION ON SIN GLE MAIN TRACK. DERAILMENT OCCURRED DUE TO IRREGULAR TRACK ALIGNMENT.,False,True,False,False,False,0.0
622,19,12,BNSF,38,STANLEY,MOUNTRAIL,Z-CHCSSE9-23 DERAILED 1 LOCOMOTIVE WHILE TRAVERSING MAIN 2 TRACK DUE TO A BROKEN RIM ON THE LOCOMOTI VE. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
623,19,7,UP,31,MITCHELL,SCOTTS BLUFF,"CNACO-28 DOORS CAME OPEN ON RAILCAR CMO503956, DUMPING THE LOAD OF COAL. CMO503956 CLIMBED THE COAL AND DERAILED. CAR WAS DRAGGED EAST AND AT THE #13 SWITCH THE TRAIN WENT INTO EMERGENCY. 2 CARS DERAI LED.",False,True,False,False,False,0.0
624,19,7,UP,31,NORTH PLATTE,LINCOLN,YNP10R-30 WAS TAKING LIGHT POWER TO WEST BOWL 49 TO COUPLE FOR THE ANPRL-30 AND DERAILED THE LEADING 3 SETS OF TRUCKS ON THE UPY422. MARKS ON THE SWITCH POINT OF THE 49/50 SWITCH SHOWED THE WHEELS CLI MBED UP THE SWITCH POINTS CAUSING THE DERAILMENT WHEN MAKING THE FACING POINT MOVE INTO BOWL 49.,False,True,False,False,False,0.0
625,19,7,UP,31,NORTH PLATTE,LINCOLN,THE HELPER ON THE YNP44R-22 WAS TRIMMING THE MNPAH DOWN EAST DEPARTURES 5 TRACK. THE HELPER FAILED T O STOP HIS TRAIN IN THE CLEAR AND COLLIDED WITH THE MNPAL-22 THAT WAS DOUBLED UP ON THE DEPARTURE YA RD LEAD.,False,False,True,False,False,0.0
626,19,7,BNSF,31,AURORA,HAMILTON,R-PWR4311-02 HAD A CUT OF RAILCARS ROLL OUT OF YARD TRACK 2300 RESULTING IN 4 RAILCARS DERAILED DUE TO FAILURE TO APPLY SUFFICIENT NUMBER OF HANDBRAKES. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
627,19,1,NS,36,CHEEKTOWAGA,ERIE,"23KC922 SHOVING EAST WITH 2 UNITS, 0 LOADS, 0 EMPTIES, AND 0 TONS ON SOUTHERN TIER MAIN MADE A HARD COUPLING WITH THEIR TRAIN (31 LOADS, 2 EMPTIES, AND 3089 TONS), DAMAGING CAR DTTX 680548.",False,False,True,False,False,0.0
628,19,12,NS,36,OWEGO,TIOGA,"H17 CREW PULLING 15 CARS EAST OUT OF INTERCHANGE TRACK. THE 12TH, 13TH, AND 14TH CAR HAD DERAILED DU E TO A BROKEN SWITCH POINT.",False,True,False,False,False,0.0
629,19,12,CRSH,36,STATEN ISLAND,RICHMOND,"CREW PULLED THROUGH TRACK 3 IN ARLINGTON YARD WITH 19 LOADED CARS AND 77 EMPTY CARS. THE CARS ROLLED BACK THROUGH TRACK 6 IN ARLINGTON YARD ONTO THE ARLINGTON LEAD, STRIKING CARS FROM THE TRAIN STANDI NG ON TRACK 3 AND DERAILING COVX 60045.",False,True,False,False,False,0.0
630,19,3,ATK,36,NEW YORK NEW YORK,NEW YORK,"WORK TRAIN CREW KN-704 OPERATING WEST OFF 13 STATION TRACK WITH E/574 AND 3 EMPTY BALLAST CARS (C/11 192, C/11915, C/11930) DERAILED THE 2ND & 3RD CARS IN CONSIST TO THE FIELD SIDE WHILE OPERATING OVER THE 69 SWITCH. THERE WERE NO REPORTS OF INJURY. THE CAUSE OF THE DERAILMENT WAS THE FLANGE OF THE WHEEL ROLLED ONTO A PIECE OF CONCRETE AND ABOVE THE RAILHEAD.",False,True,False,False,False,0.0
631,19,5,CWRO,39,CLEVELAND,CUYAHOGA,CREW WAS PULLING LOADS FROM THE FURNANCE WHEN RAIL BROKE UNDER THE 3RD BOTTLE CAUSING THE REAR 3 CAR S TO BECOME DERAILED.,False,True,False,False,False,0.0
632,19,5,CWRO,39,CLEVELAND,CUYAHOGA,"CREW WAS SHOVING WEST TO SENECA YARD WITH 4 EMPTY BOTTLES WHEN THEY WENT THROUGH THE SENECA 27 / MAI N CROSSOVER, AT WHAT TIME THE ENGINEER NOTICED THE SLOWING DOWN AND CAME TO A STOP. UPON INSPECTION , THE LEAD 3 BOTTLES WERE ON THE DUE TO THE LEAD BOTTLE PICKING THE 27 SWITCH DUE TO BEING RUN THROU GH EARLIER.",False,False,True,False,False,0.0
633,19,2,ATK,42,PHILADELPHIA,PHILADELPHIA,LOCOMOTIVE E/615 WAS BEING MOVED ON THE PIT TRACK AT RACE ST ENGINE HOUSE WHEN IT STRUCK A FALL PROT ECTION APPARATUS IN THE FOUL OF PANTOGRAPH TRAVEL CAUSING THE PANTOGRAPH ON E/615 TO BECOME INVERTED . DUE TO THE PANTOGRAPH OF E/615 STRIKING THE FALL PROTECTION APPARATUS AN EMERGENCY PLATE WAS PUT IN PLACE ON STATION TRACKS 7-10 AND 1 & 4 CONNECTION TRACKS TO ZOO INTERLOCKING.,True,False,False,False,False,0.0
634,19,7,NS,42,TUNNELHILL,BLAIR,NS TRAIN 35AC226 TRAVELING ON MAIN DERAILED.,False,True,False,False,False,0.0
635,19,12,NS,45,SAXON,SPARTANBURG,AMTRAK TRAIN. AMTRAK TRAIN 020 STRUCK A HWY-USER AT A HWY-GRADE CROSSING.,True,False,False,False,False,0.0
636,19,7,NS,45,RIDGEVILLE,DORCHESTER,WHILE 62RP916 EXPERIENCED AN UNDESIRABLE BRAKE APPLICATION AND DERAILED 36 CARS.,False,True,False,False,False,0.0
637,19,3,NS,45,DUNEAN,GREENVILLE,P74P319 ENGINEER SWAPPING ENDS OF ENGINE CONSIST ALLOWED CONSIST TO ROLL EAST ON THE DAN RIVER PASS TRACK OVER DERAIL.,False,True,False,False,False,0.0
638,19,7,NS,42,WAYNESBURG,GREENE,NS TRAIN N79CA23 DERAILED CAR CSXT 303097 WHILE EN ROUTE TO LOAD.,False,True,False,False,False,0.0
639,19,6,NS,42,CONWAY,BEAVER,"CE20 SHOVING WEST WITH 3 UNITS, 45 LOADS, 6 EMPTIES, AND 6198 TONS ON 451 TRACK DERAILED 7 CARS (XOM X 110240, UTLX 200876, AOK 28502, DWC 627661, TTPX 804410, NS 118051, & TTPX 804692.",False,True,False,False,False,0.0
640,19,6,NS,42,SIDMAN,CAMBRIA,"C4WC224 TRAVELING NORTH WITH 3 UNITS, 110 LOADS, 0 EMPTIES, AND 15,000 TONS ON WINDBER INDUSTRIAL TR ACK DERAILED 10 CARS (NS 53394, NS 47568, NS 52739, NS 47347, NS 42280, NS 53295, NS 47255, NS 53109 , NS 39192, & CR 507729).",False,True,False,False,False,0.0
641,19,7,NS,42,TUNNELHILL,BLAIR,34AC205 TRAVELING WEST ON MAIN 3 DERAILED 11 CARS AT MILEPOST PT 242.,False,True,False,False,False,0.0
642,19,7,GET,42,GETTYSBURG,ADAMS,"SETTING CARS OUT ON THE PASS TRACK CUT AWAY AND COMING TO MAIN 1 AXLE WENT ON GROUND, #3. WHILE TRYI NG TO REREAL #4 WENT ON GROUND.",False,False,True,False,False,0.0
643,19,3,URR,42,DUQUESNE,ALLEGHENY,"MAINLINE CREW WAS HAULING A LOADED COKE TRAIN WHEN THE 38TH CAR FROM THE LOCOMOTIVES DERAILED ON A C URVE, CAUSING THREE OTHER CARS TO ALSO DERAIL. CSXT 298048, THE FIRST CAR TO DERAIL, IS A HI-CUBE HO PPER WITH A HIGH CENTER OF GRAVITY. AS THIS CAR NAVIGATED A CURVE, IT DERAILED TO THE HIGH SIDE DUE TO THE INTERACTION OF LATERAL AND VERTICAL FORCES.",False,True,False,False,False,0.0
644,19,3,RJCP,42,COMMODORE,INDIANA,"PULLING 65 LOADED COAL CARS THE 2ND HEAD CAR DERAILED ON A VEHICLE HEAD SPLIT. 11 CARS TOTAL DERAILE D, 2 OF THE 11 WERE UNREPAIRABLE.",False,True,False,False,False,0.0
645,19,4,SEPA,42,YEADON,DELAWARE,"APRIL 8TH NORTHBOUND TRAIN 1342 MEDIA ELWYN LINE MADE CONTACT WITH AN UNAUTHORIZED VEHICLE DRIVEN BY A 51 YEAR OLD WOMAN HEADING EAST TO WEST AT THE UNION AVENUE GRADE CROSSING. THE ENGINEER PUT TRAIN INTO EMERGENCY AS SOON AS THE UNAUTHORIZED VEHICLE WENT AROUND WORKING CROSSING GUARD ARMS AND FLAS HING LIGHT INDICATORS, BUT COULD NOT STOP THE TRAIN IN TIME TO AVOID MAKING CONTACT WITH DRIVER'S SI DE OF THE VEHICLE. THE TRAIN PUSHED THE CAR 515FT. PAST GRADE CROSSING NORTH IN ROW UNTIL FINALLY CO MING TO REST. THE VEHICLE DRIVER WAS TAKEN TO THE HOSPITAL AND WAS LATER PRONOUNCED DECEASED ON APRI L 9TH AT 9:05.",False,False,True,False,False,0.0
646,19,3,ATK,42,CROYDON,BUCKS,"SEPTA TRAIN 719 ON TRACK 1 AT MP 69.6 REPORTED THAT A FIRE WAS COMING FROM THE TRACTION MOTOR ON LEA D MU 424. THE CREW WAS UNABLE TO EXTINGUISH THE FIRE PROMPTING 200 PASSENGERS TO BE EVACUATED FROM THE TRAIN. ONCE ALL PASSENGERS WERE OFF, THE CREW LOWERED THE PANTOGRAPHS AND THE FIRE WENT OUT. T HERE WERE NO INJURIES TO THE SEPTA CREW OR PASSENGERS.",False,False,True,False,False,0.0
647,19,12,CRSH,42,TRAINER,DELAWARE,FC21 DERAILED 1 ENGINE AND 11 CARS WHILE PULLING ON TRACK 11 IN STONEY CREEK YARD,False,True,False,False,False,0.0
648,19,11,SEPA,42,PHILADELPHIA,PHILADELPHIA,SEPTA EXTRA EQUIPMENT WITH 9 CARS PULLED DOWN WIRES AT ZOO INTERLOCKING. THREE CARS HAD PANTOGRAPH D AMAGE AND NEEDED TO BE REBUILT. AMTRAK MANAGEMENT RESPONDED TO THE SCENE AND REPORTED THE SIGNAL FEL L OFF THE SIGNAL BRIDGE INTO THE CENTENARY WIRES AD WERE FOULING THE TRACK,False,False,True,False,False,0.0
649,19,11,CRSH,42,FAIRLESS HILLS,BUCKS,"FP51 WAS SWITCHING A CUT OF CARS AND SET OUT TTZX 861017 TO THE LOW SIDE LEAD TOWARD TRACK E1. THE C AR WAS NOT SECURED AND ROLLED BACK INTO THE TRAIN THAT WAS STILL BEING SWITCHED OUT, STRIKING AND DA MAGING CAR HOKX 286036.",False,False,True,False,False,0.0
650,19,1,UP,41,PENDLETON,UMATILLA,LOCOMOTIVE ELECTRICAL FAULT ON THE UP8724 CAUSED AN UNDESIRED EMERGENCY BRAKE APPLICATION RESULTING IN DRAW BAR FAILURE.,False,False,True,False,False,0.0
651,19,1,UP,41,PORTLAND,MULTNOMAH,"YBA66-11 ENCOUNTERED A BROKEN RAIL ON THE WEST END OF BARNES YARD, ON THE SOUTH RAIL OF TRACK #14, W HICH CAUSED THREE CARS TO DERAIL.",False,True,False,False,False,0.0
652,19,5,CWRO,39,CLEVELAND,CUYAHOGA,CREW WAS PULLING 13 LOADS FROM HARVARD YARD WHEN THEY CROSSED OLD CAMPBELL ROAD ON 705 AND FELT A BO UNCE AT WHAT TIME THEY STOPPED THE TRAIN. UPON INSPECTION IT WAS FOUND THAT THE CREW PICKED THE 705 / OLD CAMPBELL ROAD SWITCH CAUSING THE DERAILMENT.,False,True,False,False,False,0.0
653,19,1,NS,39,FOSTORIA,SENECA,"L11 CREW RAN THROUGH THE MAINLINE SWITCH AFTER FAILING TO LINE BOTH ENDS FOR THEIR MOVE. WHEN THEY M ADE THEIR REVERSE MOVE TO SHOVE INTO 3 TRACK, THEY RAN THROUGH THEIR OWN PREVIOUSLY RUN THROUGH SWIT CH CAUSING 2 CARS TO DERAIL AND ADDITIONAL DAMAGEE TO 1 STANDING CAR ALREADY IN TRACK.",False,True,False,False,False,0.0
654,19,1,NS,39,BELLEVUE,HURON,"WHILE PULLING TRACKS FROM THE NORTH BOWL, LB17 PULLED WEST WITH CARS FROM CT12 AND CT05 PRIOR TO MAK ING A SHOVE MOVEMENT TO COUPLE TO AND PULL CT27. DURING THE SHOVE MOVEMENT, RADIO COMMUNICATION WAS LOST RESULTING IN A HARD COUPLING IN CT27 CAUSINGG ONE CAR TO DERAIL AND DAMAGE TO ANOTHER.",False,True,False,False,True,0.0
655,19,3,GTW,39,TOLEDO,LUCAS,"WHILE IN THE PROCESS OF KICKING CARS SOUTHWARD INTO TRACK LT53, ASSIGNMENT R90161-22 (CN2175/CN2569) KICKED TTGX 978708 BEFORE THE CARS IN LT53 CLEARED, SIDESWIPING RAILCAR UTLX 647678. NO INJURIES RE PORTED OR DANGEROUS GOODS INVOLVED.",False,False,True,False,False,0.0
656,19,12,CSX,36,COXSACKIE,GREENE,"Q40907 COLLIDED WITH AN UNOCCUPIED VEHICLE NEAR MANSION STREET IN COXSACKIE, NY. TRAIN DISPATCHER NO TED THE CREW REPORTED SEEING SOMEONE RUN FROM THE AREA.",False,False,True,False,False,0.0
657,19,5,NS,36,BUFFALO,ERIE,"W09C911 PULLING WEST WITH 2 UNITS, 15 LOADS, 102 EMPTIES, AND 5320 TONS ON SWAMP TRACK DERAILED 4 CA RS (UTLX 675281, UTLX 665406, FURX 128008, & WFRX 155855).",False,True,False,False,False,0.0
658,19,3,CRSH,34,FRANKLINVILLE,GLOUCESTER,TAMPER ME5450 WAS STRUCK BY HIGHWAY USER,True,False,False,False,False,0.0
659,19,2,SNJX,34,TRENTON,MERCER,"ON 2/1/2019, AT APPROX. 11:36 AM, TRAIN 244 LRV 3507 REPORTS SMOKE COMING FROM C-CAR AT HAMILTON STA TION. APPROX. 30 PASSENGERS DE-TRAINED AT HAMILTON STATION.
THERMAL EVENT CREATED BY TURBO FAILURE. ACTUAL MONETARY DAMAGE IS STILL BEING INVESTIGATED, BUT WILL EXCEED THE $10,700 NTHRESHOLD FOR REPO RTING.",False,False,True,False,True,10700.0
660,19,5,UP,32,SPARKS,WASHOE,"THE YSP30-28, LEAD LOCOMOTIVE UP5274, HAD A HOLD OF 54 CARS AND 3 LOCOMOTIVES PULLING EASTWARD ON TH E LEAD TOWARDS THE SOUTH RUNNER WHEN THE COUPLER FAILED ON THE CMO167386. THE CREW DIDN'T NOTICE TH E TRAIN'S 34 CARS SEPARATE AS THE ENGINEER CONTINUED TO PULL EASTWARD. AFTER STOPPING, THE FOREMAN INSTRUCTED THE ENGINEER TO COME WESTWARD WITH 3 LOCOMOTIVES AND 20 CARS AS THEY COLLIDED WITH THE 34 CARS THAT HAD SEPARATED EARLIER DERAILING 4 LOADED CORN CARS.",False,True,False,False,False,0.0
661,19,3,NS,37,ASHEVILLE,BUNCOMBE,"TRAIN E28P825 PULLING WEST WITH THREE UNITS 14 LOADS, 47 EMPTIES, 3453 TONS ON HIGH LEAD INTO CP RUS SELL AT ASHEVILLE YARD DERAILED 5 CARS, DERAILING - NATX 230526 WHEELS 1L/1R OF NATX 230526, ALL WHE ELS SOU 39604, TURNED OVER SOU 134505 AND A-END SOOU 134677.",False,True,False,False,False,0.0
662,19,3,NS,37,BESSEMER CITY,GASTON,NS TRAIN 221GP29 STRUCK A HWY-USER AT A HWY-GRADE CROSSING. VEHICLE UNOCCUPIED AT TIME OF INCIDENT. DRIVER'S INFORMATION UNKNOWN.,True,False,False,False,False,0.0
663,19,7,NS,37,GREENSBORO,GUILFORD,NS TRAIN P31P225 DERAILED REAR CARS WHILE PULLING. CAR VMSX 310388 RELEASED APPROXIMATELY 5 GALLONS OF DENATURED ALCOHOL..,False,True,False,False,False,0.0
664,19,3,NS,37,GREENSBORO,GUILFORD,"51XP207 SHOVING SOUTH ON WEST LEG OF WYE WITH 3 UNITS, 0X84, 2664 TONS DERAILED ALL WHEELS ON ALL UN ITS AND LEAD CAR.",False,True,False,False,False,0.0
665,19,11,BNSF,38,NEW ROCKFORD,EDDY,"Z CHCPTL7 06A REPORTED STRIKING THE TRAILER OF A SEMI-TRUCK ON SINGLE MAIN TRACK AT MP 117.18 ON THE K.O. SUBDIVISION, BETWEEN NEW ROCKFORD AND BRANTFORD. THIS INCIDENT DID NOT OCCUR AT A ROAD CROSSIN G (15TH STREET NORTHEAST) EQUIPPED WITH CROSSBUCKS.",False,False,True,False,False,0.0
666,19,10,BNSF,38,BOTTINEAU,BOTTINEAU,G-BOTINB9-10 DERAILED 3 RAILCARS WHILE PULLING OUT OF INDUSTRY TRACK 4320 DUE TO TRACK ROADBED SETTL ED OF SOFT. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
667,19,2,UP,32,LAS VEGAS,CLARK,"LUM49-28, LEAD LOCOMOTIVE UP4140 WAS SHOVING ON AIR, WITH 5 HAND BRAKES APPLIED, FROM THE SIDING THR OUGH THE CROSSOVER SWITCH AND DOWN 711.",False,False,True,False,False,0.0
668,19,5,RRVW,38,KINDRED,CASS,PULLING OUT THE WEST END OF THE SIDING AT KNIDRED THE 12TH CAR FROM THE HEAD END DERAILED. A TOTAL O F 4 CARS DERAILED 2 TIPPED OVER,False,True,False,False,False,0.0
669,19,4,DMVW,38,FULLERTON,DICKEY,"WHILE SHOVING THE 132 TRAIN INTO THE FULLERTON SIDING, 8 CARS DERAILED DUE TO SOFT TRACK CONDITIONS.
30. Z-ELEVATOR SIDING
**UPDATE DAMAGE AMOUNTS BOX 36 & 37**",False,True,False,False,True,0.0
670,19,5,DMVW,38,NAPOLEON,LOGAN,"28. EMBANKMENT FAILURE
SEVEN CARS OF A FIFTY FIVE CAR TRAIN DERAILED DUE TO AN EMBANKMENT FAILURE.* *AMENDED REPORT-UPDATED TRACK AND EQUIPMENT DAMAGE AMOUNTS**",False,True,False,False,True,0.0
671,19,10,RRVW,38,SHELDON,RANSOM,CREW WAS PROCEEDING THROUGH RANSOM JCT EASTWARD WHEN THE LEAD LOCOMOTIVE STARTED SHAKING SLIGHTY. CR EW BROUGHT TRAIN TO A EASY STOP AND FOUND 5 CARS AND 3 DERAILED LOCOMOTIVES.,False,True,False,False,False,0.0
672,19,2,UP,32,CALIENTE,LINCOLN,"TRAIN CSKVV-06, LEAD LOCOMOTIVE UP7736, DERAILED 25 CARS ON 2 DEGREE LEFT HAND CURVE. EVIDENCE OF B ROKEN RAIL ON HIGH SIDE OF CURVE FOUND ON RAILCAR WHEELS THAT TRAVERSED LOCATION PRIOR TO DERAILING CARS BEHIND. ACTUAL BROKEN PIECES WERE NOT RECOVERABLE DUE TO MAGNITUDE OF COAL SPILL & EXCAVATION.",False,True,False,False,False,0.0
673,19,2,UP,32,LAS VEGAS,CLARK,LUM49-10 WAS SHOVING 47 CARS INTO TRACK 201. BRAKEMAN WAS RIDING THE SHOVE AND DERAILED 3 CARS.,False,True,False,False,False,0.0
674,19,6,UP,32,WELLS,ELKO,"MNPRV-17 EXPERIENCED A UDE. THE TRAIN CREW REPORTED THAT LOOKING BACK AT THE TRAIN, THEY COULD SEE THE TRAIN HAD DERAILED APPROXIMATELY 59 CARS FROM THE HEAD END BETWEEN THE HEAD AND MID DPU. DERAIL MENT RESPONSE TEAM CHOSE A CAUSE CODE M299 DUE TO POOR TRAIN MAKEUP. NO MAKEUP RULES WERE VIOLATED BUT NEW TRAIN MAKEUP GUIDELINES WILL LIKELY COME FROM THIS DERAILMENT.",False,True,False,False,False,0.0
675,19,6,UP,32,ELKO,ELKO,IG2LT-18 HAD LEAD LOCOMOTIVE UP5860 WITH A TRACTION MOTOR FIRE AT THE EAST END OF THE ELKO YARD. NO DERAILMENT OR TRACK DAMAGE.,False,False,True,False,True,0.0
676,19,7,UP,31,NORTH PLATTE,LINCOLN,"YNP82R-26, PULLING 11 CARS, DERAILED TWO LOCOMOTIVES AT #27 POWER SWITCH. SWITCH WAS FOUND TO BE OBS TRUCTED BY EXTENDABLE PIN LIFTER THAT FELL OFF FREIGHT CAR.",False,True,False,False,False,0.0
677,19,7,UP,31,NORTH PLATTE,LINCOLN,"WHILE MAKING THEIR SECOND SHOVE IN FORWARDER 10, THE YNP37R-27 DERAILED 3 CARS ON THE 8-13 LEAD.",False,True,False,False,False,0.0
678,19,7,UP,31,NEBRASKA CITY,OTOE,"THE GSNIAO-30 DERAILED WHILE PULLING THE LOADED GRAIN TRAIN OUT OF THE GAVILON GRAIN ELEVATOR. 12 C ARS DERAILED AS THEY PASSED OVER A WOODEN BRIDGE STRUCTURE INSIDE GAVILON INDUSTRY. THE STRUCTURE C OLLAPSED IN THE FACILITY, CAUSING THE TRAIN TO DERAIL. BRIDGE WAS ABOUT 30-40 FEET ABOVE A CREEK AB OUT 7 CAR LENGTHS FROM THE MAINLINE SWITCH . 4 OF THE CARS WENT INTO THE CREEK WITH THE BRIDGE. NO INJURIES, NO HAZMAT RELEASES. CAUSE OF DERAILMENT WAS ONE OR MORE OF THE WOOD BENTS FAILED DUE TO DECAYED PILE. INDUSTRY MAINTAINS TRACK AND BRIDGE",False,True,False,False,False,0.0
679,19,3,UP,31,HASTINGS,ADAMS,LFB46-25 WAS SHOVING INTO INDUSTRY AT 4 MPH AND RAIL ROLLED UNDER CARS DERAILING 3 REAR CARS OF SHOV E. INDUSTRY MAINTAINS TRACK,False,True,False,False,False,0.0
680,19,3,BNSF,27,RUTHTON,PIPESTONE,G-RUTTAC9-27 DERAILED 4 RAILCARS WHILE PULLING OUT OF INDUSTRY TRACK 5266 DUE TO A PREVIOUSLY RUN TH ROUGH SWITCH. THE DERAILED RAILCARS IMPACTED RAILCARS IN ADJACENT TRACK. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
681,19,8,UP,27,ST PAUL,RAMSEY,"TRAIN YSP80-04 WAS PULLING INTO TRACK 26 AT HOFFMAN YARD. WHEN 5 CARS DERAILED AT THE 26 SWITCH. CAR ATW366500, FIRST WHEEL, DROPPED BEHIND SWITCH POINT DUE TO SWITCH CONDITIONS. SWITCH SHOWED SIGNS O F A POSSIBLE PREVIOUS RUN THROUGH SWITCH. INVESTIGATION INCLUDED REVIEWING THE STATIONARY CAMERAS FR OM THE PREVIOUS 24 HRS ALONG WITH A TIR FROM AN ENGINE THAT WENT THRU SWITCH EARLIER TO SEE INDICATI ON OF SWITCH. NO CREW FOUND RESPONSIBLE.",False,True,False,False,False,0.0
682,19,3,UP,27,LE SUEUR,LE SUEUR,"CBPBT9-13, LEAD LOCOMOTIVE UP5674, WAS TRAVELING SOUTH ON SINGLE MAINLINE ON CLEAR SIGNALS WHEN IT D ERAILED DUE TO FLOODING. DERAILMENT RESULTED IN ONE LOCOMOTIVE AND 13 RAILCARS OFF THE RAIL.",False,True,False,False,False,0.0
683,19,5,UP,27,ST PAUL,RAMSEY,"MPRSS-27, LEAD LOCOMOTIVE UP8526, WAS ARRIVING INTO THE STATE STREET YARD SIDE OF THE TERMINAL, WHEN THEY WERE NOTIFIED BY RADIO THAT THEY HAD 9 CARS DERAILED.",False,True,False,False,False,0.0
684,19,7,BNSF,27,ST PAUL,RAMSEY,U-CPPRSS0-04 DERAILED 7 RAILCARS WHILE PULLING INTO YARD TRACK 8005 DUE TO SWITCH NOT LATCHED OR LOC KED. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
685,19,7,CP,27,ST PAUL,RAMSEY,"683-645 LOADED SAND TRAIN WAS PULLING INTO BNSF DAYTON'S BLUFF YARD FOR DELIVERY WHEN THE 51ST CAR P ICKED TRACK 5 SWITCH CAUSING REAR OF TRAIN TO TRAVERSE TOWARDS TRACK 6 SUBSEQUENTLY DERAILING 7 CARS . WHEN APPROACHING BLUFF YARD, CREW WAS INSTRUCTED TO CONTACT `MOBILE 80` FOR INSTRUCTIONS INTO THE YARD. MOBILE 80 INFORMED CREW TO CONTACT BNSF4645 WORKING ON THE EAST END OF YARD. CREW CALLED BNSF4 645 WHO STATED THEY WERE IN THE CLEAR & CONDUCTOR WAS WALKING UP TO LINE THE TRACK 5 SWITCH FOR THEM . AS 683 PULLED INTO THE YARD, THEY WERE VERIFYING SWITCH POINTS & PROCEEDED INTO TRACK 5 AS THEY WE RE LINED. 50 CARS INTO THE TRACK MOVEMENT STOPPED ONCE THE BNSF4645 REPORTED THEY WERE ON THE GROUND . BNSF RESPONSIBLE FOR CAUSE. POD MARKINGS INDICATED SWITCH HAD THROWN UNDERNEATH THEIR MOVEMENT. UP ON INSPECTING SWITCH IT DID NOT HAVE A LATCH & WAS NOT FULLY SEATED IN THE KEEPER AFTER THROWN BY BN SF CONDUCTOR. BNSF REPORTS $360,000 TRACK DAMAGE.",False,True,False,False,True,360000.0
686,19,1,NS,18,DAYTON,TIPPECANOE,DL03 RCO WITH 3 LOCOMOTIVES AND 12 LOADS SHOVED WEST INTO SOUTH YARD PASS DERAILING 6 CARS IN B-YARD SIDING,False,True,False,False,False,0.0
687,19,12,TRRA,17,MADISON,MADISON,ENGINEER BEGAN TO PULL AHEAD WITH 5 CARS AND 4 ENGINES TO SHOVE TRACK 9 WHEN THE YARDMASTER OBSERVED CARS ON THE GROUND AND CALLED THE CREW TO STOP THE MOVEMENT.,False,False,True,False,False,0.0
688,19,9,UP,17,MELROSE PARK,COOK,"MASPR-29 WAS PULLING INTO YARD 4 FROM THE IHB VIA NORTH MELROSE. AFTER STOPPING TO LINE THE YARD 1 L EAD SWITCH, CREW TRAVERSED 2,144' WHEN THE TRAIN WENT INTO EMERGENCY. UPON INSPECTION AND AFTER INVE STIGATION IT WAS DETERMINED THE 2 CARS DERAILED DUE TO STIFF TRUCKS.",False,True,False,False,False,0.0
689,19,9,UP,17,EAST ST LOUIS,ST CLAIR,"AASFX-05 WAS PULLING OUT OF GATEWAY YARD IN THROTTLE 2 AT 4MPH WHEN 6 CARS DERAILED. THE CAUSE OF TH E DERAILMENT WAS FROM THE FLANGE CUTTING INTO THE CLIMBING THE LOW SIDE OF THE RAIL AT A POINT WHERE THE GAUGE OF THE RAIL WENT FROM 57.5 INCHES TO 56 INCHES IN A 10 FOOT SPAN. THE WHEEL WAS HUNTING T O NEGOTIATE THE AREA WHEN IT CLIMBED UP THE RAIL RESULTING IN THE DERAILMENT. ALS MAINTAINS TRACK. A LS TRACK DAMAGE = $26,455",False,True,False,False,True,26455.0
690,19,10,CSX,13,UNION CITY,FULTON,A74413 WAS TRAVELING NORTH ON THE AWP SUBDIVISION WHEN THEY STRUCK AN UNOCCUPIED SEMI TRUCK LOADED W ITH POLYMERS AT THE XXB016.88 WATSON STREET. VEHICLE BECAME STUCK WHILE TRYING TO TRAVERSE THE CROSS ING PRIOR TO GATES COMING DOWN. PROTECTION ALSO AT CROSSING: ADVANCE WARNING.,True,False,False,False,False,0.0
691,19,12,UP,17,JOLIET,WILL,"MASPR-12, LEAD LOCOMOTIVE UP2717, WAS DEPARTING AT MP 37 ON THE JOLIET SUB. TRAIN MOVED A TOTAL OF 881 FEET AND WENT INTO UDE. UPON INSPECTION CONDUCTOR FOUND THE SECOND CAR FROM THE HEAD END HAD DE RAILED DUE TO MASSIVE BUILD-UP ON WHEELS OF RAILCAR BKTY150173.",False,False,True,False,False,0.0
692,19,12,UP,17,STERLING,WHITESIDE,"MCBPR-21 WHILE MAKING MID-TRAIN 3 CAR SETOUT AT STERLING YARD, SIDESWIPED THE REAR PORTION OF THEIR TRAIN LEFT ON THE MAIN IN THE FOUL, WHILE MAKING THE SHOVE INTO THE YARD.",False,False,True,False,False,0.0
693,19,12,UP,17,MADISON,MADISON,"MNLTR-10 WAS PULLING THEIR TRAIN THROUGH INBOUND TRACK 2 AT TRRA MADISON. AFTER PULLING INTO THE CLE AR ON THE SOUTH END, THE CREW STOPPED, MADE A CUT ON THE NORTH END AND BEGAN PULLING NORTH WITH THEI R 5 REMAINING CARS: AT WHICH POINT 2 AUTORACKS DERAILED DUE TO TRAIN HANDLING. TRRA MAINTAINS TRACK . TRRA TRACK DAMAGE = $16,742",False,True,False,False,True,16742.0
694,19,6,CC,19,FARLEY,DUBUQUE,"L56591-15 (CN5405, 5E 150T 300F) WAS SHOWING 5 CARS EASTWARD INTO TRACK D WHEN TILX290860 ON MOVEMEN T COLLIDED WITH TILX281119 WHICH WAS FOUL IN TRACK FA77. TILX281119 SUSTAINED WALKWAY DAMAGE. NO HAZ MAT OR INJURIES INVOLVED.",False,False,True,False,True,0.0
695,19,2,BNSF,19,CRESTON,UNION,H-LINGAL1-21 DERAILED 10 RAILCARS PULLING OUT OF YARD TRACK 110. NO HAZARDOUS MATERIALS WERE RELEAS ED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
696,19,3,BNSF,4,WINSLOW,NAVAJO,M-KGMWIN1-04 DERAILED 5 RAILCARS WHILE PULLING INTO YARD TRACK 2826 DUE TO A SPRING/POWER SWITCH MEC HANISM MALFUNCTION. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
697,19,9,SAN,13,SANDERSVILLE,WASHINGTON,"AIC TRAIN CONSISTING OF 2 UNITS, 2 LOADS, 57 MTYS, 2200 TONS, 3365 FT, STUCK A TRACTOR-TRAILER AT AN AT-GRADE PASSIVE CROSSING WHILE TRAVELING NORTH ON THE MAINLINE AT 19 MPH ON SINGLE TRACK. THE MOT ORIST WAS TRAVELING EAST TO WEST ON GEORGE J LYONS PKWY PULLING A LOADED TRAILER OF GOLF CART BATTER IES. THE LEAD LOCOMOTIVE (SAN 1600) WAS OCCUPIED BY 3 T&E EMPLOYEES (EN, CO, BK). AS THE TRAIN APP ROACHED THE CROSSING ALL CREWMEMBERS REPORT THE WHISTLE WAS SOUNDED, BELL RINGING, WITH HEADLIGHT ON BRIGHT. THE ENGINEER REPORTS PLACING THE TRAIN IN EMERGENCY BRAKING WHEN IT WAS APPARENT THE MOTOR IST WAS NOT STOPPING AT THE AT-GRADE CROSSING. THE WARNING DEVICES AT THE CROSSING CONSISTED OF CRO SSBUCKS AND STOP SIGNS ON SAME POST. THE LEAD LOCOMOTIVE STRUCK THE TRAILER CAUSING SEVERAL OF THE GOLF CART BATTERIES TO RUPTURE UPON IMPACT. BATTERY ACID CONSISTING OF 10%-38% SULFURIC ACID ENTERE D THE CAB OF THE LOCOMOTIVE WHICH MADE CONTACT WITH ALL THREE RAILROAD EMPLOYEES. THE TRAIN CAME TO A STOP 280 FT NORTH OF THE AT-GRADE CROSSING. THE MOTORIST TOLD THE TRAIN CREW THAT HE WAS OPERATI NG A GPS DEVICE WHEN APPROACHING THE CROSSING AND DID NOT STOP FOR THE TRAIN. THE MOTORIST WAS GIVE N A CITATION FOR FAILURE TO YIELD BY GEORGIA STATE PATROL. THE MOTORIST REPORTED HE WAS NOT INJURED , THE THREE RAILROAD EMPLOYEES ON THE LOCOMOTIVE RECEIVED FIRST AID AND WERE TRANSPORTED TO HOSPITAL FOR OBSERVATION.",True,False,False,False,False,0.0
698,19,8,NS,13,FLOWERY BRANCH,HALL,NS TRAIN 204P407 STRUCK A HWY-USER AT A HWY-GRADE CROSSING.,True,False,False,False,False,0.0
699,19,8,CSX,13,ATLANTA,FULTON,"Y10717 HAD PLACED 1 CAR IN H14 TTXZ 864441, TESTED BRAKE AT 1056. THEY WENT TO THE AB MAIN AND COUPL ED INTO 74 CARS, KNOCKED 20 BRAKES OFF. 24 MINUTES LATER WHEN PULLING THE CUT SOUTH AT 1117, THE CAR IN H14 ROLLED OUT HITTING THE SIDE OF THE CUT OF CARS DERAILING THE TTZX 864442 ON ITS SIDE. LAFX 6 0018 LOAD OF CEMENT AND ACFX 95833 LOAD OF WOOD PULP WERE RAKED.",False,True,False,False,False,0.0
700,19,6,UP,19,SIOUX CITY,WOODBURY,"YSX04-10 PULLED 23 CARS OUT OF 14 TRACK DERAILING 2 CARS. INVESTIGATION REVEALED THAT THE CUT OF CA RS HAD 5 HAND BRAKES ON THE SOUTH END THAT WERE NOT RELEASED PRIOR TO MOVING. WHEN THE ERCX6076 PUL LED ON THE CARS WITH BRAKES, ONE SET OF TRUCKS OF THE ERCX6076 LIFTED UP ON THE 14/15 SWITCH POINT I T WAS SITTING ON AND THEN DROPPED BETWEEN THE POINT AND THE STOCK RAIL GAPPING THE SWITCH FOR THE IF RX21430 LEAD SET OF WHEELS TO FOLLOW INTO 15 TRACK WHILE ONE SET OF WHEELS CONTINUED DOWN 14 TRACK. THE AFT SET OF WHEELS ON THE ERCX6076 DERAILED ON THE MOVEMENT INTO 15 WHILE THE TWO CARS ACCORDION ED BETWEEN 14 AND 15 TRACK.",False,True,False,False,False,0.0
701,19,2,UP,19,MARSHALLTOWN,MARSHALL,YMT01-06 WAS PULLING 50 CARS OUT OF 3 TRACK. THE 29TH THROUGH 34TH CARS DERAILED ON THE LEAD DUE TO A BROKEN RAIL.,False,True,False,False,False,0.0
702,19,2,UP,19,BOONE,BOONE,"LNI21-06 WAS ENTERING THE WEST END OF BOONE YARD. AFTER ENTERING 8 TRACK THE TRAIN EXPERIENCED AN U DE AND DERAILED ONE CAR, CMO20734.",False,True,False,False,False,0.0
703,19,2,UP,19,CLINTON,CLINTON,"MCLPE-10, LEAD LOCOMOTIVE UP5585, PULLED UP TO GLUCOSE AFTER GETTING AUTHORITY, MAINLINE SWITCH WAS LINED BUT DERAIL LEADING TO MAINLINE SWITCH WAS IN DERAILING POSITION. 2 LOCOMOTIVES AND 4 CARS DER AILED AS A RESULT.",False,True,False,False,False,0.0
704,19,5,BNSF,17,WILLOW SPRINGS,COOK,Y-WSP3012-10 DERAILED 1 LOCOMOTIVE WHILE PULLING LIGHT POWER OUT OF YARD TRACK 1712 DUE TO FAILURE T O COMPLY WITH RESTRICTED SPEED IN-TURN RUNNING THROUGH OVER AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
705,19,5,BNSF,17,GALESBURG,KNOX,RCO Y-GAL3022-16 HAD 2 RAILCARS IMPACT EACH OTHER DURING HUMP OPERATIONS IN YARD TRACK 2047 DUE TO D EFECTIVE BRAKE ON RAILCAR. RESULTED IN DAMAGE TO BOTH RAILCARS. NO HAZARDOUS MATERIALS WERE RELEASED .,False,False,True,False,True,0.0
706,19,9,UP,17,DUPO,ST CLAIR,"YDU51-10 WAS SHOVING SOUTH TO TRACK 303 WITH ALL CARS OFF AIR. THE ENGINEER WAS INSTRUCTED TO BRING MOVE TO A STOP AT THE NORTH END OF TRACK 303 TO ALLOW CONDUCTOR TO REPOSITION AT THE SOUTH END OF TR ACK 303 AND PROTECT THE SHOVE. THE CONDUCTOR WAS UNAWARE THE TRAIN BROKE IN TWO 53 CARS AHEAD OF HIS LOCATION AND WERE ROLLING SOUTH. WHEN HE REPOSITIONED, HE GAVE ENGINEER A FRESH CAR COUNT TO CONTIN UE THE SHOVE, AT WHICH TIME THE 83 CARS ATTACHED TO THE LOCOMOTIVE SHOVED INTO THE 53 CARS THAT HAD BROKEN AWAY. THE IMPACT INTO THE 53 CARS CAUSED DERAILMENT OF 14 CARS, INCLUDING ONE HAZMAT CAR THAT CAUGHT FIRE. 1 DRUG POSITIVE - NOT DETERMINED TO BE A CASUAL FACTOR. AT THE TIME OF THE INCIDENT TH E RAIL EQUIPMENT WAS MOVING ABOVE THE MAXIMUM FOR THE TRACK CLASS REPORTED. #11 - 2158 PERSONS EVAC UATED",False,True,False,True,False,0.0
707,19,9,UP,17,DUPO,ST CLAIR,"YDU51-10 WAS SHOVING SOUTH TO TRACK 303 WITH ALL CARS OFF AIR. THE ENGINEER WAS INSTRUCTED TO BRING MOVE TO A STOP AT THE NORTH END OF TRACK 303 TO ALLOW CONDUCTOR TO REPOSITION AT THE SOUTH END OF TR ACK 303 AND PROTECT THE SHOVE. THE CONDUCTOR WAS UNAWARE THE TRAIN BROKE IN TWO 53 CARS AHEAD OF HIS LOCATION AND WERE ROLLING SOUTH. WHEN HE REPOSITIONED, HE GAVE ENGINEER A FRESH CAR COUNT TO CONTIN UE THE SHOVE, AT WHICH TIME THE 83 CARS ATTACHED TO THE LOCOMOTIVE SHOVED INTO THE 53 CARS THAT HAD BROKEN AWAY. THE IMPACT INTO THE 53 CARS CAUSED DERAILMENT OF 14 CARS, INCLUDING ONE HAZMAT CAR THAT CAUGHT FIRE. 1 DRUG POSITIVE - NOT DETERMINED TO BE A CASUAL FACTOR. CAR#: UTLX 200035 METHYL ISOBU TYL KETO, WHOLE CAR. AT THE TIME OF THE INCIDENT THE RAIL EQUIPMENT WAS MOVING ABOVE THE MAXIMUM FOR THE TRACK CLASS REPORTED. #11 - 2158 PERSONS EVACUATED",False,True,False,True,False,0.0
708,19,9,UP,17,EAST ST LOUIS,ST CLAIR,"AASFX-12 WAS PULLING WEST OUT OF ALS GATEWAY YARD WHEN THE GACX62791 DERAILED, CAUSING A TOTAL OF 10 CARS TO STRING-LINE ON THE ST LOUIS HORN. DEGREE OF CURVE DID NOT ALLOW FOR TRAIN TO NEGOTIATE WITH OUT DERAILING. ALS MAINTAINS TRACK. ALS TRACK DAMAGE = $1,802",False,True,False,False,True,1802.0
709,19,1,LIRC,18,CLARKSVILLE,CLARK,"Q21602 STRUCK TRACTOR TRAILER THAT WAS STUCK ON CROSSING. TRAILER BOTTOMED OUT ON CROSSING AND THE D RIVER COULD NOT MOVE THE VEHICLE. AGE OF DRIVER 62. PROTECTION ALSO AT CROSSING: PAVEMENT MARKINGS ( STOP LINES & RR XING SYMBOLS). LIRC SIGNAL DAMAGE ESTIMATE IS 25,000.",True,False,False,False,True,0.0
710,19,4,CSX,24,CUMBERLAND,ALLEGANY,Y29018 FAILED TO SECURE W06 AND KICKED CARS INTO THE TRACK CAUSING THE CUT TO ROLL THREE QUARTER OF A CAR LENGTH PAST THE CLEARANCE POINT ON THE EAST END. THE REST OF THE CUT OF CARS THEY WERE SWITCHI NG FROM WAS IN W07 HANGING BACK TOWARDS THE RECEIVING YARD. THE Y19019 THEN TOOK OVER AND WHEN THEY PULLED THE NEXT CUT UP TO SWITCH FROM W07 THE FOREMAN NOTICED DAMAGE TO A CAR AND REPORTED IT. FURTH ER INVESTIGATION SHOWED THAT 3 CARS WERE DAMAGED BY SIDE SWIPE FROM W06 BEING OUT OF CLEARANCE DUE T O IT NOT BEING SECURED.,False,False,True,False,True,0.0
711,19,10,MNN,27,ROSEAU,ROSEAU,"#29(CONTRIBUTING CAUSE TO THE DERAILMENT IS THE SIDE TRACK WAS NOT INSPECTED OR RECORDED THAT IT HAS BEEN INSPECTED WITHIN THE LAST MONTH. HAD THIS TRACK BEEN PROPERLY INSPECTED THE WIDE GAUGE WOULD H AVE BEEN NOTICED AND REPAIRED) RAILCARS INVOLVED SOUTH TO NORTH 22105, 480463, 481777 & 350249
THE TRAIN WAS PULLING OUT OF SIDING & THE FOURTH TRUCK ON 480463 FELL OFF THE RAIL, 481777 TRUCKS FOLLOWED WITH THE 1 TRUCK FROM THE 350249. THE 4TH & 5TH TRUCKS DUG INTO THE ROADBED PULLING AWAY FR OM TRACK CAUSING THE 22105 & 480463 TO TIP OVER. TRAIN CREW WERE PULLING THEIR TRAIN OUT OF ROSEA U SIDING WHEN ENGINEER FELT A JERK AND BEFORE HE COULD REACT THE TRAIN WENT INTO EMERGENCY. THE COND UCTORE DROVE BACK TOWARDS REAR OF TRAIN AND COULD SEE THAT SOME RAILCARS HAVE TIPPED OVER.",False,True,False,False,False,0.0
712,19,6,UP,27,ST PAUL,RAMSEY,MPRSS-28 LEAD LOCOMOTIVE UP6768 WAS PULLING INTO TRACK 22 AT HOFFMAN. THEY STOPPED ON THE SOUTH END OF 22 SO THE CONDUCTOR COULD GET OFF AND LINE A SWITCH. CREW THEN STARTED AHEAD AND WERE THEN NOTI FIED THEY DERAILED 4 CARS.,False,True,False,False,False,0.0
713,19,2,NS,37,WALKERTOWN,FORSYTH,"UV04 COUPLED TO 11 CARS IN TRACK 12, ENGINEER DID NOT ALLOW FOR AIR TO BUILD BEFORE SHOVING ON 25 LO ADED CARS. HE THEN WENT STRAIGHT TO NOTCH 6 THROTTLE BRIEFLY, THEN WENT TO NOTCH 8 THROTTLE LOADING IN EXCESS OF 1300 AMPS WHICH CAUSED AUTO RACK TTGXX 922016 SOUTH SET OF TRUCKS TO TURN ROLLING OVER WEST RAIL.",False,False,True,False,False,0.0
714,19,2,NS,37,CHARLOTTE,MECKLENBURG,119P311PULLING SOUTH ON RABBITT LEAD WITH 3 LITE UNITS DERAILED NS 9277 AND NS 9018,False,True,False,False,False,0.0
715,19,5,NS,37,WILSONS MILLS,JOHNSTON,350P225 IN THE SIDING BETWEEN POWHATAN AND NEUSE DERAILED 26 CARS. CAUSE AND CAUSE CODE UPDATED.,False,True,False,False,False,0.0
716,19,3,NS,37,CHARLOTTE,MECKLENBURG,PC01 PULLING NORTH ON YARD LEAD WITH 2 LITE UNITS DERAILED UNIT 3016.,False,True,False,False,False,0.0
717,19,3,CSX,37,HAMLET,RICHMOND,Y19521 DERAILED 4 CARS PULLING FROM THE FORWARDING YARD TO BOWL. :CONFIRMED OVER SPEED,False,True,False,False,False,0.0
718,19,6,NS,37,CRAMERTON,GASTON,"153P311 PULLING SOUTH WITH 3 UNITS, 45X17, 5770 TONS DERAILED AOKX 90280",False,True,False,False,False,0.0
719,19,4,NS,37,SOUTHMONT,DAVIDSON,PL24 PULLING NORTH WAS SIDESWIPED BY EQUIPMENT ROLLING NORTH OUT OF TRACK CT34.,False,False,True,False,False,0.0
720,19,4,CP,38,SAWYER,WARD,"499-09 DERAILED SIX CARS WHILE TRAVELLING WESTBOUND ON THE PORTAL SUBDIVISION. THE TRAIN WENT INTO E MERGENCY AT MP 459.5. SIX CARS DERAILED AFTER THE CROSS-KEY PIN FAILED ON THE WEST DRAWBAR OF THE QC 77126 (POSITION 44). THIS CAUSED THE DRAWBAR TO IMPACT THE GROUND, LIFTING THE CAR AND DERAILING 3 EMPTIES & 3 LOADS. NO DANGEROUS INVOLVED.",False,True,False,False,False,0.0
721,19,12,NCRC,31,ALBION,BOONE,CREW SET A CUT OF 11 CARS ON MAIN & PREPARED TO RUN AROUND CARS ON THE MAIN THROUGH TRACK 716. WHEN ENGINEER STARTED BACKUP MOVEMENT A SCRAPING NOISE WAS NOTED BY CONDUCTOR. ENGINEER WAS TOLD TO STOP. CREW NOTED THAT LOCOMOTIVE HAD SIDESWIPED CAR CRNX 94081 (FIRST CAR OF CUT OF 11 CARS). DAMAGE TO C AR & LOCOMOTIVE. IT WAS DETERMINED THAT CAR WAS IN FOUL OF ADJOINING TRACK.,False,False,True,False,True,0.0
722,19,3,UP,31,NORTH PLATTE,LINCOLN,"YNP83R-04 WAS PULLING EAST ON THE NORTH PULLBACK. THE TRIM TOWER PILOT TOLD THE ENGINEER TO STOP. THE ENGINEER, CALLED BACK SHORTLY AFTERWARDS SAYING HE WAS OVER THE ROCK PILE ON THE PULLBACK. THER E WERE 2 LOCOMOTIVES AND 2 LOADED AUTO RACKS OVER THE END OF TRACK, WITH THE HEAD END FOULING THE SO UTH BELT TRACK - 400' PAST THE END OF TRACK SIGN.",False,False,True,False,False,0.0
723,19,3,UP,31,OSHKOSH,GARDEN,CNACO-02 TRAVELING EAST ON MAIN TRACK ONE AT MP75.86 DERAILED 22 CARS DUE TO INSUFFICIENT BALLAST WI TH A SECONDARY CAUSE OF CROSS LEVEL OF TRACK IRREGULAR.,False,True,False,False,False,0.0
724,19,3,UP,31,NORTH PLATTE,LINCOLN,"YNP32R-24, DERAILED RAILCAR SSW80501 WHILE SHOVING IN WEST BOWL 24.",False,True,False,False,False,0.0
725,19,3,UP,31,OSHKOSH,GARDEN,2CBTWL9-03 DERAILED 35 LOADED COAL HOPPERS DUE TO BROKEN RAIL.,False,True,False,False,False,0.0
726,19,3,UP,31,NORTH PLATTE,LINCOLN,"YNP06R-04, BYPASSED COUPLERS BETWEEN THE TTZX84755 AND THE CRYX5011, CAUSING THE DERAILMENT OF SIX C ARS.",False,True,False,False,False,0.0
727,19,7,UP,32,SPARKS,WASHOE,YSP10-20 OPERATING UP5268 LIGHT POWER CAME OUT OF THE YARD ON THE WEST END THROUGH THE CROSS OVERS A T CPRV243 INTO THE RAMP TRACKS. THE RAMP CONTRACTORS RELEASED THE RAMP TO BE PULLED. RAMP CONTRACTOR S TOOK DOWN THEIR FLAGS AND THE DERAIL ON TRACK 102 BUT LEFT THE DERAIL FOR TRACKS 800 IN THE DERAIL ING POSITION. YSP10-20 RAN OVER THE DERAIL DERAILING TWO SETS OF WHEELS ON THE UP5268.,False,True,False,False,False,0.0
728,19,8,UP,32,NORTH LAS VEGAS,CLARK,"LUM49-25 DERAILED 4 CARS AT THE VALLEY YARD IN TRACK 402/403. THERE ARE NO INJURIES, NO CARS OUT TO FOUL, AND ABLE TO RUN TRAFFIC ON THE MAINLINE.",False,True,False,False,False,0.0
729,19,8,UP,32,NORTH LAS VEGAS,CLARK,"LUM49-25 DERAILED 4 CARS AT THE VALLEY YARD IN TRACK 402/403. THERE ARE NO INJURIES, NO CARS OUT OF FOUL, AND ABLE TO RUN TRAFFIC ON THE MAINLINE.",False,True,False,False,False,0.0
730,19,7,CSX,36,SAVANNAH,WAYNE,"P28107 COLLIDED WITH AN UNOCCUPIED VEHICLE NEAR BROWN ROAD. AMTRAK IS REPORTING 12,875.00 IN DAMAGES .",False,False,True,False,False,0.0
731,19,10,WNYP,36,OLEAN,CATTARAUGUS,"CREW BUILDING A TRAIN IN THE YARD. TAMPER PARKED ON A CURVE. LOCOMOTIVE WAS RUNNING LONG HOOD IN MO DERATE FOG, ENGINEER RAN INTO UNOCCUPIED TAMPER AT RESTRICTED SPEED OR LESS.
AMENDED REPORT UPDAT ED TO SHOW PRELIMINARY ESTIMATE BASED ON AUDIT REVIEW W / FRA 12/23/19 1-27-2020-AMENDED CAUSE CODE AS RECOMMENDATION PER FRA.",False,False,True,False,False,0.0
732,19,10,WNYP,36,OLEAN,CATTARAUGUS,"STANDING UNOCCUPIED TAMPING MACHINE PARKED ON CURVE UNDER BRIDGE STRUCK BY SLOW MOVING SWITCH MOVEME NT RUNNING LONG HOOD AT DAWN WITH MODERATE FOG
AMENDED REPORT UPDATED TO SHOW PRELIMINARY ESTIMAT E BASED ON AUDIT REVIEW W / FRA 12/23/19. 1-27-2020-AMENDED CAUSE CODE AS RECOMMENDATION PER FRA.",True,False,False,False,False,0.0
733,19,3,NS,36,PAINTED POST,STEUBEN,"NS TRAIN 309H729 PULLING WEST WITH 3 UNITS, 23 LOADS, 159 EMPTIES, AND 8022 TONS WHEN THE FRAME OF C AR DJTX 30767 FAILED RESULTING IN CAR BREAKING IN HALF. NO DERAILMENT OCCURRED.",False,False,True,False,False,0.0
734,19,3,NS,39,STEUBENVILLE,JEFFERSON,"60EC328 TRAVELING SOUTH WITH 4 UNITS, 115 LOADS, 0 EMPTIES, AND 16,276 TONS ON STUS SIDING DERAILED 12 CARS (TILX 334260, AOKX 481075, CBFX 306275, AOKX 499792, AOKX 481705, TILX 334297, HWCX 7790, AO KX 480618, HWCX 169108, AOKX 482089, AOKX 497789,AOKX 483898).",False,True,False,False,False,0.0
735,19,3,NS,39,MINGO JUNCTION,JEFFERSON,"60EC327 TRAVELING SOUTH WITH 4 UNITS, 115 LOADS, 0 EMPTIES, AND 16,269 TONS ON INDUSTRY RELAY 1 TRAC K DERAILED 2 UNITS, NS 9494 & BNSF 5267.",False,True,False,False,False,0.0
736,19,1,NS,39,BELLEVUE,HURON,"LB22 WAS PULLING A CUT OF CARS EAST OUT OF WEST YARD 15 AND FOULED THE 1/1A (BENFORDS CROSSOVER) WIT HOUT PERMISSION WHILE RCO JOB LB23 WAS SHOVING THROUGH THE SAME CROSSOVER, RESULTING IN A RAKING COL LISION/DERAILMENT.",False,True,False,False,False,0.0
737,19,6,NS,39,NEW HOPE,PREBLE,NS TRAIN 46RL021 LEAD LOCOMOTIVE NS7034 CAUGHT FIRE.,False,False,True,False,False,0.0
738,19,1,BNSF,40,TULSA,TULSA,Y-TUL1021-11 EXPERIENCED DAMAGE TO 1 RAILCAR DURING HUMPING OPERATION IN YARD TRACK 2015 DUE AUTOMAT IC CONTROL SYSTEM INADEQUATE CONTROL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,False,True,False,True,0.0
739,19,1,BNSF,40,OKLAHOMA CITY,OKLAHOMA,Y-OCK4021-14 DERAILED 3 RAILCARS WHILE SHOVING YARD TRACK 1234 EXPERIENCED DAMAGE TO DUE AUTOMATIC C ONTROL SYSTEM SWITCH FAILURE. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,True,0.0
740,19,7,RVT,41,WHITE CITY,JACKSON,"MECHANIC (OPERATOR) OPERATED THE RVT 82 SWITCHER LOCOMOTIVE (OPERATING LIGHT ENGINE, LOCOMOTIVE/RVT 82) INTO THE LOCOMOTIVE SHOP BUILDING (UNITS NORMAL PARKING LOCATION WHEN NOT IN ACTIVE USE) ON THE WEST SHOP TRACK, WITH THE LONG HOOD END POINTED IN THE FORWARD (NORTHWARD) DIRECTION. EMPLOYEE STOPP ED THE LOCOMOTIVE APPROXIMATELY 1-2 FEET SHORT OF THE NORMAL LOCOMOTIVE PARKING LOCATION (EXTREME NO RTH END OF THE WEST SHOP TRACK). THE GENERAL MANAGER (UTILITY TRAINMAN/BRAKEMAN) WAS PROVIDING HAND SIGNALS TO THE OPERATOR TO INDICATE THE PROPER STOP LOCATION. AFTER THE INITIAL STOP, IT IS BELIEVED THE OPERATOR MAY HAVE INADVERTENTLY DISTURBED THE THROTTLE HANDLE FROM THE IDLE POSITION. THE LOCOM OTIVE BEGAN TO LOAD AND MOVED FORWARD 1-2MPH ANOTHER APPROXIMATELY 18 FEET, MOVING OFF OF THE NORTH END OF THE TRACK AND THROUGH THE NORTH WALL OF THE LOCOMOTIVE SHOP BUILDING BEFORE BEING BROUGHT TO A FINAL STOP. FRONT TWO AXLES CAME TO REST BEYOND THE END OF THE TRACK (I.E. DERAILED).",False,True,False,False,False,0.0
741,19,4,BNSF,41,KLAMATH FALLS,KLAMATH,Y-KIF272-2-23A DERAILED 2 RAIL CARS AND 2 LOCOMOTIVES DUE TO DEFECTIVE OR MISSING CROSS-TIES ON CUST OMER OWNED AND MAINTENANCE TRACK. NO HAZMAT RELEASED.,False,True,False,False,False,0.0
742,19,10,BNSF,41,PORTLAND,MULTNOMAH,"FOREIGN UPRR TRAIN F-MTTSEO-08 DERAILED 1 LOCOMOTIVE IN YARD TRACK 705. AFTER PULLING THROUGH AN IMP ROPERLY LINED SWITCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WIT H RESTRICTED SPEED IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE R ELEASED.",False,True,False,False,False,0.0
743,19,5,UP,41,STANFIELD,UMATILLA,EAST END JOB PINNED OFF A SINGLE CAR FOR BOWL 26 THEN PINNED OFF 3 LOADS FOR BOWL 26 - THERE WAS NO HEEL OR SECURED CAR IN 26 AT THIS TIME AND THE 4 CARS ROLLED OUT WEST END OF 26 INTO SIDE ON CUT BEI NG PULLED OUT OF BOWL 29. THIS CAUSED THE WEST CAR IN BOWL 26 TO DERAIL AND LAY DOWN ON ITS SIDE.,False,True,False,False,False,0.0
744,19,5,UP,41,PORTLAND,MULTNOMAH,"YPD67R-18, SW1 RAN THROUGH THE 40 SWITCH AND THEN PITCHED CONTROL TO THE FOREMAN WHO SHOVED BACK 3/4 OF A CAR TO THE CLEARANCE CONE. FOREMAN PITCHED CONTROL BACK TO SW1 AND AS THE FOREMAN WAS RIDING THE REAR CAR HE COULD SEE A CAR TIPPING AWKWARDLY AND TOLD SW1 TO STOP THE MOVMENT, RESULTING IN 5 C ARS DERAILING.",False,True,False,False,False,0.0
745,19,1,BNSF,40,TULSA,TULSA,MECHANICAL EMPLOYEES DERAILED 1 LOCOMOTIVES WHILE OPERATING LIGHT POWER IN YARD TRACK 1604 DUE TO TR ACK BROKEN RAIL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
746,19,1,BNSF,40,ENID,GARFIELD,"Y-ENI1021-24 DERAILED 2 RAILCARS AND 1 LOCOMOTIVE IN YARD TRACK 8199. AFTER PULLING THROUGH AND IMPR OPERLY LINED SWITCH, SUBSEQUENTLY DERAILED UPON CHANGING DIRECTIONS. CAUSE IS FAILURE TO COMPLY WITH RESTRICTED SPEED IN TURN RUNNING THROUGH AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIAL WAS RELE ASED.",False,True,False,False,False,0.0
747,19,1,BNSF,40,TULSA,TULSA,HUMP CREW WAS IN THE PROCESS OF HUMPING CARS WHEN THE SYSTEM IDENTIFIED THAT TRACK 2025 HAD CARS IN THE FOUL. THE OPERATOR OVERRODE THE SYSTEM ALLOWING CARS TO ROLLS TO TRACK 2026 WHICH CAUSED THE CA RS TO IMPACT AND DERAIL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
748,19,2,KRR,40,HUGO,CHOCTAW,"ON SATURDAY, FEBRUARY 16, 2019 AT 1200 ONE LOADED LUMBER RAILCAR WAS DISCOVERED TO HAVE BEEN SET ON FIRE EAST OF THE HUGO YARD. THE LOCAL FIRE DEPARTMENT CONTACTED ARDC WHO INFORMED TRAINMASTER MASTER SON AND MYSELF OF THE SITUATION. THE FIRE APPEARED TO HAVE BEEN STARTED IN THE MIDDLE OF THE CAR AND SPREAD FROM THERE. THE FIRE CAUSED THE CAR TO BUCKLE AND COLLAPSE IN THE CENTER.",False,False,True,False,False,0.0
749,19,1,KRR,40,BOKCHITO,BRYAN,"CREW WAS TRAVELING EAST NEAR IN BOKCHITO, OK. TRAVELING AT 22 MPH WHEN THE ENGINEER FELT THE TRAIN J OLT AND GO INTO EMERGENCY. ONCE THE TRAIN CAME TO A COMPLETE STOP THE CONDUCTOR BEGAN WALKING TOWARD S THE REAR OF THE TRAIN WHEN HE WAS APPROACHED BY THE LOCAL POLICE NOTIFYING HIM OF THE DERAILMENT.",False,True,False,False,False,0.0
750,19,6,GNBC,40,BESSIE,WASHITA,CL121 WAS PULLING LOADS FRO THE WEST ELEVATOR IN BESSIE. HEAVY RAIN IN THE PREVIOUS FEW DAYS HAD MAD E THE GROUND SOFT. THE CROSS TIES WERE NOT SUFFICIENT TO HANDLE THE LOAD AND SOFT GROUND.,False,False,True,False,False,0.0
751,19,1,TSU,40,SAPULPA,CREEK,"TRAIN HELD 5 EMPTY RAIL CARS, PREPARING TO PULL 9 LOADED CARS FROM THE CONNECTION. CREW PULLED PAST THE WEST TRACK SWITCH AND SHOVED SOUTH DOWN THE MAINLINE. CARS HAD DERAILED ON THE PULL, AND CREW SHOVED BACK NORTH UP THE MAINLINE BEFORE ENGINEER AND CREW WERE AWARE OF THE CARS DERAILING.",False,True,False,False,False,0.0
752,19,7,ATK,42,PHILADELPHIA,PHILADELPHIA,"PHILADELPHIA WORK TRAIN CREW KP-702 SHOVING 14 STONE CARS NORTH FROM MH LEAD INTO 21 TRACK. WHILE SH OVING THE 5TH,6TH &7TH CAR ROLLED OVER ON ITS SIDE. 3RD CAR DERAIL THE NORTH AXLE DUE TO UNEVEN LOAD OF STONE INSIDE CARS. THE CAUSE IS THE UNEVEN LOAD OF STONE INSIDE 3 CARS CAUSING CARS TO ROLL OVE R WHILE IN A CURVE.",False,True,False,False,False,0.0
753,19,6,URR,42,DUQUESNE,ALLEGHENY,REMOTE CREW WAS SHOVING A 21 CAR TRAIN NORTH ON 8 CLASS WHEN THE FIFTH CAR FROM THE LEAD DERAILED AT THE 8 CLASS SWITCH DUE TO THE STOCK RAIL AND SWITCH POINT BEING WORN. THIS CAUSED SIX OTHER CARS TO ALSO DERAIL.,False,True,False,False,False,0.0
754,19,5,NS,42,CRESSON,CAMBRIA,"N63C229 TRAVELING WEST WITH 2 UNITS, 0 LOADS, 0 EMPTIES, AND 0 TONS ON CRESSON RUNNER DERAILED 1 UNI T (NS 6300).",False,True,False,False,False,0.0
755,19,3,SEPA,42,CROYDON,BUCKS,THE CREW WAS ON CROYDON STATION WHEN THEY FIRST NOTICED SMOKE THEN A FIRE HAD STARTED ON THE SECOND TRUCK OF THE FIRST. THE TRACTION MOTOR WAS ON FIRE. THERE WERE APPROXIMATELY 200 PASSENGERS ON THE T RAIN AND WERE EVACUATED TO CROYDON PLATFORM. TRAIN 719 THEN CUT THE TRACTION MOTOR OUT AND SECURED T HE PANTOGRAPH AND PRECEDED TO THE YARD.,False,False,True,False,False,0.0
756,19,6,NS,39,PORTSMOUTH,SCIOTO,"PULLING INTO YARD AT PORTSMOUTH DERAILED REAR ENGINE NS 9132 REAR TRUCKS DERAILED, 4 CARS 2 ON SIDE AND 1 LEANING; SPILL LINE 2 HKRX 600236 4 TONS LINE 3 HKRX 600238 800LBS SCOULAR GRAIN;",False,True,False,False,False,0.0
757,19,6,NS,39,EVENDALE,HAMILTON,**** INDIANA OHIO RAILWAY TRAIN **** IORY 11 FAILED TO PROPERLY PROTECT THEIR SHOVE MOVEMENT INTO SH 11 COLLIDING WITH TRAIN T46T811 THAT WAS STATIONARY IN ADJACENT TRACK SH12 RESULTING IN DERAILMENT.,False,True,False,False,False,0.0
758,19,1,NS,39,BELLEVUE,ERIE,LB41 WAS HUMPING CARS WHEN DERAILMENT OCCURRED DUE TO BUILT UP TREAD ON ALL WHEELS OF NS 300312.,False,True,False,False,False,0.0
759,19,6,IORY,39,EVENDALE,HAMILTON,"WHILE SETTING OUT A BAD ORDER CAR AT NS INTERCHANGE, THE CONDUCTOR MISTAKENLY LINED ONE END OF A CRO SSOVER AWAY FROM THE INTENDED ROUTE AND INTO THE SIDE OF A STANDING TRAIN. THE CONDUCTOR THEN BACKED HIS TRAIN UP INTO THE SIDE OF THE STANDING TRAIN, CAUSING A SIDE COLLISION, DERAILING 3 CARS. CREW MADE A STANDING CUT ON THE 7TH CAR (BAD ORDER) IN 10 TRACK WITH INTENTIONS OF SETTING IT OUT IN TRAC K 11. THE CONDUCTOR IMPROPERLY LINED THE 11/CROSSOVER SWITCH INTO A STANDING TRAIN ON TRACK SH12.",False,True,False,False,False,0.0
760,19,12,NYA,36,NEW YORK -QUEENS,QUEENS,"YARD CREW WAS SHOVING 20 LOADED STONE HOPPERS EAST OFF OF TRACK 5 WEST, WHEN THE 15TH CAR IN THE CON SIST, HZGX 8732, DERAILED ITS TRAILING WHEELS ON THE EAST END OF 5 WEST. THIS CAUSED ALL WHEELS ON THE 16TH CAR, HZGX 8693, AND THE LEAD FOUR WHEELS OF THE 17TH CAR, HZGX 8714 TO DERAIL. AS HZGX 869 3 DERAILED, IT MADE CONTACT WITH STANDING EQUIPMENT ON TRACK 4 WEST, CAUSING SIDESWIPE DAMAGE TO HOP PER CARS GACX 14499 AND GACX 680144. INVESTIGATION REVEALED THAT AN INTERNAL DEFECT IN THE RAIL RE SULTED IN A BROKEN RAIL.",False,True,False,False,True,0.0
761,19,11,MNCW,36,CROTON ON HUDSON,WESTCHESTER,COUPLER DAMAGE OCCURRED WHILE THE HTS-7 SWITCHING CREW WAS MAKING A HITCH ON TRACK 88 IN HARMON YARD . THE CONDUCTOR WAS DIRECTING THE MOVE FROM THE LEADING END IN CAR 4297 AT THE TIME THE COUPLING WAS ATTEMPTED.,False,False,True,False,True,0.0
762,19,3,ATK,36,RHINECLIFF,DUTCHESS,"BEARING FAILURE: TRAIN 234 WAS DELAYED AT RHINECLIFF AFTER ARRIVING ON #1 TRACK SETTING OUT BUSINES S CLASS C/48167 (LAST CAR IN CONSIST). UPON ARRIVING INTO RHINECLIFF, THE BEARING WAS SMOKING. THE JOURNAL ON THE EAST END TRUCK MELTED A TEMPIL-STIK. THE CREW WAS INSTRUCTED TO CUT THE CAR FROM TH E TRAIN AND SECURE IT WITH A HANDBRAKE AND CHOCKS.",False,False,True,False,False,0.0
763,19,6,CSX,36,SELKIRK,ALBANY,Y19822 CREW FAILED TO PROTECT THE LEADING END OF THEIR LITE ENGINE MOVEMENT WHEN SHOVING WEST ON DRI LL 3 RESULTING IN A SIDE SWIPE DERAILMENT AT THE 9 CROSS-OVER WITH THE Y19722 CUT THAT WAS BEING PUL LED OUT OF TRACK 055 ON TO DRILL 1.,False,True,False,False,False,0.0
764,19,1,LI,36,SMITHTOWN,SUFFOLK,"PORT JEFFERSON- NO. 652 ENGINE 520 REPORTS STRIKING A DEER WEST OF SMITHTOWN PASSENGER STATION. OM 0 7-11-2019, UPDATED ENGINEERING COSTS MAKES THIS CASE FRA REPORTABLE.",False,False,True,False,False,0.0
765,19,5,LI,36,SPEONK,SUFFOLK,"EQUIPMENT TRAIN 5785 WAS STRUCK BY EASTBOUND TRAIN 8700. 5785 WAS STOPPED ON THE SOUTH SIDING, CONTR OLLED SIDING, AND THE REAR OF 5785 WAS FOULING THE SK2 INTERLOCKING. DUE TO A SIGNAL MALFUNCTION, TR AIN 8700, WHICH WAS OPERATING ON MONTAUK SINGLE TRACK WAS GIVEN A SIGNAL TO PROCEED ON SK2'S WESTWAR D LIMITS EASTBOUND SIGNAL AND STRUCK 5785 AT APPROXIMATELY 30M PH. TRAIN 5785 DERAILED UPON IMPACT A ND WAS OPERATED WEST FOR APPROXIMATELY 2000’ CAUSING DAMAGE TO TRACK AND SWITCHES. ON 07-26-2019, DA TA IN BOXES 2, 2A, 2B REMOVED. ON 08-01-2019, UPDATED BOX 21 TO SINGLE MAIN TRACK. ON 08-22-2019, BO X 6 UPDATED TO 0302 AM.",True,True,False,False,True,0.0
766,19,5,LI,36,SPEONK,SUFFOLK,"EQUIPMENT TRAIN 5785 WAS STRUCK BY EASTBOUND TRAIN 8700. 5785 WAS STOPPED ON THE SOUTH SIDING CONTRO LLED SIDING AND THE REAR OF 5785 WAS FOULING THE SK2 INTERLOCKING. DUE TO A SIGNAL MALFUNCTION, TRAI N 8700, WHICH WAS OPERATING ON MONTAUK SINGLE TRACK WAS GIVEN A SIGNAL TO PROCEED ON SK2'S WESTWARD LIMITS EASTBOUND SIGNAL AND STRUCK 5785 AT APPROXIMATELY 30M PH. TRAIN 5785 DERAILED UPON IMPACT AND WAS OPERATED WEST FOR APPROXIMATELY 2000’ CAUSING DAMAGE TO TRACK AND SWITCHES. ON 07-26-2019, DTA IN BOXES 2, 2A, AND 2B REMOVED. ON 08-01-2019, UPDATED BOX 21 TO SOUTH CONTROLLED SIDING. ON 08-22-2 019, BOX 6 UPDATED TO 0302 AM.",True,True,False,False,True,0.0
767,19,2,CSX,36,BUFFALO,ERIE,THE Q56102 WAS GIVEN PERMISSION BY THE YARDMASTER TO TRAVERSE 5 YARD LEAD WITH LITE POWER AND MOVE W EST. THE YARDMASTER THEN GAVE THE Y39002 PERMISSION TO PROCEED WEST USING 6 YARD LEAD. THE Q56102 M OVING WEST TRAVELED PAST THE HAND THROWN SWITCH TOWARDS 5 YARD LEAD AND REALIZES THAT THE POWER SWIT CH CONTROLLED BY THE YARDMASTER IS AGAINST HIM AND STOPS IN THE FOUL OF 6 YARD LEAD. THE LEAD LOCOM OTIVE OF THE Y39002 THEN COLLIDES WITH THE Q56102 LEAD ENGINE DERAILING BOTH UNITS OF THE Q56102. BO TH UNITS OF THE Y39002 AS WELL AS THE FIRST CAR IN THE Y39002 CUT ALSO DERAILED. RESULTS OF THE INV ESTIGATION INDICATE THAT THE YARDMASTER FAILED TO COMMUNICATE THE PROPER ROUTING FOR MOVEMENT TO THE Q56102. THE YARDMASTER CONTROLS THE ELECTRIC SWITCHES AND HAD THE SWITCH IMPROPERLY LINED TOWARDS 6 YARD LEAD. THE YARDMASTER BELIEVED THE Q56102 WAS LINED TOWARDS 5 YARD LEAD BECAUSE HE THOUGHT THE Q56102 WAS ON A DIFFERENT TRACK WHEN HE GAVE Q561 PERMISSION OUT TOWARDS 5 YARD LEAD.,False,True,False,False,False,0.0
768,19,9,LI,36,HOLLIS,QUEENS,"WHILE SHOVING EAST, YFD-201 DERAILED 3 STONE CARS WITHIN HOLBAN YARD.",False,True,False,False,False,0.0
769,19,2,LI,36,RICHMOND HILL,QUEENS,"CAB CAR 5002 ROLLED EAST FROM FIVE RECEIVING AND DERAILED OVER A SPLIT DERAIL AT THE EAST END OF JAM AICA RECEIVING YARD. ON 07-11-2019, UPDATED ENGINEERING COSTS MAKES THSI CASE FRA REPORTABLE.",False,True,False,False,False,0.0
770,19,3,MNCW,36,NEW YORK -BRONX,BRONX,VAC TRUCK TC 10505 COLLIDED WITH THE TC 4006 ON TRACK 1 JUST NORTH OF THE 1S SIGNAL AT CP-106,False,False,True,False,False,0.0
771,19,3,CSX,36,SAUGERTIES,ULSTER,Q26127 HAD AN OPEN DOOR WHICH STRUCK THE LEAD ENGINE ON THE Q15826 DAMAGING CSXT 935.,True,False,False,False,False,0.0
772,19,3,MNCW,36,PAWLING,DUTCHESS,"TRAIN 956 WAS TRAVELING SOUTH ON TRACK 1 OPERATING AT CORBIN ROAD CROSSING WHEN IT MADE CONTACT WITH THE DETACHED TRAILER OF A TRUCK. REGARDING THE RAILROAD EMPLOYEE COUNTS, THERE WERE FIVE EMPLOYEES ON BOARD, TWO WERE CREW MEMBERS WORKING THE TRAIN, TWO WERE DEADHEADING EMPLOYEES, AND ONE WAS AN O FF-DUTY EMPLOYEE COMMUTING TO/FROM WORK. THE INJURED EMPLOYEES WERE NOT THE TRAIN CREW. THERE COULD BE ANY NUMBER OF ON-DUTY EMPLOYEES THAT ARE USING THE TRAIN FOR COMMUTATION. THE GUIDE STATES THAT DEADHEADING EMPLOYEES SHOULD BE SHOWN AS ON-DUTY BUT THEY’RE NOT PART OF THE “NUMBER OF CREW MEMBER S.”",False,False,True,False,False,0.0
773,19,5,LI,36,FARMINGDALE,NASSAU,TRAIN 2062 STRUCK A TRACTOR TRAILER AT MERRITTS ROAD CROSSING. THE TRACTOR TRAILER TRUCK HAD BEEN ST OPPED WITH THE CAB OF THE TRUNK OCCUPYING THE CROSSING PAD WHEN THE GATE CAME DOWN BETWEEN THE CAB A ND THE TRAILER OF THE VEHICLE. DRIVER ABANDONED VEHICLE PRIOR TO IT BEING STRUCK BY THE TRAIN.,True,False,False,False,False,0.0
774,19,4,BPRR,36,MACHIAS,CATTARAUGUS,SIBF EXPERIENCED AN UNDESIRED EMERGENCY AND UPON WALKING THEIR TRAIN NOTICED THE 25TH CAR HAD A BURN T JOURNAL CAUSING A DERAILMENT,False,True,False,False,False,0.0
775,19,1,NJTR,36,NEW YORK NEW YORK,NEW YORK,TRAIN #311 DEPARTING TRACK #8 IN NY PENN STATION REPORTED POWER INTERRUPTION AND DAMAGE TO THE B-END COLLECTOR HEAD ON PANTOGRAPH LOCATED ON ENGINE #4624.,False,False,True,False,True,0.0
776,19,8,LI,36,NEW YORK NEW YORK,NEW YORK,"SPLIT-RAIL-DERAIL SWITCH 109 WAS DAMAGED AFTER PJ1245X WAS BACKED THROUGH IT IMPROPERLY POSITIONED T RAILING POINT, AFTER RECEIVING AUTHORIZED PERMISSION FROM THE BLOCK OPERATOR TO REVERSE WITHOUT FIRS T ENGAGING ADEQUATE PROCEDURAL CONTROLS.",False,True,False,False,True,0.0
777,19,3,UP,32,BEOWAWE,EUREKA,"MRVNPP-01, LEAD LOCOMOTIVE UP5929, WAS TRAVELING EAST ON MAIN TRACK 2 WHEN IT STRUCK A THOMAS PETROL EUM TRAILER THAT THE DRIVER DID NOT PULL CLEAR OF THE TRACK BEFORE STOPPING WHILE TRAIN WAS APPROACH ING. TRAILER RUPTURED RELEASING APPROXIMATELY 4,000 GALLONS OF DIESEL FUEL ONTO THE GROUND. NO INJ URIES WERE REPORTED FROM EITHER OF THE TRAIN CREW OR THE DRIVER OF THE TRUCK.",True,False,False,False,False,0.0
778,19,7,UP,32,LAS VEGAS,CLARK,"LUM55-26, LEAD LOCOMOTIVE UP4503, CREW WAS SETTING OUT CARS IN INDUSTRY. AS THE CREW SHOVED IN TO SE TOUT CARS ON THE INBOUND TRACK THE CARS ON THE LOADING TRACK WERE AT CLOSE CLEARANCE. THE CREW SHOVE D IN AND SIDE SWIPED THE CAR ON THE LOADING TRACK. AS THEY WERE PULLING OUT THE CAR ON THE LOADING T RACK WAS PULLED OFF THE RAIL BY THE CUT PULLING OUT AND TURNED SIDEWAYS, CAUSING THE OTHER CARS TO D ERAIL.",False,False,True,False,False,0.0
779,19,7,UP,32,ELGIN,LINCOLN,"THE MNPWCB-08, LEAD LOCOMOTIVE UP8078, DERAILED 32 LOADED AUTORACKS. NEITHER EMPLOYEE DID ANYTHING W RONG, DUE TO THE TRAIN MAKE-UP, THE AUTO RACKS IN MIDDLE OF THE TRAIN AND GRADE WITH DEGREE OF CURVE S CAUSED A SLACK ACTION EVENT.",False,True,False,False,False,0.0
780,19,7,ATK,34,NEWARK,ESSEX,"PANTOGRAPH/CATENARY: NJTR TRAIN 7880 REPORTED STRIKING A CATENARY WIRE, MP 10.5, EAST OF HUNTER INT ERLOCKING ON TRACK 1. THE COMMUTER CAME TO A STOP ON `A` TRACK AT THE HOME SIGNAL. NJTRS EQUIPMENT DAMAGE IS $39,266.00.",False,False,True,False,True,39266.0
781,19,7,ATK,34,HAMILTON SQUARE,MERCER,AT APPROXIMATELY 2:45 PM A CATENARY CAR TCA13001 ON #2 TRACK CAUGHT FIRE WHILE PERFORMING MAINTENANC E WORK EAST OF HAMILTON STATION AT MP 53.0. THE CAUSE OF THE FIRE HAS NOT BEEN DETERMINED. 07/18/1 9 A-REPORT UPDATE: ESTIMATED DAMAGE IS $3.5 MILLION. AMTRAK IS STILL COLLECTING INFORMATION ON THI S EVENT.,False,False,True,False,True,3.5
782,19,7,NJTR,34,HOBOKEN,HUDSON,YH-19 OPERATED THROUGH IMPROPERLY LINED SWITCH #1071 AFTER CONDUCTOR OPERATED SWITCH #1074 UNDER THE F-END TRUCK OF LITE ENGINE #4502 CAUSING L2 AND R2 WHEELS TO DERAIL WHILE LINING ROUTE TO TRACK #11 8,False,True,False,False,False,0.0
783,19,7,NJTR,34,NEWARK,ESSEX,"NJTR TRAIN #7880 ENROUTE EAST ON TRACK 1 WITHIN HUNTER INTERLOCKING STRUCK TWOWIRES CAUSING PANTOGRA PH ON ENGINE #4640 TO BE COMPLETELY TORN OFF ACCOUNT BROKEN INSULATOR, BROKEN MESSENGER WIRE AND BRO KEN AUXILLARY WIRE.",True,False,False,False,False,0.0
784,19,7,CRSH,34,NEWARK,ESSEX,FOI8 SHOVING TO TRACK 14 CAR DERAILED ON FROG,False,True,False,False,False,0.0
785,19,4,NJTR,34,NETCONG,MORRIS,DOVER EXTRA #4212 OPERATING WITH ONE ENGINE LONG NOSE EAST OPERATED OVER DERAIL 3093A IN THE DERAILI NG POSITION CAUSING THE FIRST AXLE OF ENGINE #4212 TO DERAIL. CONDUCTOR WAS NOT ON THE LEADING END O F THE MOVEMENT.,False,True,False,False,False,0.0
786,19,9,CRSH,34,JERSEY CITY,HUDSON,CONDUCTOR DID NOT CORRESPOND CROSS OVER SWITCH AND RAN THROUGH IT - MADE MULTI MOVES OVER SWITCH,False,False,True,False,False,0.0
787,19,8,PATH,34,HARRISON,HUDSON,ON FRIDAY AFTERNOON AT APROXIMATELY 4:00 PM 3 SWITCHMEN WERE PULLING CARS OUT OF THE PIT TRACK 9 EAS T AT THE HARRISON CAR MAINTENANCE FACILITY. 2 CARS (5117-5645) WERE OPERATED OUT OF THE BUILDING WIT H THE OVERHEAD TROLLEY 600 V POWER CORD STILL ATTACHED TO CAR 5645. THE CORD WAS RIPPED FROM ITS MOV ABLE GUIDEWAY AND PULLED OUT SIDE OF THE BUILDING CAUSING DAMAGE TO THE OVERHEAD POWER TROLLEY AS WE LL AS DAMAGE TO CAR 5645 WHEN THE TROLLEY ATTACHMENT TIP WAS BROKEN OFF.,False,False,True,False,True,0.0
788,19,6,NJTR,34,KEARNY,HUDSON,YARD CREW #MM-40 ENROUTE WEST ON TRACK #8 WITH CONDUCTOR PRECEDING MOVE DERAILED ENGINE #1001 AFTER OPERATING THROUGH IMPROPERLY LINED SWITCH #2220. CREW FAILED TO ENSURE HAND OPERATED SWITCH #2220 WA S PROPERLY LINED PRIOR TO MOVE.,False,True,False,False,False,0.0
789,19,6,NJTR,34,PARK RIDGE,BERGEN,TRAIN #1216 STRUCK A TRESPASSER WHILE ENROUTE EAST NEAR MP 24 CAUSING SUBSEQUENT DAMAGE TO CAB CAR # 6709,True,False,False,False,True,0.0
790,19,4,NS,34,PHILLIPSBURG,WARREN,"NS H76H527 OPERATING WEST ON FOREIGN RAILROAD (DOVER AND DELAWARE RIVER RAILROAD) WASHINGTON LINE WI TH 5 UNITS, 4 LOADS, AND 2 EMPTIES STRUCK THE SOUTH MAIN STREET BRIDGE WITH CAR FBOX 505641.",True,False,False,False,False,0.0
791,19,4,PATH,34,JERSEY CITY,HUDSON,A 7 CAR CONSIST 5785-5127-5710-5720-5101-5151-5753 WAS OPERATED FROM 3 TRACK AT JOURNAL SQUARE INTO 8 TRACK IN THE A YARD AT JOURNAL SQUARE IN ORDER TO TURN THE TRAIN FOR ITS NEXT SUCCESIVE INTERVAL T O 33RD STREET. AT APROXIMATELY 8:13 AM THE ENGINEER OPERATING THE CONSIST FAILED TO CONTROL THE SPEE D OF THE TRAIN AND IMPACTED THE BUMPING BLOCK ON THE WEST END OF 8 TRACK AT APROXIMATELY 9 MPH. MAXI NUM ALLOWABLE SPEED IN JOURNAL SQUARE 8 YARD IS 8MPH. THERE IS INDICATION FROM THE TRAINS EVENT RECO RDER THAT THE ENGINEER WAS NOT OPERATING IN ACCORDANCE WITH RULE 318 OF THE PATH BOOK OR RULES REQUI RING ENGINEERS TO OPERATE IN A MANNER SUCH THAT THEY ARE PREPARED TO STOP SHORT OF THE BUMPING BLOCK OR AT THE APPROPRIATE CAR STOP MARKER. THE BUMPING BLOCK WAS DISLODGED FROMS ITS NORMAL LOCATION AL ONG WITH 3 RAILROAD TIES THAT SUPPORTED IT UNDERNEATH. DAMGED OCCURED TO THE #1 END OF THE DRAUGHT G EAR IN OPERATING CAR 5785 AS WELL AS DAMAGE TO A SIGNAL LAMP ON THE BUMPING BLOCK AND ADJACENT ATC W IRE SUPPORT POLE. INVESTIGATION IS ACTIVE AND LOOKING AT POSSIBLE MECHANICAL FAILURES IN THE TRAIN C ONSIST AS WELL. TRAIN CONDUCTOR WHO WAS ABOARD OPERATING CAR 5785 AT THE TIME OF THE INCIDENT IS CLA IMING A BACK INJURY AS A RESULT OF THE INCIDENT.,False,False,True,False,True,0.0
792,19,10,ATK,34,HARRISON,HUDSON,NJTR TRAIN 5737 OPERATING AS DEADHEAD EQUIPMENT REPORTED DERAILED ON #14 TRACK AT MP 7.5 REA INTERLO CKING.,False,True,False,False,False,0.0
793,19,10,CRSH,34,NEWARK,ESSEX,"TBOX 670418, NYC 901000, AND NYC 901006 WERE DAMAGED WHEN TBOX 670418 WAS HUMPED AT 1.5MPH OVERSPEED AND COLLIDED WITH STANDING CARS.",False,False,True,False,True,0.0
794,19,10,CRSH,34,NEWARK,ESSEX,YARDMASTER HUMPED LOADED GATX 225385 INTO CLEAR TRACK 054 AND IT ROLLED THROUGH THE INERTS AND SIDES WIPED ENGINE NS 1072 ON TRACK 046.,False,False,True,False,False,0.0
795,19,7,CRSH,34,BAYONNE,HUDSON,EJR CREW WAS PULLING EAST AFTER RUNNING THROUGH A SWITCH RESULTING IN CTCX 729143 AND TCBX 251857 BE ING DERAILED,False,True,False,False,False,0.0
796,19,2,CRSH,34,CAMDEN,CAMDEN,"LOAD SHIFTED AND BLEW OUT END OF CAR, STRIKING ANOTHER CAR.",False,False,True,False,False,0.0
797,19,8,PATH,34,JERSEY CITY,HUDSON,AT 4:30 PM A PA4 WORK CAR DERAILED NEAR 75 SWITCH IN C-YARD IN JERSEY CITY NEW JERSEY. A SWITCHMAN H AD PREVIOUSLY OPERATED CONSIST 865-867-801-873-F53-F25 WEST FROM TRACK 33 AND RAN THROUGH 75 SWITCH WITH THE WESTERN MOST TRUCK OF OPERATING CAR 865. THE SUBSEQUENT MOVE EAST CAUSED THE WESTERN MOST T RUCK TO TRAVEL DOWN S TRACK SINCE THE SWITCH HAD BEEN SPLIT AND THE REMAINDER OF THE CONSIST TRAVELE D DOWN THE C-YARD LEED UNTIL S TRACK AND THE LEAD TRACK DIVERGED AND CAUSED THE DERAILMENT OF CAR 86 5. SWITCH 75 HAD BEEN THROWN INTO THE NORMAL POSITION FOR THE 4:10 LIGHT TRAIN TO TRAVEL EAST ONTO T HE MAIN LINE FROM S2 AND THEN NEVER PUT BACK INTO THE REVERSE POSITION BY THE TOWER OPERATOR FOR THE C YARD SWITCHING MOVES TO CONTINUE.,False,True,False,False,False,0.0
798,19,9,ATK,34,TRENTON,MERCER,PANTOGRAPH/CATENARY: TRAIN 2160 STOPPED ON 2 TRACK JUST WEST OF HAM INTERLOCKING WITH A BROKEN PANT OGRAPH ALARM ON THE REAR PC 2033. THE CREW INSPECTED AND COULD ONLY DETERMINE THE PANTOGRAPH WAS DO WN. ET FOUND A PART OF THE PANTOGRAPH WAS DISLODGED.,False,False,True,False,False,0.0
799,19,9,ATK,34,PRINCETON JUNCTION,MERCER,PANTOGRAPH/CATENARY: TRAIN 2258 STOPPED ON #1 TRACK AT MP 47.1 DUE TO A BROKEN PANTOGRAPH ALARM ON REAR PC/2008. THE CREW INSPECTED AND FOUND THAT THE PANTOGRAPH WAS DAMAGED AND NOT SEATED. AT APPR OXIMATELY 9:23 PM THE DAMAGED PANTOGRAPH WAS REMOVED ON PC/2008 AND THE AC PLATE WAS CANCELLED.,False,False,True,False,True,0.0
800,19,10,PATH,34,NEWARK,ESSEX,"A PRELIMINARY INVESTIGATION SHOWS A BROKEN INSULATED JOINT AT SIGNAL L18X AND A TRACK GAUGE MEASUREM ENT OF 59 INCHES. CONSIST 5808-5111-5120-5723-5784-5751-5611-5727 WAS TURNING FOR SERVICE IN NEWARK SOUTH STREET YARD. AFTER THE AIR TEST WAS COMPLETED THE TRAIN WAS OPERATED IN AUTOMATIC MODE INTO NE WARK PENN STATION FOR ITS NEXT INTERVAL. 6 FEET EAST OF THE L18X IF THE #4 AXEL OF CAR 5751 DERAILED AND WAS DRAGGED APROXIMATELY 2000 FEET INTO THE STATION WHERE THE TRAIN WAS PROPERLY BERTHED IN AUT OMATIC MODE. DAMAGE TO THE TRACK BED OCCURED FROM THE WHEELS OF THE #4 AXEL RIDING IN AND OUTSIDE TH E GAUUGE. CAR 5751 STRUCK C PLATFORM IN NEWARK AND DAMAGE THE CAR BODY AND APROXIMATELY 250 FEET OF PLATFORM. THE TRACK PACK GEAR BOX WAS ALSO DAMAGED ON CAR 5751.
REPORT AMENDED ON 10-23-2019 TO S HOW THE AMENDED ESTIMATE OF REPAIRS.",True,True,False,False,True,0.0
801,19,10,BNSF,31,LINCOLN,LANCASTER,Y-LIN5911-01 DERAILED 1 LOCOMOTIVE WHILE PULLING OUT OF YARD TRACK 915 DUE TO FAILURE TO COMPLY WITH RESTRICTED SPEED IN-TURN RUNNING THROUGH AN IMPROPERLY DERAIL. NO HAZARDOUS MATERIALS WERE RELEASED .,False,True,False,False,False,0.0
802,19,9,NJTR,34,RIVER EDGE,BERGEN,"TRAIN #1610 STRUCK AN OCCUPIED AUTOMOBILE THAT ENTERED MAIN STREET CROSSING AND WENT UNDER THE GATE IN PATH OF TRAIN. 2 INJURIES. OTHER WARNING DEVICES INCLUDE STOP LINES, RR X-ING SYMBOLS, ENS SIGN D ISPLAYED OTHER MUTCD SIGNS. DRIVER CITED FOR RECKLESS DRIVING AND DISREGARDING GATE.",True,False,False,False,False,0.0
803,19,3,NJTR,34,KEARNY,HUDSON,TRAIN #5725 OPERATED FROM ELECTRIFIED TERRITORY INTO NON-ELECTRIFIED TERRITOR WITH PANTOGRAPH RAISED ON #4521 WHILE ENROUTE WEST OFF TRACK #C-7 AFTER TRAVE SING SWITCH #3014 IN NORMAL POSITION.,False,False,True,False,False,0.0
804,19,3,NJTR,34,PATERSON,PASSAIC,NS TRAIN #H55H616 OPERATING WEST DURING SHOVING MOVEMENT OPERATED OVER A FIXEDDERAIL RESULTING IN DE RAILMENT OF NS 5616.,False,True,False,False,False,0.0
805,19,8,UP,31,NORTH BEND,DODGE,"THE MSSNP-20 WAS SCHEDULED TO MAKE A 57 CAR REAR END PICKUP AT NORTH BEND. THEY STOPPED AT 1138 ONCE CLEAR OF THE SWITCH. THEY SHOVED EAST 1180 FT WITH THE HIGHEST NOTCH BEING 2. COUPLING WAS MADE AT 1.2MPH AND WAS STRETCHED. AS THEY CONTINUED WEST 460' OUT OF TRACK 148, THEY DERAILED AT THE COMEBAC K PRIOR TO THE MAINLINE SWITCH. MSSNP-20 PULLED OUT OF THE SIDING AT 5.8MPH, WHEN THE CONDUCTOR NOTI CED THE CARS ROCKING. 4 RAILCARS DERAILED DUE TO WIDE GAGE DUE TO TIE CONDITION.",False,True,False,False,False,0.0
806,19,10,UP,31,NORTH PLATTE,LINCOLN,"YNP10R-13, LEAD LOCOMOTIVE UPY327, UPON SHOVING INTO 309 WITH THE MNPPD-13, THE CUT SEPARATED AND EA ST CAR AT POINT OF SEPARATION WAS FOUND TO BE MISSING DRAWBAR. FURTHER INSPECTION, LEAD TO FINDING THE DRAWBAR OBSTRUCTING THE SOUTH PULLBACK AND BOTH UNITS DERAILED AT WEST RECEIVING TRANSFER SWITCH .",False,True,False,False,False,0.0
807,19,10,UP,31,KEARNEY,BUFFALO,"GSEIKR-21 CONDUCTOR SHOVED REAR OF TRAIN TO MP3 OF KEARNEY INDUSTRIAL LEAD AND SECURED THE REAR 77 C ARS. THEY BEGAN TO PULL THE HEAD 35 CARS DOWN TO SPOT AND NOTICED SOMETHING DID NOT LOOK RIGHT. TH E CONDUCTOR TOLD THE ENGINEER TO STOP. WHEN THE CONDUCTOR WENT TO THE HEAD END, HE DISCOVERED 7 CAR S DERAILED AFTER THE SWITCH. INDUSTRY MAINTAINS TRACK",False,True,False,False,False,0.0
808,19,10,BNSF,31,LAKESIDE,SHERIDAN,E-CLSATM0-77 IMPACTED THE E-CEBNAM0-71 WHILE TRAVERSING MAIN 2 TRACK DUE TO FAILURE TO COMPLY WITH R ESTRICTED SPEED. RESULTED IN 1 LOCOMOTIVE AND 4 RAILCARS DERAILED. APPROXIMATELY 20 GALLONS OF TRACT ION MOTOR OIL WAS RELEASED FROM A DP LOCOMOTIVE.,False,True,False,False,False,0.0
809,19,4,UP,31,SUTHERLAND,LINCOLN,"THE CIMNA9-26, LEAD LOCOMOTIVE UP6523, WAS TRAVELING WEST ON THE SOUTH MORRILL SUB WHEN THE LEAD UNI T BLEW ITS MOTOR CAUSING FIRE AND THE CAB FILLED UP WITH SMOKE. NO DERAILMENT OR TRACK DAMAGE.",False,False,True,False,True,0.0
810,19,9,UP,31,NORTH PLATTE,LINCOLN,150 EMPTY COAL RAILCARS HAD ROLLED FROM TRACK 284 IN THE BAILEY YARD AND CAME TO A STOP BETWEEN CONT ROL POINTS B286 AND B284 ON THE BELT TRACK. DUE TO 70 PLUS MPH WINDS IN WEATHER EVENT. NO DERAILMENT .,False,False,True,False,False,0.0
811,19,9,UP,31,NORTH PLATTE,LINCOLN,YNP48R-19 FOUND 2 STACKERS DERAILED IN BOWL 51 AS A RESULT OF CROSSED DRAWBARS.,False,True,False,False,False,0.0
812,19,9,UP,31,NORTH PLATTE,LINCOLN,POWER MOVE INTO THE VAN YARD. HOSTLER PILOT CAUGHT CROSSING PLANK AND DRAGGED IT INTO SWITCH AND DER AILED ONE TRUCK ON UNIT UP5217.,False,False,True,False,False,0.0
813,19,6,BNSF,31,MASCOT,HARLAN,G-CBLBVA5-20 DERAILED 3 RAILCARS AND 1 DP LOCOMOTIVE WHILE TRAVERSING SINGLE MAIN TRACK DUE TO TRACK ALIGNMENT IRREGULAR DUE TO THERMAL MISALIGNMENT. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
814,19,6,UP,31,NORTH PLATTE,LINCOLN,2 CARS WERE FOUND DERAILED IN WEST BOWL 47 DUE TO CROSSED DRAWBARS.,False,True,False,False,False,0.0
815,19,6,UP,31,ALEXANDRIA,JEFFERSON,"CNAIM9-27, LEAD LOCOMOTIVE UP8875, WAS TRAVELING AT 48 MPH EAST BOUND ON MAIN 2 ON THE MARYSVILLE SU B WHEN THE TRAIN WENT INTO EMERGENCY AND DERAILED 24 CARS.",False,True,False,False,False,0.0
816,19,2,BNSF,31,SOUTH BEND,CASS,E-SAICAM0-03 DERAILED 1 RAILCAR WHILE TRAVERSING MAIN 1 TRACK DUE TO DEFECTIVE BRAKE CAUSED FLAT SPO TS ON WHEEL. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
817,19,1,BNSF,31,LINCOLN,LANCASTER,E-NMANAM0-05 DERAILED 1 RAILCAR WHILE PULLING OUT OF YARD TRACK 903 DUE TO MECHANICAL PERSONNEL NOT PLACING WHEELS BACK ON THE RAIL PROPERLY. NO MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
818,19,1,MRL,30,BOZEMAN,GALLATIN,LOADED COAL UNIT TRAIN DERAILED ON DESCENDING GRADE.,False,True,False,False,False,0.0
819,19,9,NS,37,CHARLOTTE,MECKLENBURG,"NS TRAIN PC01 RCL ASSIGNMENT PULLED RAN THROUGH A SWITCH, THEN MADE A REVERSE MOVE OVER THE SWITCH, DERAILING BOTH SIDES OF AXLE 1 AND 2 ON THE SECOND LOCOMOTIVE, NS 4625.",False,True,False,False,False,0.0
820,19,5,NS,37,PAW CREEK,MECKLENBURG,"221P317 HEADED EASTBOUND, DERAILED BNSF 240066 AT CHARLOTTE INTERMODAL.",False,True,False,False,False,0.0
821,19,5,NS,37,PINE HALL,STOKES,"WHILE SPOTTING THEIR TRAIN IN BELEWS CREEK, 746V822 DERAILED CAR NDYX 934291 R&L 3 AND 4, CAR NDYX 9 34300 ALL WHEELS AND TILX 420126 R&L 3 AND 4.",False,True,False,False,False,0.0
822,19,5,CSX,37,HAMLET,RICHMOND,Y10117 SHOVING A11 THRU T46 TRACK DERAILED AT THE SWITCH POINT OF T46.,False,True,False,False,False,0.0
823,19,4,NS,37,CHARLOTTE,MECKLENBURG,"PC02 PULLING WEST ON PAD 5 CONNECTOR TRACK WITH 24X1, 3438 TONS DERAILED LEAD THREE CARS",False,True,False,False,False,0.0
824,19,4,BNSF,30,LIBBY,LINCOLN,MAINTENANCE OF WAY HAD A RAILCAR ROLL OUT ON A SINGLE MAIN TRACK RESULTING IN IMPACTING A HYRAIL VEH ICLE AND OTHER MAINTENANCE OF WAY EQUIPMENT RESULTING IN THE RAILCAR AND EQUIPMENT DERAILED AND SIGN IFICANT DAMAGES. THE CAUSE WAS CUTTING OFF EQUIPMENT IN MOTION. NO HAZARDOUS MATERIALS WERE RELEASED .,False,True,False,False,False,0.0
825,19,4,BNSF,30,GREAT FALLS,CASCADE,Y-GRF2031-20 IMPACTED A CUT OF RAILCARS AND DERAILED 2 RAILCARS WHILE SHOVING INDUSTRY TRACK 494 DUE TO FAILURE TO CONTROL SHOVE MOVE IN TURN RUNNING AN IMPROPERLY LINED SWITCH. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
826,19,4,MRL,30,LIVINGSTON,PARK,CREW ON THE MRL 4305 ATTEMPTED A SHOVING MOVE INTO THE ROUNDHOUSE READY TRACK. ROUTE WAS IMPROPERLY LINED FOR TRACK 211. CREW SHOVED AND STRUCK THE MRL 4405 HELPER SET THAT WAS PARKED IN 211.,True,False,False,False,False,0.0
827,19,10,MRL,30,HELENA,LEWIS AND CLARK,FOUR CARS DERAILED WHILE MAKING AN EASTWARD SHOVE MOVE.,False,True,False,False,False,0.0
828,19,9,MRL,30,MISSOULA,MISSOULA,"MRL 401 CAME OUT OF THE WEST END OF THE SCALE TRACK, PROCEEDED EAST DOWN MIDDLE ONE AND RAN INTO THE SIDE OF U FTEFYN2 02 CAR NUMBER 47, UTLX 683045. TRAIN SPEED EXCEEDED THE MAXIMUM SPEED FOR THE FR A TRACK CLASS - CAUSE CODE H607 APPLIED (FAILURE TO COMPLY WITH RESTRICTED SPEED OR ITS EQUIVALENT N OT IN CONNECTION WITH A BLOCK OR INTERLOCKING SIGNAL).",False,False,True,False,False,0.0
829,19,8,MRL,30,MISSOULA,MISSOULA,"H PASLAU1 01 DERAILED AT MP 2.8 ON THE 10TH SUB MAIN. CAR WAS NOT UNLOADED PROPERLY LEAVING A SUBST ANTIAL AMOUNT OF PRODUCT REMAINING IN THE CAR. REMAINING PRODUCT WAS DISPROPORTIONATELY RIGHT LEAN AGAINST SOUTH SIDE OF CAR, CAUSING UNSTABLE L/V RESULTING IN DERAILMENT ON LIGHT SIDE OF CAR AS IT C AME OUT OF THE CORNER.",False,True,False,False,False,0.0
830,19,8,MRL,30,HELENA,LEWIS AND CLARK,"WHILE YARDING INTO CARTER 3, TRAIN DERAILED (EIGHT CARS).",False,True,False,False,False,0.0
831,19,8,BNSF,30,HAVRE,HILL,TRAIN X-KALPBN-9-22H FAILED TO STOP SHORT OF A DERAIL THAT WAS NOT IN THE DOWN POSITION IN YARD TRAC K 2691. TWO LOCOMOTIVES AND 1 CAR DERAILED. NO HAZMAT RELEASE.,False,True,False,False,False,0.0
832,19,10,NS,26,WAYNE,WAYNE,"NS TRAIN B18B622 WAS SHOVING EAST AND DERAILED REAR CAR NS 167428 WHEELS (R1234, L1234) WHILE MAKING A REVERSE MOVEMENT THROUGH PREVIOUS RUN THROUGH SWITCH.",False,True,False,False,False,0.0
833,19,9,NS,26,DETROIT,WAYNE,"NS TRAIN 120L617 DERAILED THE 15TH, 16TH, AND 17TH CAR IN THE CUT AFTER SHOVING 14 CARS INTO CLASS O NE. THE WHEELS ON THE EAST SET OF TRUCKS ON THE NS 487910, CLIMBED THE CLASS 2 SWITCH POINT AND PROC EEDED DOWN THE CLASS YARD LEAD.",False,True,False,False,False,0.0
834,19,12,CRSH,26,DETROIT,WAYNE,AIR HOSE SEPARATED BETWEEN ETTX 703734 AND CTTX 695133 PUTTING THE TRAIN INTO EMERGENCY AND DERAILIN G 12 CARS,False,True,False,False,False,0.0
835,19,1,NOGC,22,GRETNA,JEFFERSON,"THE CREW KICKED GATX 29834 INTO TRACK 75 AND CONTINUED TO KICK SEVERAL CARS OVER TRACKS INCLUDING TR ACK 75. ONCE DONE, THE CREW COUPLED TO TRACK 76 AND WAS PULLING OUT WHEN THE CREW NOTICED TWO CARS O N THE GROUND IN TRACK 76. CREW STOPPED TRAIN AND WALKED TRACK 76. THEY NOTICED CRDX 130023 AND UTLX 665059 DERAILED AND HAD DAMAGE TO THE CAR. THEY CONTINUED TO WALK WHERE THEY ALSO FOUND GATX 29834 A ND PROX 77253 WAS DERAILED WITH CAR DAMAGE.",False,True,False,False,True,0.0
836,19,1,NOPB,22,NEW ORLEANS,ORLEANS,"CREW WAS PULLING A LOADED OIL TRAIN ACROSS CSX OWNED TRACK. THE TWO (2) TRAILING LOCOMOTIVES DERAILE D ON NOPB OWNED TRACK PRIOR TO ENTERING CSX OWNED TRACK. THE LAST LOCOMOTIVE DAMAGED THE FLOODWALL A S IT CROSSED THROUGH THE THRESHOLD. NOPB ESTIMATED TRACK DAMAGES $4700; CSX ESTIMATED DAMAGES $12,8 45.46 (CSX TRACK: $3,138.40 AND CSX SIGNAL: $9,707.06)",False,True,False,False,True,17673.46
837,19,11,ATK,26,SANDSTONE,JACKSON,"TREE STRIKE: TRAIN 355(27) WAS DELAYED 50 MINUTES AFTER STRIKING A TREE. THE CONDUCTOR REPORTED DAM AGE TO THE DITCH LIGHT, A CRACKED WINDSHIELD, AND BROKEN WINDSHIELD WIPERS ON LOCOMOTIVE/ID4622. TWO WINDOWS WERE ALSO BROKEN IN CAFÉ CAR/58006. THERE WERE NO INJURIES TO ANY OF THE PASSENGERS.",False,False,True,False,False,0.0
838,19,1,CSX,24,CURTIS BAY,ANNE ARUNDEL,"N81024 LEFT THEIR EQUIPMENT IN FOUL BY 201 ON CP 9 AT CURTIS BAY. COAL PIER CREW SHOVED CP 8 110 CAR S WEST TO ALLOW N81024 TO GET THEIR LOCOMOTIVES IN THE CLEAR ON THE EAST END OF THE COAL COMING OFF CP 9 . AS THE COAL PIER CREW SHOVED WEST PROTECTING THE SHOVE, THEY ATTEMPTED TO STOP 10 CARS SHORT OF THE CLEARANCE POINT ON THE WEST END OF CP 8. WHEN THE OPERATOR LOCO # 5 BEGAN PUSHING THE STOP BUTTON COAL PIER PUSHER LOCO # 5S REMOTE THE SLACK RAN OUT AND DRAGGED THEM BACK ESTIMATED 635 FEE T RESULTING IN EQUIPMENT STRIKE THE EQUIPMENT LEFT IN THE FOUL BY INBOUND CREW ON N81024.",False,False,True,False,False,0.0
839,19,7,ATK,24,ODENTON,ANNE ARUNDEL,"TRAIN KW 901 WITH ENGINE 571 PULLING 6 BALLAST CARS ON #1 TRACK AT MP 113.9 DERAILED 5 CARS TOWARD 2 TRACK SIDE. THE TRAIN WAS IN THE PROCESS OF DUMPING BALLAST AT 1 TO 2 MPH AT THE TIME OF DERAILMEN T. THE 2ND CAR WAS FOUND LEANING AND THE 3RD THROUGH 6TH CARS WERE ON THEIR SIDE. THERE WERE NO IN JURIES TO REPORT. AS A RESULT OF THE DERAILMENT, THE BALLAST WAS BEING OFFLOADED ON THE HIGH SIDE O F THE UNEVEN TRACK GEOMETRY.",False,True,False,False,False,0.0
840,19,7,ATK,24,EDGEWOOD,HARFORD,"PANTOGRAPH/CATENARY: TRAIN 2168 WAS CANCELLED DUE TO PANTOGRAPH DAMAGE. TRAIN 2168 RECEIVED A `BRO KEN PANTOGRAPH ALARM` WHILE OPERATING THROUGH MP 75.3 WOOD INTERLOCKING. THERE WAS ALSO A SWITCH FA ILURE WITH THE 43SW AT MP 71.6, WHICH CAUSED FURTHER DELAYS DUE TO THE LENGTH OF SINGLE TRACKING ARO UND BOTH AREAS.",False,False,True,False,True,0.0
841,19,10,CSX,26,DEARBORN,WAYNE,"WHILE SHOVING TRACK R07 TO SPOT AT ROUGEMERE, Y29011 DERAILED LINES 79-89 OF THEIR CUT IN TRACK W03. INVESTIGATION REVEALED BROKEN RAIL CAUSED DERAILMENT.",False,True,False,False,False,0.0
842,19,1,ATK,22,KENNER,JEFFERSON,"TRAIN 59 OPERATING WITH LOCOMOTIVE E/58 AND 7 CARS STRUCK A SEMI-TRACTOR TRAILER TRUCK AT MP 903.60, LITTLE FARMS AVE CROSSING. THE AGE OF THE DRIVER WAS NOT AVAILABLE.",True,False,False,False,False,0.0
843,19,1,IC,22,BATON ROUGE,EAST BATON ROUGE,L56871-05 WAS SHOVING SOUTHWARD INTO TRACK BR74 AND THE CONDUCTOR WAS NOT ON THE LEADING END OF THE MOVEMENT. THEY SHOVED OUT OF BR74 ONTO BR76 AND OVER A PORTABLE DERAIL CAUSING XOMX 720394 AND LRS 1 66670 TO DERAIL. THE CREW WAS D&A TESTED AND ALL RESULTS WERE NEGATIVE.,False,True,False,False,False,0.0
844,19,1,NOPB,22,NEW ORLEANS,ORLEANS,"TWO (2) COVERED HOPPER CARS DERAILED WHILE DOUBLING AN OUTBOUND TRAIN IN CSX YARD. CSX ESTIMATED EQU IPMENT DAMAGE: $89,000 AND CSX ESTIMATED TRACK DAMAGE: $9,487.",False,True,False,False,True,98487.0
845,19,7,UP,22,PORT ALLEN,WEST BATON ROUGE,THIRD PARTY SWITCHER USA RAIL WAS SHOVING CARS AT THE EAST END OF THEIR YARD WHEN THEIR REAR CAR RAN THROUGH UPRR'S POWER SWITCH DERAIL AND DERAILED THE SRCX715. THE CAR FELL OVER ON ITS SIDE AND DAMA GED THE POWER SWITCH AND THE SIGNAL POLE.,False,True,False,False,False,0.0
846,19,6,UP,22,WESTWEGO,JEFFERSON,"WHEN COMING WEST OFF THE BRIDGE, THE YAV24-04 DERAILED 1 CAR WHILE PULLING INTO THE DRILL TRACK. CA USE WAS DUE TO EXCESSIVE BRAKING.",False,True,False,False,False,0.0
847,19,6,UP,22,WESTWEGO,JEFFERSON,"YAV37-04 WAS DRAGGING OUT OF TRACK 3 WITH 19 CARS AND DID NOT NOTICE THE SWITCH LINED AGAINST THEIR MOVE. WHEN CREW GAVE SHOVING INFORMATION, THEY SHOVED BACK DERAILING 4 CARS AND ONE ENGINE.",False,True,False,False,False,0.0
848,19,6,UP,22,ALEXANDRIA,RAPIDES,YAL53R-12 WAS PULLING A CUT OF CARS OUT TO SWING FOR OUTBOUND TRAIN. CROSSOVER SWITCH WAS IMPROPERL Y LINED BY THE YAL05-12 RESULTING IN THE DERAILMENT OF 4 CARS.,False,True,False,False,False,0.0
849,19,10,IC,22,BATON ROUGE,EAST BATON ROUGE,"CREW OF L52471-11 WAS SWITCHING ON THE NORTH END OF THE YARD. THE CONDUCTOR HAD TWO CARS REMAINING T O GO INTO TRACK 5 FROM THE NORTH END, BUT DID NOT HAVE ENOUGH ROOM ON THE NORTH END FOR THE CARS. TH E CONDUCTOR FAILED TO PROTECT HIS SHOVE SUBSEQUENTLY SHOVING TRACK #5 INTO THE SIDE OF AN OUTBOUND T RAIN L58272-11 DEPARTING FROM TRACK 4. AS A RESULT, SEVERAL CARS SUSTAINED DAMAGE.",False,False,True,False,True,0.0
850,19,10,BNSF,22,LACASSINE,JEFFERSON DAVIS,R-RDV2231-23 HAD DAMAGE TO 1 RAILCAR WHILE SHOVING YARD TRACK 4198 DUE TO FAILURE TO CONTROL RESULTI NG IN COUPLING AT EXCESSIVE SPEED. NO HAZARDOUS MATERIALS WERE RELEASED.,False,False,True,False,True,0.0
851,19,4,CSX,24,BALTIMORE,BALTIMORE CITY,"Y23421 COUPLED TO THE CARS ALREADY IN Y03 AT MT WINANS. AFTER COUPLING, STRETCHING, AND CUTTING THE AIR IN THE FOREMAN STARTED RELEASING THE HANDBRAKES. HE RELEASED 5 OF THE HAND BRAKES ON THE CARS H E COUPLED TO IN Y03. A SEPERATION OCCURRED 3 CARS EAST OF WHERE THE FOREMAN MADE THE INITIAL COUPLE. THE NOW 34 CARS ROLLED EAST AT AN ACCELERATED PACE AND DERAILED WHEN THEY ENCOUNTERED THE SPLIT RA IL AT THE EAST END OF THE YARD. THE 4 EAST END TANK CARS DERAILED. UPON FURTHER INVESTIGATION WE FOU ND ANGLE COCKS CLOSED ON GLNX 34706, CSXT 137051, AND EQUX 19114. WE ALSO FOUND THE CUT LEVER PULLED ON THE CSXT 137051 BEING THE INITIAL CAUSE OF THE SEPERATION. PROX 40450 LEAKED 1 GALLON OF FUEL O IL",False,True,False,False,False,0.0
852,19,4,CSX,24,NEWBURG,CHARLES,"WHILE MAKING A SHOVE MOVEMENT INSIDE THE MORGANTOWN POWER PLANT INDUSTRY TRACKS, 5 CARS IN THE MIDDL E OF THE CUT OF 22 CARS DERAILED. THE INVESTIGATION OF THE LDVR FROM THE PREVIOUS TWO TRAINS SHOWS T HAT THE SWITCH WAS LINED CORRECTLY FOR THE OUTSIDE LOOP TRACK ON BOTH VIDEOS BEFORE THE DERAILMENT. THESE TRACKS INCLUDING THE SWITCH ARE MAINTAINED BY THE INDUSTRY AND ARE INSPECTED QUARTERLY BY CSX. THE LAST INSPECTION TOOK PLACE ON 3-29-19 AND NO CONDEMNABLE DEFECTS WERE TAKEN WITH THE SWITCH. TH E FIRST MANAGER THAT ARRIVED TO THE SCENE NOTICED THAT EMPLOYEES FROM THE INDUSTRY HAD TAMPERED WITH THE SWITCH PRIOR TO ANY OF THE INVESTIGATIVE TEAMS ARRIVAL. THEY HAVE ALSO TAKEN INTO THEIR POSSESS ION A BROKEN LUG AND ONLY SHOWED IT TO US WHEN QUESTIONED. THE INDUSTRY ALSO HAD ACTIVE TRACK WORK T AKING PLACE INSIDE THEIR FACILITY DURING THE TIME OF INVESTIGATION.",False,True,False,False,False,0.0
853,19,7,CSX,24,BALTIMORE,BALTIMORE CITY,Q03207 DERAILED IN THE HOWARD ST TUNNEL DUE TO A TRACK OBSTRUCTION DUE TO EXCESSIVE FLOODING CAUSED BY A BROKEN BALTIMORE CITY WATER MAIN ABOVE THE TUNNEL.,False,True,False,False,False,0.0
854,19,11,NS,21,LOUISVILLE,JEFFERSON,"RAIL BROKE UNDER MOVEMENT AS DV40 WAS PULLING 40 CARS OUT OF YARD TRACK BY02 DERAILING 4 CARS, LINES 12-15 IN THEIR CUT: EQUX 018259, EQUX 016562, EQUX 621011 AND TCIX 023008.",False,True,False,False,False,0.0
855,19,11,CSX,21,AUXIER,FLOYD,N31329 TRAVELING WEST ON BIG SANDY STRUCK ROCK SLIDE ON NUMBER 1 MAIN.,True,False,False,False,False,0.0
856,19,2,UP,22,ALEXANDRIA,RAPIDES,THE YAL02R-10 WAS SHOVING FROM WEST TO EAST. THE TRAIN SHOVED OVER A DERAIL RESULTING IN AN 8-CAR D ERAILMENT. THERE WAS AN IMPROPER JOB BRIEFING PRIOR TO THE MOVE BETWEEN THE YARDMASTER AND THE CREW REGARDING WHO WOULD WATCH THE SHOVE.,False,True,False,False,False,0.0
857,19,2,UP,22,LOTTIE,POINTE COUPEE,LLM11R-16 WAS SHOVING NORTH AT 5 MPH INTO TRACK 19 AND DERAILED THE MWCX101479 WHILE COUPLING INTO T HE UTLX646459 NEAR THE 22 SWITCH ON THE EAST TRIM LEAD DUE TO THE RAILCAR WHEELS SLID OUT FROM UNDER THE MWCX CAR.,False,True,False,False,False,0.0
858,19,4,KCS,22,DE QUINCY,CALCASIEU,STRUCK A VEHICLE FOULING THE TRACK. NO ONE IN VEHICLE. NOT AT A XING. MP 719 BEAUMONT SUBDIVISION,True,False,False,False,False,0.0
859,19,6,KCS,22,BATON ROUGE,EAST BATON ROUGE,CREW WAS IN SOLVAY INDUSTRIES. CARS WERE LEFT FOUL BY INDUSTRY EMPLOYEES IN TRACK 723. CREW WENT T O COUPLE TO CARS TO SHOVE IN CLEAR & SWITCH WAS LINED FOR ADJACENT TRACK & CARS SIDE SWIPED. MP D-2 20 NEW ORLEANS SUB,False,False,True,False,False,0.0
860,19,2,NS,13,HOWARD,TAYLOR,187 CREW PULLED INTO THE SIDING TO CLEAR THE MAINLINE. CONDUCTOR AND CONDUCTOR TRAINEE LOCKED THE SW ITCHES BACK FOR THE MAINLINE AND MOUNTED THE BOTTOM OF THE TRAIN AND WAS PULLED TOWARD THE SOUTH END OF THE SIDING. ONCE CREW REACHED A CERTAIN POINTTHE CONDUCTOR AND CONDUCTOR TRAINEE DISMOUNTED. THE 187 ENGINEER SHOVED BACK TO GET THE CONDUCTOR AND CONDUCTOR TRAINEE ON THE HEAD END OF THE TRAIN WH EN THEY SHOVED THROUGH THE SPRING SWITCH AT THE NORTH END OF HOWARD AND PULLED SOUTHWARD ONCE ALLCRE W MEMBERS WERE ON LOCOMOTIVE DERAILING TWO CARS.,False,True,False,False,False,0.0
861,19,2,NS,13,GAINESVILLE,HALL,"G52GP20 PULLING NORTH WITH 3 ENGINES, 30 LOADS, 0 EMPTIES, 4,244 TONS, 1,700 FEET DERAILED THE 27TH AND 28TH HEAD CARS ON A PERVIOUSLY RUN-THROUGH SWITCH.",False,True,False,False,False,0.0
862,19,4,FCR,13,ATLANTA,FULTON,CREW WAS SHOVING 31 EMPTIES AND 3 LOADS TO THE CSX INTERCHANGE. THE 26TH CAR IN THE CONSIST DERAILED CAUSING 2 OTHER CARS TO DERAIL. THE DERAILMENT WAS CAUSED BY REVERSE ELEVATION IN A CURVE.,False,True,False,False,False,0.0
863,19,6,NS,13,GARDEN CITY,CHATHAM,GS06 PULLED INTO CT25 HOLDING ONTO 52 CARS WHEN LINES 24-29 DERAILED DUE TO BROKEN RAIL UNDER MOVEME NT OF TRAIN.,False,True,False,False,False,0.0
864,19,10,UP,17,NORTHLAKE,COOK,"YPR12R-29, DURING NORMAL SWITCHING OPERATIONS DERAILED LOADED TANK CARS CTCX725386, TCBX251950, TILX 270429, AND UTLX662424, WHILE SHOVING INTO TRACK 216.",False,True,False,False,False,0.0
865,19,8,UP,17,NORTHLAKE,COOK,THE NAHX551266 WAS REPORTED WITH DAMAGE IN MCS. THE SERVICE UNIT INVESTIGATED AND COULD NOT DETERMI NE WHAT CAUSED THE DAMAGE OR WHERE THE DAMAGE OCCURRED.,False,False,True,False,True,0.0
866,19,8,UP,17,MELROSE PARK,COOK,"CAR CHSX255077 FOUND WITH DAMAGE IN PROVISO YARD, NO MATE CAR AVAILABLE. NO DERAILMENT.",False,False,True,False,True,0.0
867,19,11,UP,17,NILWOOD,MACOUPIN,"ATK TRAIN 302-27 STRUCK A CROSSING GATE ARM. E/4603 WAS STRUCK ON THE FIREMAN'S SIDE AND A CRACKED WINDSHIELD WAS REPORTED. NO INJURIES WERE REPORTED. AMTRAK EQUIPMENT DAMAGE = $15,718",True,False,False,False,True,15718.0
868,19,9,ATK,11,"WASHINGTON, DC","WASHINGTON, DC","A CLASS 4 ENGINEER WHILE OPERATING 2 LITE ENGINES, E/541 AND E/182, DERAILED E/182 AT MP 134.5 ON TR ACK 24 NORTH OVER THE DERAIL AND BLUE FLAG WHILE OPERATING IN REVERSE DIRECTION WITHOUT POINT PROTEC TION. THE CLASS 4 ENGINEER WAS OPERATING FROM E/182 AND THE REAR TRUCK AND 2 AXLES DERAILED. THE E NGINEER OPERATED IN A REVERSE DIRECTION OVER DERAIL WITHOUT POINT PROTECTION.",False,True,False,False,False,0.0
869,19,2,ATK,11,"WASHINGTON, DC","WASHINGTON, DC","RULE VIOLATION: WS-202A ON YARD ENGINE 737 WAS TO LEAVE 19 SHOP TRACK ON THE SOUTH END, AND MAKE A REVERSE MOVEMENT TO 14 SHOP. THEY PASSED STOP SIGNAL 659 WITHOUT AUTHORITY AND TRAVELED 574.6 FT., BREAKING SWITCH #616 WHICH WAS NOT LINED FOR THEIR MOVEMENT. SOUTH END 616 SWITCH ROD AND MACHINE D AMAGED BEYOND REPAIR. THERE WERE NO INJURIES TO REPORT.",False,False,True,False,False,0.0
870,19,12,VREX,11,"WASHINGTON, DC","WASHINGTON, DC",ENGINEER COMMITTED RULE VIOLATION WHEN HE MOVED THE CONSIST NORTH PAST A STOP SIGNAL AT UNION STATIO N. THE TRAIN WAS MOVING FROM THE STATION TO 41 TRACK WHEN IT WENT PAST THE SIGNAL AND CAUSED DAMAGE TO A SWITCH AT UNION STATION - ECLIPSING THE REPORTING THRESHOLD.,False,False,True,False,True,0.0
871,19,5,UP,19,CEDAR RAPIDS,LINN,"THE IANR TRAIN WACR-27 CAME INTO NORTH YARD ON 13 TRACK TO SHOVE INTERCHANGE CARS ON 14 TRACK BEFORE HEADING THROUGH THE YARD TO THE CEDAR RAPIDS IOWA CITY RAILROAD (CIC). IANR WACR-27 TIED DOWN 10 C ARS FOR CIC ON 13 TRACK AND STARTED TO PULL WITH 4 OF THEIR 5 LOCOMOTIVES ON LINE WITH 5 LOADED OAT CARS RIGHT BEHIND THEIR POWER, FOLLOWED BY 10 EMPTY FLAT CARS AND 20 MORE LOADED OAT CARS ON THE TAI L END, AND USED TOO MUCH AUTOMATIC BRAKE TO STOP FOR A SWITCH LINED AGAINST THEM, WHICH CAUSED THE L EADING TRUCKS ON THE SECOND EMPTY FLAT CAR (OTTX97289) TI DERAIL WITHOUT THE CREW NOTICING. THE IAN R WACR-27 CREW THEN PULLED THEIR TRAIN AHEAD ABOUT 40 CAR LENGTHS TO CLEAR THE 14 SWITCH WITH LEADIN G TRUCKS TO OTTX97289 DERAILED THE ENTIRE TIME, THEN SHOVED BACK INTO 14 TRACK TO DO THEIR SETOUT. WITH THE LEADING WHEELS OF OTTX9729 DERAILED, AT THE TRAIN SHOVED BACK INTO 14 TRACK TO DO THEIR SET OUT, OTTX97289 TRIED TO GO DOWN TRACK 15 DUE TO THE LEADING WHEELS BEING DERAILED OUTSIDE THE RAIL. WHEN THE IANR WACR-27 CREW ATTEMPTED TO STOP THEIR TRAIN IN 14 TRACK WITH TOO MUCH AUTOMATIC BRAKE, THE 20 LOADED OAT CARS ON THEIR TRAIN RAN OUT AND SNAPPED THE HEAD END OF THE TRAIN TRYING TO GO DO WN 15 TRACK OVER TO TRACK 14 WHICH CAUSED ABOUT A 12 INCH MISALIGNMENT OF TRACK 14 AND TRACK 15 FOR ABOUT 100 YARDS AND CAUSED 5 ADDITIONAL EMPTY FLAT CARS TO DERAIL, 2 OF WHICH CAUSED THE BOLSTERS AN D WHEELS TO BE RIPPED FROM UNDER THE FLAT CARS (UP93545 AND OTTX97732). IANR REPORTED $49,743 EQUIP",False,True,False,False,False,49743.0
872,19,7,CP,19,COLUMBUS JCTN,LOUISA,"475-04 TRAVELING NORTH ON THE OTTUMWA SUBDIVISION MADE CONTACT WITH A SEMI TRACTOR TRAILER AT DOX XI NG 695494R - IA 70. TRAIN CREW OBSERVED VEHICLE STRADDLING THE CROSSING AND DRIVER OUTSIDE OF VEHICL E FRANTICALLY WAVING HER ARMS TRYING TO GET TRAIN TO STOP. CROSSING WAS PROTECTED BY ADVANCE WARNING SIGNS, LIGHTS, GATES AND BELLS. TRAIN WAS PLACED IN EMERGENCY AND MADE CONTACT WITH REAR PORTION OF THE TRAILER. SEMI DRIVER WAS INTERVIEWED AND SAID THE VEHICLE STALLED AND SHE WAS UNABLE TO RE-STAR T. DOT CONDUCTED A VEHICLE INSPECTION AND FOUND NO DEFECTS. NO INJURIES TO TRAIN CREW MEMBERS OR VEH ICLE DRIVER.",False,False,True,False,False,0.0
873,19,2,UP,19,DES MOINES,POLK,"MECHANICAL WAS SHOVING 4 UNITS LIGHT POWER TOWARDS THE PIT, 2 LOCOMOTIVES DERAILED DUE TO ICE AND SN OW BUILDUP. THE LEADING 2 WHEELS ON THE LEADING LOCOMOTIVE REMAINED ON THE RAIL WHILE THE FOLLOWING 4 ON UP3843 AND ALL WHEELS ON UP5074 DERAILED.",False,True,False,False,False,0.0
874,19,11,NKCR,8,HOLYOKE,PHILLIPS,"NKCR CREW WAS IN THE PROCESS OF SHOVING THEIR 54 CAR TRAIN ON THE LOOP TRACK IN HOLOKE TO TIE DOWN. SWITCH WAS MISALIGNED FOR THE LOOP TRACK AND AS THE CARS TRAVERSED THROUGH THE FACING POINT SWITCH O NTO THE CROSSOVER, THEY DERAILED AT THE SPLIT RAIL DERAIL.",False,True,False,False,False,0.0
875,19,12,BNSF,8,TRINCHERA,LAS ANIMAS,"E-SPSBTM0-48 DERAILED 1 RAILCAR WHILE TRAVERSING SINGLE MAIN TRACK DUE TO CROSS LEVEL OF TRACK IRREG ULAR, NOT AT A JOINT. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
876,19,6,CSX,13,NEWNAN,COWETA,"A74105 WAS WORKING BWAY INDUSTRY, WHEN THEY FAILED TO APPLY SUFFICIENT HAND BRAKES TO SECURE CARS. C ARS RAN AWAY, STRUCK A STANDING CUT OF 7 CARS AND DERAILED ONE CAR WHICH CAUSED UNREPAIRABLE DAMAGE TO TWO CARS.",True,True,False,False,True,0.0
877,19,6,CSX,13,WAYCROSS,WARE,"Q54104 WAS SHOVING IN TO R03 WHEN THE RAIL BROKE IN THE R13 CROSSOVER, DERAILING 7 CARS.",False,True,False,False,False,0.0
878,19,9,CSX,13,SAVANNAH,CHATHAM,"Y19206 KICKED A SINGLE LOADED TANK CAR GATX 212841 INTO THE SOUTH END OF A31, WHERE 5 LOADS WERE ALR EADY TIED DOWN CLEAR ON THE YELLOW TIE. THIS TANK CAR DID HIT THE CUT ALREADY THERE, BUT FAILED TO C OUPLE. THE TANK THEN ROLLED BACK OUT TOWARD THE LADDER AND INTO THE SIDE OF KLRX 615053.",False,False,True,False,False,0.0
879,19,12,UP,19,MANLY,WORTH,"MITDM-14 WAS TRAVELING SOUTH ON THE ALBERT LEA MAIN WHEN IT DERAILED 9 CARS IN MANLY, IA. NO INJURI ES OR HAZMAT RELEASES REPORTED. 1 SET OF WHEELS DERAILED SOUTH OF THE IANR MAIN LINE SWITCH IN MANL Y AND WAS CARRIED ON THE GROUND FOR 0.2 MILES UNTIL IT HIT THE NORTH SWITCH OF THE MANLY SIDING. AT THIS POINT, THE OTHER 8 CARS DERAILED.",False,True,False,True,False,0.0
880,19,12,UP,19,COUNCIL BLUFFS,POTTAWATTAMIE,"MCBDM-01 COUPLED TO AND PULLED OUT OF 471 AFTER DETERMINING WHAT THE CONDUCTOR THOUGHT WAS LINED INT O 473 BY LOOKING DOWN THE LEAD AND OBSERVING TWO RED TARGETS. HE ATTEMPTED TO SHOVE BACK INTO TRACK 473, WHEN THE CONDUCTOR NOTICED HE WAS NOT LINED TO 473, HE INSTRUCTED THE ENGINEER TO STOP. BY TH IS TIME THE CUT OF CARS THEY HAD A HOLD OF HAD ENTERED INTO TRACK 474, IMPACTED THE STANDING CUT THA T WAS IN THERE, SUBSEQUENTLY DERAILING 4 CARS.",False,True,False,False,False,0.0
881,19,7,KCS,22,BATON ROUGE,EAST BATON ROUGE,CREW WAS SERVICING INDUSTRY BRPP WHEN THEY SHOVED OUT OF SOUTH END & SWIPED 2 CARS CAUSING 1 CAR TO DERAIL. MP 217 NEW ORLEANS SUBDIVISION,False,True,False,False,False,0.0
882,19,2,IAIS,19,ALTOONA,POLK,"POLK COUNTY SNOW PLOW STOPPED ON A DIAGONAL CROSSING AND WAS STRUCK BY IAIS BICB-18. THERE WERE STO P SIGNS ON THE CROSSBUCKS, BUT DRIVER DIDN'T STOP UNTIL HE WAS ON THE CROSSING.",True,False,False,False,False,0.0
883,19,2,IANR,19,WATERLOO,BLACK HAWK,"THIS CREW WAS SITTING ON MAIN TRACK AT BRYANT YARD. WHILE SITTING STATIONARY ON THIS 4 LOCOMOTIVE CO NSIST, A NORTHBOUND LITE ENGINE CONSIST (7 LOCOMOTIVES) ATTEMPTING TO STOP INORDER TO ENTER THE SOUT H NEW LEAD SWITCH, FAILED TO STOP DUE TO NO BRAKING EFFECT AND COLLIDED WITH THIS CONSIST. THIS CREW DID NOTHING TO CONTRIBUTE TO THIS INCIDENT.",False,False,True,False,False,0.0
884,19,1,IC,17,CICERO,COOK,"A44681-11 WAS IN THE PROCESS OF SHOVING THROUGH HA03 TRACK WHEN THEY RAN THROUGH AN IMPROPERLY LINED 2/3 SWITCH. THEY THEN MADE A REVERSE MOVE BACK THROUGH THE SWITCH WHICH CAUSED VELX 12571, VELX 125 52 AND UTLE 666953 TO DERAIL. WHEN THE CARS DERAILED THEY IMPACTED CGTX 30064 WHICH WAS STANDING IN A CUT OF CARS ON TRACK HA02 CAUSING IT TO DERAIL. THERE WERE NO LEAKS OR EXPOSURES OF HAZARDOUS MATE RIAL. D&A TESTING WAS DONE AND ALL RESULTS WERE NEGATIVE.",False,True,False,False,False,0.0
885,19,9,UP,17,CREVE COEUR,TAZEWELL,"CWTDE-27 EXITED THE PEORIA MAINLINE AT PEORIA JUNCTION MP 80.3 AND ONTO TZPR MAIN LINE WHERE THEY ST OPPED AT MP 5 ON THE SOUTHERN SUB AND HAD TO BE TALKED BY THE SIGNAL. ONCE ON THE MOVE THE TRAIN WE NT INTO EMERGENCY, AFTER TRAVELING A DISTANCE OF 1.3 MILES. INSPECTION OF THE TRAIN FOUND 4 CARS DE RAILED. TZPR MAINTAINS TRACK. TZPR TRACK DAMAGE = $44,025",False,False,True,False,True,44025.0
886,19,10,CSX,1,MONTGOMERY,MONTGOMERY,Y29328 SWITCHMAN WAS SHOVING INTO N19 DOWN THE LEAD. THERE IS A CROSSOVER SWITCH FROM THE N18/N19 LE AD TO THE NEW TRACK THAT THE CAR INSPECTORS HAD PREVIOUSLY LINED AND LOCKED FOR MOVEMENT ON THE CROS SOVER IN ORDER TO WORK N19. THE CAR INSPECTOR FAILED TO LINE THE SOUTH END OF THE CROSSOVER BACK FOR MOVEMENT ON THE N18/N19 LEAD TO CORRESPOND WITH THE NORTH END OF THE CROSSOVER. THE Y29328 SWITCHMA N FAILED TO STOP SHORT OF THE SOUTH END OF THE CROSSOVER THAT WAS IMPROPERLY LINED FOR HIS MOVEMENT RESULTING IN AN FRA REPORTABLE SIDE SWIPE.,False,False,True,False,False,0.0
887,19,8,NS,1,VANCE,TUSCALOOSA,"NS TRAIN 27AA720 WAS SHOVING INTO MERCEDES WITH 61 EMPTY MULTILEVELS AT 2500 TONS. WHILE SHOVING INT O THE INSIDE STORAGE TRACK THE RAIL SPREAD UNDERNEATH MOVEMENT, SUBSEQUENTLY DERAILING 7 CARS ON THE BRIDGE SWITCH LEAD.",False,True,False,False,False,0.0
888,19,12,BNSF,1,ADAMSVILLE,JEFFERSON,H-MEMBIR1-07 DERAILED 7 RAILCARS WHILE TRAVERSING SINGLE MAIN TRACK. NO HAZARDOUS MATERIALS WERE REL EASED. CAUSE IS UNDER ACTIVE INVESTIGATION.,False,True,False,False,False,0.0
889,19,12,CSX,1,MIDLAND CITY,DALE,"THE A72203 BROUGHT 4 LOCOMOTIVES INTO PILGRIMS PRIDE INDUSTRY AND WAS INSTRUCTED BY THE INDUSTRY TO COUPLE UP TO A CUT OF CARS AND SHOVE BACK TO CLEAR THE PASS TRACK SWITCH. ONCE THE A72204 COUPLED A ND THEN LATER BEGAN TO SHOVE, THE TRAIN WENT INTO EMERGENCY AFTER TRAVELLING APPROXIMATELY 6 CARS. IT WAS THEN DISCOVERED THE TRAIN HAD DERAILED 6 CARS AT A PREVIOUSLY RUN THRU SWITCH BY THE CUSTOMER .",False,True,False,False,False,0.0
890,19,3,IC,22,BATON ROUGE,EAST BATON ROUGE,"KCS CREW WAS SHOVING TRACK #36 AND RAN OVER A DERAIL THAT CAUSED 3 CARS TO DERAIL, AND STRIKE 2 CARS SITTING IN THE NEXT TRACK. TWO OF THE CARS FOULING IC'S MAIN LINE AND CAUSED MINIMAL DAMAGE TO THE IC TRACKS. KCS PROVIDED AN ESTIMATE OF $51,650 IN DAMAGE TO THEIR EQUIPMENT. KCS WILL SEND A 6180 .78 TO THEIR EMPLOYEE. KCS EQUIPMENT DAMAGES $27,000",False,True,False,False,True,78650.0
891,19,6,LAS,22,MINDEN,WEBSTER,THE LASR 132 WAS PULLING 25 CARS NORTH ON THE MAIN INSIDE THE MINDEN YARD WHEN THE 7TH CAR DERAILED AND TRAVELED 120' BEFORE COMING TO REST ON ITS SIDE. DUE TO THE CAR BEING EQUIP WITH DOUBLE SHELF CO UPLERS AN ADDITIONAL 13 CARS ROLLED OVER IN THE PROCESS. THERE WAS NO PRODUCT RELEASED AND NO INJURI ES ASSOCIATED WITH THIS INCIDENT. THE CAUSE OF DERAILMENT WAS DETERMINED TO BE A BROKEN RAIL.,False,True,False,False,False,0.0
892,19,6,ATK,24,BALTIMORE,BALTIMORE CITY,"AS THE BALLAST REGULATOR TRAVERSED THE OVERHEAD BRIDGE THE RIGHT WING (NORTH SIDE OF EQUIPMENT) APPE ARED TO STRIKE THE BRIDGE RAILS CAUSING THE TCA 14317 TO DERAIL. THE RIGHT WING WAS NOT IN THE LOCK ING POSITION. SEVERAL TIES WERE DAMAGED, 11 WERE REPLACED AT THE TIME OF INCIDENT WITH MORE TO FOLL OW. TCA14317 SUSTAINED DAMAGE TO THE RIGHT WING AND THE SWEEPING PLATE ON THE RIGHT SIDE IS MISSING .",False,True,False,False,True,0.0
893,19,3,CSX,24,CUMBERLAND,ALLEGANY,"Y19014 PULLING WEST ON THE 4TH GROUP HUMP LEAD, DERAILED 4 CARS DUE TO CLIMBING OVER THE SOUTH RAIL AND CONTACTING THE RETARDER STRUCTURE.",False,True,False,False,False,0.0
894,19,12,GTW,26,DETROIT,WAYNE,TRAIN M38331-11 WAS TRAVELING ACROSS SHARED ASSETS ON THE CONRAIL WHEN LINES 122 AND 123 HAD SEPARAT ED CAUSING THE TRAIN TO GO INTO EMERGENCY. THE CONDUCTOR PROCEEDED TO WALK HIS TRAIN WHEN HE FOUND E LEVEN CARS DERAILED IN THE CURVE.,False,True,False,False,False,0.0
895,19,7,KCS,22,SHREVEPORT,CADDO,CREW WAS PULLING THE LONG 6 FROM THE EAST MAIN & DERAILED 2 CARS. MP 551.8 SHREVEPORT TERMINAL SUBD IVISION,False,True,False,False,False,0.0
896,19,5,UP,22,SHREVEPORT,CADDO,"MAXFW-06, WHILE TRAVELING SOUTH ON THE REISOR SUB, STRUCK A TANKER TRUCK AT MP 295.15. RESULTING IN DERAILMENT OF 3 LCOMOTIVES AND 26 RAILCARS AND INJURY.",True,True,False,False,False,0.0
897,19,7,BRC,17,BEDFORD PARK,COOK,"AT APPROXIMATELY 17:55, TRAIN MASCHX-19, DERAILED 3 CARS WHILE YARDING TRAIN ON 01 EAST RECEIVING. T RAIN PULLED IN TO THE EAST END OF 01 EAST RECEIVING, ONCE CREW REACHED THE WEST END OF TRACK CONDUCT OR DETRAINED AT THE CLEAR POINT & TRAIN CONTINUED WESTWARD BEING COUNTED DOWN BY WEST YARDMASTER. ON CE CREW WAS ADVISED BY WEST YARDMASTER THEY HAD CLEARED THE EAST END ENGINEER APPLIED FULL INDEPENDE NT BRAKE DERAILING CARS TTGX 964290 (R&L 1-4), TTGX 852223 (R&L 3/4), CLSX 1349 (R 3/4). AFTER REVI EW OF INCIDENT APPEARS THE LOCOMOTIVE ENGINEER APPLIED TOO HEAVY OF A BRAKE APPLICATION WHEN STOPPIN G THE TRAIN WHICH THEN CAUSED THE TTGX 964290 TO NOT NEGOTIATE THE CURVE COMING OUT OF 01 EAST AND D ERAILING.",False,True,False,False,False,0.0
898,19,4,UP,22,MARINGOUIN,POINTE COUPEE,"LLM32R-17, SWITCH NUMBER 28 IN THE BOWL WAS DAMAGED BY DRAGGING MATERIAL FROM CAR BNSF546243. THE L OAD WAS SHIFTED ON THE CAR CAUSING STRAPS TO BREAK AND HANG FROM CAR. NO DERAILMENT OR CAR DAMAGE.",False,False,True,False,True,0.0
899,19,4,UP,22,SHREVEPORT,CADDO,"WHILE TRAVELING NORTH ON THE RESIOR SUB, THE GSPONY-07 STRUCK A SALT WATER TRUCK AT A CROSSING RESUL TING IN THE DERAILMENT OF 24 CARS AND 3 LOCOMOTIVES.",True,True,False,False,False,0.0
900,19,9,UP,22,OPELOUSAS,ST LANDRY,"MNSEW-09, LEAD UNIT UP5789, STRUCK A TRACTOR TRAILER THAT WENT AROUND GATES AND FAILED TO STOP AT RO AD CROSSING. THE CREW NOTICED THE VEHICLE STUCK IN THE CROSSING SO THE ENGINEER PLACED THE TRAIN IN EMERGENCY.",True,False,False,False,False,0.0
901,19,12,CSX,1,BIRMINGHAM,JEFFERSON,Y32020 WAS SWITCHING CARS FROM R03 AND MADE A CUT LEAVING CARS STANDING IN R03. AFTER MAKING THE CUT AND PULLING OUT OF R03 THE CARS IN THE MIDDLE OF THE CUT LEFT STANDING SEPARATED AND BEGAN ROLLING NORTH AS THE BRAKES WERE TIED ON THE SOUTH END OF THE TRACK. THE CARS CONTINUED TO ROLL NORTH STRIKI NG THE SIDE OF THE Y39320 THAT WAS IN THE PROCESS OF PULLING CARS FROM R04 TO THE WEST YARD. UPON IN SPECTION OF THE SEPARATED CARS IT WAS DETERMINED THAT THE MWCX 101548 HAS A BROKEN LOCK LIFTER. THE BREAK ALLOWED THE KNUCKLE TO COME OPEN AFTER A SERIES OF START AND STOPS. CAR ENGINEERING HAS BEEN C ONTACTED TO REVIEW THIS SERIES OF COUPLER. : CONFIRMED OVER SPEED,False,False,True,False,False,0.0
902,19,10,NS,1,IRONDALE,JEFFERSON,"AB21 SHOVING SOUTH, RAN THROUGH BACK SIDE SWITCH, MADE A REVERSE MOVE (STRETCH). SHOVED SOUTH DERAIL ING 5 CARS, FOULING EF04-EF07",False,True,False,False,False,0.0
903,19,9,AGR,1,KIMBROUGH,WILCOX,"WHILE SHOVING CARS, EXCESSIVE BUFF CAUSED ONE SET OF TRUCKS OF EMPTY BOX CAR TO LIFT OFF RAIL AND DE RAIL. AS SHOVING MOVEMENT CONTINUED, DERAILED SET OF TRUCKS TRIED TO RERAIL AND CAUSED 2 CARS TO ROL L DOWN INTERCHANGE TRACK CAUSING, A 6-CAR DERAILMENT. NS-HFI. NS EQUIPMENT COSTS: $65650.
01-16 -2020 REVISED-INCLUSION OF THIS FORM 54. NS EQUIP=$65650
",False,True,False,False,False,131300.0
904,19,3,KCS,22,SHREVEPORT,CADDO,CREW PULLED EMPTY CARS OUT & DID NOT SECURE. MADE SHOVE BACK WITH LOADED CARS & EMPTY CARS ROLLED INTO TRAIN & DERAILED 2 CARS. MP 564 SHREVEPORT TERMINAL SUBDIVISION,False,True,False,False,False,0.0
905,19,11,NS,1,CHATTANOOGA,TALLAPOOSA,AC12 DURING NORMAL SWITCHING OPERATIONS CONDUCTOR CUT OFF 7 CARS IN MOTION PUSHING CAR GACX 054071 O UT THE SOUTHEND OF THE TRACK SIDE SWIPING CARS ON THE LEAD RESULTING IN THE DERAILMENT OF 3 CARS.,False,True,False,False,False,0.0
906,19,12,BNSF,29,KANSAS CITY,JACKSON,Y-KCK311-1-25A TRAIN RAN THROUGH SWITCH DUE TO FAILURE TO COMPLY WITH RESTRICTED SPEED OR ITS EQUIVA LENT NOT IN CONNECTION WITH A BLOCK OR INTERLOCKING SIGNAL AND SWITCH IMPROPERLY LINED. NO HAZMAT R ELEASED.,False,False,True,False,False,0.0
907,19,12,UP,31,NORTH PLATTE,LINCOLN,"MAKEUP TEAM MOVING WEST FELT THE LOCOMOTIVE BOGGING DOWN; STOPPED THE MOVEMENT AND PULLED BACK EAST, NOTICING THEY HAD DERAILED ON THE MAKEUP LEAD AS THE LATCH ON THE SWITCH WAS NOT FULLY SECURED IN T HE HASP.",False,True,False,False,False,0.0
908,19,7,BNSF,31,LINCOLN,LANCASTER,Y-HAV3571-29 DERAILED 6 RAILCARS WHILE PULLING OUT OF YARD TRACK 3001 DUE TO A BROKEN TRACK SWITCH P OINT. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
909,19,6,UP,31,NORTH PLATTE,LINCOLN,RAILCAR CR582353 WAS FOUND DAMAGED DUE TO A SHIFTED LOAD IN NORTH PLATTE FOR TRANSLOAD. NO DERAILMEN T OR TRACK DAMAGE.,False,True,False,False,True,0.0
910,19,7,BNSF,31,SUPERIOR,NUCKOLLS,"H-TULLIN1-06 DERAILED 14 RAILCARS WHILE TRAVERSING SINGLE MAIN TRACK DUE TO EXTREME ENVIRONMENTAL CO NDITION, FLOOD. NO HAZARDOUS MATERIALS WERE RELEASED.",False,True,False,False,False,0.0
911,19,9,UP,22,LIVONIA,POINTE COUPEE,"DURING NORMAL HUMPING OPERATIONS THE LLM22R-13 HUMPED THE SPPX1102 (LOADED TANK) AS A SINGLE. AS IT TRAVERSED OVER THE 16/35 SWITCH, THE SWITCH LINED UNDER THE CAR, DERAILING IT. A CUT OF THREE CARS W AS IMMEDIATELY RELEASED BEHIND. THE UTLX631261 (LOADED TANK) DERAILED UPRIGHT, UTLX631238 (LOADED TA NK) WAS UNDAMAGED, UTLX631180 DERAILED UPRIGHT. IMMEDIATELY FOLLOWING THAT A CUT OF TWO CARS WAS REL EASED UTLX600321 (LOADED TANK) WAS DAMAGED, THE UTLX630757 (LOADED TANK) WAS UNDAMAGED.",False,True,False,False,True,0.0
912,19,6,NOGC,22,BELLE CHASSE,PLAQUEMINES,"CREW WAS PULLING A CUT OF 63 LOADED GRAIN HOPPERS WHEN THE TRAILING WHEELS ON THE 55TH CAR, CHTT 721 633, L3 WHEEL PICK/ROAD UP SWITCH POINT CAUSING THE SWITCH POINT TO OPEN UP. THIS CAUSED THE TRAILIN G WHEEL ON THE 55TH CAR, 56, 57, 58, AND 59 CARS TO GO TOWARD TRACK 87. ONE CUT WAS IN A BIND, THE 5 5TH CAR DERAILED CAUSING THE 56 AND 57 CAR TO ROLL OVER AND 58 AND 59TH CAR TO ALSO DERAIL.",False,True,False,False,False,0.0
913,19,3,KCS,22,BATON ROUGE,EAST BATON ROUGE,SHOVING TRACK #36 & RAN OVER A DERAIL & CAUSED DERAILMENT OF 3 CARS & THEN STRUCK 2 CARS SITTING IN NEXT TRACK. ILLINOIS CENTRAL RR TRACK DAMAGE $500. MP 787. NEW ORLEANS SUBDIVISION,True,True,False,False,True,500.0
914,19,5,BNSF,30,GLASGOW,VALLEY,L-MON8149-28 DERAILED 1 LOCOMOTIVE WHILE PULLING LIGHT POWER INTO YARD TRACK 2402 DUE TO TRACK SWITC H POINT GAPPED. NO HAZARDOUS MATERIALS WERE RELEASED.,False,True,False,False,False,0.0
915,19,8,UP,22,LIVONIA,POINTE COUPEE,"LLM21R-14 WAS SHOVING 127 CARS INTO TRACK 304 TO COMPLETE THE SET OF TRAIN MLIHO-14. THE CREW WAS UT LIZING THE SHOVE LIGHTS TO SPOT THE TRAIN TO AIR ON THE NORTH END OF THE YARD. THE CREW STRUCK A DER AIL THAT WAS PLACED EARLIER IN THE DAY BY THE 9163 TIE GANG TO PROTECT THE GANG AS THEY WERE WORKING IN TRACK 305, IN TURN DERAILING 12 CARS.",True,True,False,False,False,0.0
916,19,8,UP,22,LIVONIA,POINTE COUPEE,"LLM11R-25 DERAILED 10 CARS WHILE SHOVING TRACK 304. NO RELEASED, NO INJURIES. CAUSE WSA POOR TIE CON DITIONS.",False,True,False,False,False,0.0
917,19,8,UP,22,AVONDALE,JEFFERSON,TRAIN MLIWX-25 DERAILED 7 CARS WHILE PULLING TOWARDS THE SOUTH YARD MAIN. CAUSE FOUND TO BE SOFT ROA DBED CAUSED 5/8` CROSS LEVEL.,False,True,False,False,False,0.0
918,19,8,IC,22,BATON ROUGE,EAST BATON ROUGE,"L52371-26 WAS PERFORMING NORMAL SWITCHING ON THE SOUTH END IF THE YARD. CONDUCTOR WAS PULLING PINS F ROM UP THE LEAD AROUND THE NUMBER 5 SWITCH WITH THE BRAKEMAN WAS WORKING THE FIELD. CONDUCTOR KICKED A SINGLE CAR TO TRACK 1. AFTER THE CAR CLEARED, THE BRAKEMAN LINED THE TWO SWITCH AND PROTECTED THE SHOVE INTO TRACK 2. AFTER SECURING THE CAR HE PULLED THE PIN AND SEND THE REMAINING 3 CRS BACK OUT TO THE CONDUCTOR WHO WAS NOW AT THE 2 SWITCH. AS THE CUT PULLED OUT OF TRACK 2 THE CAR SEND TO 1 ROL LED OUT AND STRUCK THE CARS IN TRACK 2 SUBSEQUENTLY DERAILING TWO CARS UPRIGHT.",True,True,False,False,False,0.0
919,19,8,IC,22,GEISMAR,ASCENSION,"R97971-05 WAS SHOVING NORTHWARD FROM THE MAIN AT MILE 391.1 ON THE BATON ROUGE SUB TOWARDS THE LEAD WHEN THEY DERAILED LOADED HAZMAT CARS VELX 12534 (STABILIZED SULFUR TRIOXIDE, ALL WHEELS) AND UTLX 6 61357 (METHYLENE DIPHENYL DISOCYANATE, ONE SET OF TRUCKS). BOTH CARS DERAILED UPRIGHT. NO INJURIES A ND NO LEAKS. CAUSE WAS UNABLE TO BE DETERMINED. NO ISSUES WERE FOUND WITH TRAIN, CARS, TRACKS OR HAN DLING.",False,True,False,False,False,0.0
920,19,9,UP,22,KEATCHIE,DE SOTO,"MNLEW-12, LEAD UNIT UP5427, WAS TRAVELING SOUTH WHEN IT COLLIDED WITH A SEMITRAILER. TRUCK WAS STOPP ED ON CROSSING WITH NO DRIVER.",False,False,True,False,False,0.0
921,19,9,IC,22,HAMMOND,TANGIPAHOA,"TRAIN M30171-10 STRUCK A TRACTOR-TRAILER THAT STOPPED AND WENT ACROSS THE CROSSING. THE SEMI WAS SPL IT, AND PUSHED THE BRIDGE. NO INJURIES TO THE TRUCK DRIVER.",True,False,False,False,False,0.0
922,19,3,UP,22,SHREVEPORT,CADDO,"ZAILC-07 DERAILED 28 CARS WHILE TRAVELING WESTBOUND ON THE REISOR SUB. BECAUSE THE DAMAGE TO THE SW ITCH RAILS OCCURRED THROUGHOUT ITS LENGTH, AND PRIOR TO THE FRACTURED WELD (WHICH WAS LOCATED PAST T HE SWITCH), IT IS VERY UNLIKELY THE FRACTURED WELD CAUSED THE DERAILLMENT. FURTHERMORE, A LACK OF I MPACT MARKS ON THE WHEELS FURTHER INDICATES THE FOUR CARS PRIOR TO THE FIRST DERAILED CAR DID NOT EN COUNTER A BROKEN RAIL. HOWEVER, BECAUSE THE CARS WERE INSPECTED SO LONG AFTER THE DERAILMENT, IT IS POSSIBLE THAT ANY MARKS COULD HAVE BEEN WORN FROM THE WHEELS DURING THAT TIME. THE DAMAGE TO THE S WITCH RAILS FURTHER INDICATES A CAR DERAILED PRIOR TO THE SWITCH, WHILE ON THE INDUSTRIAL LEAD. BAS ED ON THE EVIDENCE SUBMITTED TO DATE, THE EXACT CAUSE OF THE DERAILMENT IS INCONCLUSIVE.",False,True,False,False,True,0.0
923,19,11,SCAX,6,SANTA FE SPRINGS,LOS ANGELES,"ON 11/22/19 AT 0539 WESTBOUND M681 STRUCK A UNOCCUPIED RECREATIONAL VEHICLE AT MP 157.8 ROSECRANS CR OSSING DOT #027656A ON THE BNSF SAN BERNARDINO SUBDIVISION. AT THE TIME OF THE ACCIDENT THERE WERE 1 05 PASSENGERS AND TWO CREW MEMBERS ON-BOARD. THE RV CAUGHT FIRE AND ALSO CAUGHT THE CAB CAR ON FIRE RESULTING IN SUBSTANTIAL DAMAGE TO THE CAB CAR. DAMAGE COST TO CAB CAR IS ESTIMATED AT 500,000.",True,False,False,False,True,0.0
924,19,11,SCAX,6,LOS ANGELES,LOS ANGELES,"BOMBARDIER EQUIPMENT OPERATOR WAS INSTRUCTED TO TAKE A DOUBLE SET OF EQUIPMENT INTO S&I TRACK 1 FOR SERVICING. THERE WAS A SET OF EQUIPMENT AT THE NORTH END OF S&I 1 PREPARING TO DEPART TOWARDS THE ST ORAGE TRACKS. THE OPERATOR IN THE DOUBLE SET FELL ASLEEP AND FAILED TO STOP SHORT OF THE EQUIPMENT. AS A RESULT OF THE IMPACT, 5 CARS (12 AXLES) WERE DERAILED CAUSING DAMAGE TO THE RAIL. THE EMPLOYE E INVOLVED WAS TAKEN FOR A DOT DRUG AND ALCOHOL SCREEN AND STATEMENTS WERE TAKEN FROM THOSE INVOLVED . THE EMPLOYEE HAS BEEN REMOVED FROM DUTY AND DISCIPLINARY ACTIONS TO BE APPLIED AFTER ROOT CAUSE AN ALYSIS IS COMPLETED. THE EMPLOYEE ON THE STANDING EQUIPMENT INJURED HIS BACK UPON IMPACT.",False,True,False,False,True,0.0
925,19,7,IC,22,GEISMAR,ASCENSION,"L51971-18 (IC 9637, GTW 6228) WAS PROCEEDING SOUTHWARD AT APPROXIMATELY 5 MPH WHEN SEVEN CARS DERAIL ED. CAUSE WAS DUE TO SURFACING ON THE TURNOUT, WHICH CAUSED AN OPEN RAISED WING RAIL.",False,True,False,False,False,0.0
926,19,11,ATK,36,GERMANTOWN,COLUMBIA,BOULDER/ROCK STRIKE: TRAIN 283 WAS PLACED INTO EMERGENCY AND DELAYED 2 HOURS AND 23 MINUTES AFTER S TRIKING A LARGE ROCK APPROXIMATELY 4 IN DIAMETER. THE CREW ALSO REPORTED EXTENSIVE DAMAGE TO ENGINE 701,False,False,True,False,True,0.0
927,19,8,BNSF,41,MADRAS,JEFFERSON,H-BAKPAS9-09 DERAILED 5 LOCOMOTIVES AND 1 RAILCAR WHILE TRAVERSING SINGLE MAIN TRACK DUE TO BOULDERS OBSTRUCTING THE TRACK. 4200 GALLONS OF DIESEL FUEL WAS RELEASED FOR THE LEAD LOCOMOTIVE.,False,True,False,False,False,0.0
928,19,5,UP,41,BAKER,BAKER,"MPDOG-01, LEAD LOCOMOTIVE UP553, THIRD ENGINE UP5694 WAS ON FIRE. NO DERAILMENT OR TRACK DAMAGE.",False,False,True,False,True,0.0
929,19,7,UP,22,DE QUINCY,CALCASIEU,"WHILE TRAVELING SOUTH, THE MLIHO-30, LEAD UNIT UP7518, TRAVELING AT 34 MPH STRUCK THE TRAILER OF A L OW BOY 18-WHEELER, TRACTOR-TRAILER ON THE CROSSING. NO INJURIES TO CREW OR DRIVER. SIGNIFICANT DAMAG E TO LOCOMOTIVE AND CROSSING DEVICES.",True,False,False,False,False,0.0
930,19,8,IC,22,ST GABRIEL,ASCENSION,RCL97971-28 WORKING ON THE SOUTH END OF THE YARD PULLED CARS OUT OF THE SOUTH END OF TRACK #1 AND DO UBLED TO CARS IN TRACK #3. THEY NOTICED 2 GAPS IN THE TRACK AND SHOVED TRACK #3 WITH THE INTENT TO COUPLE UP THE TRACK. AFTER COUPLING THEY PULLED SOUTH OUT OF THE TRACK AND DOUBLED TO THE MAIN. TH E RCL98271-28 CREW SWITCHING ON THE NORTH END OF THE YARD DICOVEDED THAT TILX401740 THEY KICKED TO T RACK #1 HAD SIDSWIPED UTLX900486 IN TRACK #3.,False,False,True,False,False,0.0
931,19,3,IC,22,RESERVE,ST JOHN THE BAPTIST,"AT 0530 CST ON MARCH 3RD, BATON ROUGE SUB, MP 419.6: CUSTOMER WAS IN THE PROCESS OF SHOVING EMPTY RE LEASES NORTHWARD FROM TRACK 2 ONTO THE CN LEAD AND INTO TRACK RS16 WHEN RAILCAR ICG 767387 SIDE SWIP ED RAILCARS CRGX 29287 AND GATX 94152. NO INJURIES OR DERAILMENTS REPORTED. ALL 3 RAILCARS SUSTAINED DAMAGES.",False,True,False,False,False,0.0
932,19,1,NS,39,BELLEVUE,ERIE,LB04 REMOTE JOB WAS HEADED EAST IN A7 WITH 19 SWITCH INDICATING PROPERLY ON THE GROUND AND ROUTE 4 B OARD WHEN DERAILMENT OCCURRED.,False,True,False,False,False,0.0
933,19,11,BNSF,6,BARSTOW,SAN BERNARDINO,Y-BAR2062-05 WAS PULLING TRACK 1430 A SECTION OF TRACK BROKE AWAY CAUSING 1 LOCOMOTIVE AND 3 CARS TO DERAIL. NO HAZMAT RELEASED.,False,True,False,False,False,0.0
934,19,9,UP,6,OAKLAND,ALAMEDA,"CAR CSXT620070 ARRIVED ON OAKLAND INTERMODAL RAMP (LOADED) WITH HEAVY DAMAGE TO THE (E) CELL OF THE CAR. NO RECORD OF WHERE THE DAMAGE OCCURRED OR WHO CAUSED IT. THE BODY OF THE E CELL WAS SPLIT ON THE L & R SIDESILLS. NO DERAILMENT OR TRACK DAMAGE. AFTER INVESTIGATION, IT APPEARS THE DAMAGE WAS DONE WHEN BEING LOADED.",False,False,True,False,True,0.0
935,19,11,UP,6,LONG BEACH,LOS ANGELES,"MWCLB-12 WAS SHOVING FROM PIER B YARD 7 INTO MEAD YARD TRACK 1. AFTER COMPLETING THE SHOVE, THE CON DUCTOR ASKED THE ENGINEER TO TAKE THEM AHEAD. THE TRAIN WENT INTO EMERGENCY WHEN CAR TTGX975197 CLI MBED THE WORN POINT ON THE FROG, CAUSED BY GUARD CHECK BEING LESS THAN MINIMUM ALLOWABLE LIMITS. WH EN THE TRAIN STRETCHED, THE CARS CAME APART AND STRUCK A CUT OF CARS THAT WERE IN TRACK 9. PHL MAIN TAINS TRACK. PHL TRACK DAMAGE = $44,138",True,False,False,False,True,44138.0
936,19,11,UP,6,TRAVER,TULARE,"GSTRSN-30, LEAD LOCOMOTIVE 2743, DERAILED INSIDE FOSTER FARM'S GRAIN FACILITY. INVESTIGATION FOUND THAT THE OUTLET GATE LOCKING MECHANISM AT THE BOTTOM OF HOPPER CAR FURX845222 WAS DAMAGED BY THE CUS TOMER DURING THE OFFLOADING PROCESS, AND SUBSEQUENTLY TRIGGERED THE DERAILMENT. INDUSTRY MAINTAINS TRACK",False,True,False,False,True,0.0
937,19,8,ATK,36,NEW YORK NEW YORK,NEW YORK,SWITCH/FROG: TRAIN 91 STOPPED JUST WEST OF `A` INTERLOCKING DUE TO SEVERE HI LOW CONDITION BETWEEN LOUNGE 28011 AND VIEWLINER 62005. ONCE TRAIN 91 SHOVED BACK TO NO.12 TRACK LOUNGE 28011 ALLEGEDLY R AISED THEN DROPPED BACK DOWN CAUSING OVERRIDING BUFFER PLATES BETWEEN THE TWO CARS. THE CAUSE WAS D UE TO A CONDITION WITH THE NO.107 FROG AND NO.107 SWITCH.,False,False,True,False,False,0.0
938,19,8,ATK,36,LONG ISLAND CITY,QUEENS,"AMTRAK CREW YSJ901 OPERATING NJTR TRAIN 3126 WITH NO PASSENGERS DERAILED ON THE EAST END OF SUNNYSID E YARD ON #18 TRACK, WITH THE REAR CAR C/1454 DERAILING AXLE 1 AND 2 , OVER THE HAND OPERATED SWITCH THAT LEADS TO # 17 AND #18 TRACKS FOULING #17 TRACK. THE HAND OPERATED SWITCH WAS LOCKED IN THE KE EPER AND THE FIRST 9 CARS PROCEEDED OVER THE SWITCH INTO THE #18 TRACK EXCEPT THE 10TH CAR C/1454.",False,True,False,False,False,0.0
939,19,8,MNCW,36,CROTON ON HUDSON,WESTCHESTER,HTS-6 WAS MAKING A SWITCHING MOVE IN BUILDING 6 WHEN THE BUFFER PLATE OF CAR 6390 A-END BUFFER WENT ON TOP OF THE B-END BUFFER OF CAR 6262. THE EXACT LOCATION OF THE INCIDENT IS UNKNOWN DUE TO MULTIPL E SWITCHING MOVES.,False,False,True,False,False,0.0
940,19,11,CSX,36,NIAGARA FALLS,NIAGARA,"B79416 PULLED INTO THE YARD FROM TRACK 2 TO THE NEW WAY. AFTER PULLING IN 5,117 FEET THE 85TH THROU GH THE 88TH CAR DERAILED DUE TO BROKEN RAIL.",False,True,False,False,False,0.0
941,19,1,GRS,36,HOOSICK,RENSSELAER,"VERMONT RAIL SYSTEM TRAIN DERAILED 8 CARS ON THE INTERCHANGE TRACK AT HOOSICK JUNTION NEW YORK. PART OF THE DERAILMENT WAS ON PAN AM RAILWAYS TRACK. DAMAGING TRACK AND SIGNAL PROPERTY.
VRS HAS A DETA ILED NARRATIVE EXPLAINING THE REASON FOR THE M507 CODE.
",False,True,False,False,False,0.0
942,19,1,ATK,36,BRONX,BRONX,PANTOGRAPH/CATENARY: TRAIN 2151 STOPPED ON 1 TRACK IN THE INTERLOCKING AT PELHAM BAY MP 15.0. THE CREW REPORTED STRIKING A WIRE HANGING FROM THE CATENARY AND DAMAGING THE PANTOGRAPH ON PC 2005.,False,False,True,False,False,0.0